ML19330A544
| ML19330A544 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 07/23/1980 |
| From: | Gallagher J PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | Grier B NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| References | |
| IEB-80-17, NUDOCS 8007280560 | |
| Download: ML19330A544 (2) | |
Text
_
PHILADELPHIA ELECTRIC COMPANY 2301 MARKET STREET P.O. BOX 8699 PHILADELPHI A. PA.19101
.e, lil/JJO.. ".',"m,
IWS DOCUMENT CONTAWS so.m m aui.^*
msi eu soo3 POOR QUAUTY PAGES July 23, 1930
- I r. 3oyce !!. Grier, Director Office of Inspection and Enforcement Region I US 'Jeclear Regulatory Commission 631 Park Avenue "ing of Prussi, PA 19406
Dear Mr. Crier:
This is in response to your letter of July 3,
- 19SO, which forwarded IE Bulletin 80-17 and contained a twenty-day ti.:e limit from the time of notification for performing acram testo described in the 3ulletin.
The twenty-day limit e :c p i r e s at 12:01 a.m.
on July 2d, 1980 Your letter also provided far an extension of this time if shutdown of a unit would severely impact the power reliability in our area.
Philadelphia Electric Company (PE) as part of the Pennsylvania - New Jersey - Maryland (PJM) power pool has been running all available generating equipment to meet the high power denands in ou r region.
The high temperatures, which the entire PJM area has been experiencing, have created all time high power demands for PE Company and PJM.
Long range forecasts are such that there is a likelihood that peak power demand could be repeated any time during the remainder of the sumner season.
Peach Bottom No. 2 Unit is presently in a refueling outage but is expected back in service by the end of July.
The scram tests on this unit will be completed before startup.
PJM advises that an outage of Peach Bottom No. 3 Unit at this time would severely impact the reliability in this region.
Because of the high power demands likely in this area and the critical location of Peach Bottom for supplying power and vitally needed voltage support to the PJM power grid, we are requesting that the required outage of No. 3 Unit be extended until the weekend of August 9, 1980.
It is expected that No. 2 Unit will be 1
8007389 60d
a
.e" Mr. Boyco !!. Crier Page 2 generating at full capacity by that time and an outage o f N' o. 3 Unit will be possible without severe effects on the power system.
The following measures have been taken to insure the operability of the Control Rod Drive system.
a)
A surveillance test has been initiated which strokes the scram discharge volume vent and drain valves daily to verify proper operation.
Valve position is verified and recorded in the surveillance log once per shift.
b)
The operability of the three gallon limit switch in the scram discharge instrument volume tank is verified during the daily surveillance test identified in item a.
c)
Procedures have been revised to provide additional instructions to the operators for a failure to scram.
Very truly vours, hN1 J
cc: Mr.
D.
Eisenhut Office of Inspection & Enforcement Division of Reactor Operations Inspection Washington, DC 20555
-