ML19329B928

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RO NP-32-77-01:on 770428,incore Instrumentation Installed W/O Direct Supervision of Licensed Senior Reactor Operator. Caused by Procedure Inadequacy.Procedure Modified to Meet Tech Specs
ML19329B928
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 05/10/1977
From: Batch S, Lingenfelter J
TOLEDO EDISON CO.
To:
Shared Package
ML19329B920 List:
References
NUDOCS 8002060913
Download: ML19329B928 (2)


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. SUPPLEMENTAL INFORMATION FOR LER NP-32-77.1 DATE OF EVENT: April 28, 1977 FACILITY: Davis-Besse Unit i ed IDENTIFICATION OF OCCURRENCE: Installing incere detectors in violation of Technical Specifications 3.9.2, 3.9.5 and 6.2.2e. Incore instrumentation was being installed without the direct supervision of a Senior Reactor Operator licensed person: there was no com=unication between Control Room and personnel at the refueling station; no audible source range indication in Containment and Control Room.

Conditions Prior to Occurrence: The plant was in Mode 6 with the Reactor Vessel i Head off.

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Description of Occurrence: At 0830 on April 28, 1977, began installing incore I instrumentation. After the nineteenth incore detector was installed at 1035, it was recognized this action was in violation of Technical Specifications.

[ The work was i=cediately suspended and a meeting of the Station Review Board was called to review the event.

Designation of Apparent Cause of Occurrence: This event has been determined to have been caused by procedure inadequacy in IC 2001.04, "Incore Detector Handling" and Replacement".

Analysis of Occurrence: The effect on reactivity coefficient of inserting the incore detectors into the initial core is insignificant. It is therefore con-cluded that the event.did not result in a threat to the health and safety of the public or to station personnel.

Corrective Action: A modification was made to the procedure to meet the Technical Specifications and allow the work to continue.

Failure Data: No previous similar events have occurred.

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DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-32-77-1 DATE OF EVENT: April 28, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Installing incore detectors in violation of Technical Specifications 3.9.2, 3.9.5 and 6.2.2e. Incore instrumentation was being installed without the direct supervision of a Senior Reactor Operator licensed person; there was no communication between Control Room and personnel at the refueling station; no audible source range indication in Containment and Control Room.

Conditions Prior to Occurrence: The plant was in Mode 6 with the Reactor Vessel Head off.

Description of Occurrence: At 0830 on April 28, 1977, began installing incore instrumentation. Af ter the nineteenth incore detector was installed at 1035, it was recognized this action was in violation of Technical Specifications.

O The work was immediately suspended and a meeting of the Station Review Board t 1 was called to review the event.

V Designation of Apparent Cause of Occurrence: This event has been determined to have been caused by proc 2 dure inadequacy in IC 2001.04, "Incore Detector Handling" and Replacement".

Analysis of Occurrence: The effect on reactivity coefficient of inserting the incore detectors into the initial core is insignificant. It is therefore con-cluded that the event did not result in a threat to the health aid safety of the public or to station personnel.

Corrective Action: A modification was made to the procedure to meet the Technical 3

Specifications and allow the work to continue.

Failure Data: No previous similar events have occurred.

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