ML19329B177
| ML19329B177 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 10/08/1975 |
| From: | Roe L TOLEDO EDISON CO. |
| To: | Schwencer A Office of Nuclear Reactor Regulation |
| References | |
| NUDOCS 8001300776 | |
| Download: ML19329B177 (7) | |
Text
__
NRC DISTHiBUTION FOR PART 50 DOCKET MA.uRIAL (TEMPORARY FORM)
CONTROL NO. 10820 I
FILE: _
FROM: Toledo Edir.on DATE OF DOC DATE REC'D LTR TWX RPT OTHER Toledo, Ohio Lowell. Rowe 10-8-75 10-10-75 XXX
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TO:
ORIG CC OTHER SENT NRC PDR A. Schwencer 1 Signed-0 SENT LOCAL PDR CLASS UNCLASS PROPINFO INPUT NO CYS REC'D DOCKET NO:
XXX 1
50-346 DESCRIPTION:
ENCLOSURES:
Letter Re. our letter of 7-7-75..Trans the Letter submitting info. pertaining to Partial Follcwing.....
Loop LOCA Analysisi.. W/ Attached table 1, and figure 1 & 2...
(1 Copy Enclosure Received)
PLANT NAME: Davis Besse
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s TDLEDO EDISON Docket No. 50-346 LOWELL E. ROE v.c. am....at Faciht.e. Deveicoment (419) 259-5242 October 8, 1975 egulatorf' RQfg
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e 0CT10ihhh:b, A. Schwencer, Chief Light Water Reactors Branch 2-3
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U.S. Nuclear Regulatory Commission
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Washin ;on, D.C.
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Dear Mr. Schwencer:
Enclosed is the information pertaining to Partial Loop Operation as rec,uested in your letter of July 7, 1975. This information will be submitted in Revision 16 to the FSAR as the response to your " Request for Additional Information No. 15.1.2".
To our knowledge this com-pletes the ECCS information which you have requested to date.
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THE TCLEDO EDISON CCMPANY EDISCN PLAZA 300 MADISCN AVENUE TCLEDO. CHIO 43652,1,Q @ g
Attrchment #1 Davis-Besse Nuclear Power Station Unit 1 Partial Loop LOCA Analysis This study shows that in the event of a LOCA during partial loop operatio'n, peak cladding temperatures and metal-water' reactions are significantly lower than that occurring for a similar break during four pump operation. The partial loop analysis was performed assuaing the worst case break (8.55f t DE, C "l) reported in BAW-10105 at the maximum D
Kw/f t which will be allowed by Technical Specifications for this mode of operation.
The maximum cladding temperature for the partial loop LOCA analysis is 1675F, which is 391F less than for the same break at full power and flow conditions.
There are 5 possible break configuracions at the pump discharge for partial loop operation:
1.-
3 pump operation a.
break in idle pump discharge b.
break in active pump discharge of loop with the idle pump c.
break in a pump discharge of loop with two active pumps 2.
2 pump operation, one idle pump in each loop a.
break in active pump discharge b.
break in idle pump discharge Analysis of the 3-pump operation instead of 2-pump operation was chosen for the following reasons. First, 3-pump operation is the more probable partial loop operational mode.
Second the rated power level for 3-pump operation is 77% of full power rating compared to 51% of full power rating for 2 pi aps operating. The reflooding rate will be lower for higher core power, thus a greater cladding temperature rise after
- - - > ~,
m m
,the end of blowdown (E0B) is expected for 3 pumps operating.
A break at the active pump discharge of the locp with the idle pump was anfalyzed. Large break LOCA's reported in BAW-10105 shcw that positive core flow remains highly positive during the initial phase of the blowdown transient. As the head of the RC pumps degrades, due to 2-phase effects, the magnitude of the positive core flow diminishes. The break flow rate dominates the second half of the transient and the core flow is reversed.
With 3 pumps operating about 43.5% of the RC flow is directed through the active pump in the loop with the idle pump.
Thus, placing the break at the d.ischarge of this pu=p would substantially degrade the positive flow through the core during the first half of the blowdown. This would result in high cladding temperature. Analyzing chis break location will ensure that the most conservative assumptions affecting core flow during the blowdows. transient have been considered.
The parameters used in the partial loop CPAFT and THETA models are consistent with the spectrum analysis reported in section 5 of BAW-10105, except for the following:
1.
The total plant power fo.: both cases analyzed is reduced to 77% of rated power for 3-pump operation. The peak linear heat rate fer the hot bundle is the maximum which will be allowed by technical specificatiens at tne 6 ft elevation for this mode of operation.
2.
Since there is a power imbalance between the loop with 2 active RC pumps and the loop wi:h 1 active RC pump, the load ratio between the steam generators is changed to 2.39:1 by controlling the feedwater flow to each steam generator.
3.
The flow and pressure distribution was modeled to reflect the imbalance caused by the idle pump and the reduction in the RC..
~
m v
flow to 75% of normal 4 pump operation. At steady state
- conditions the idle pump is locked in positian because flow is
. reversed in that cold leg. The flow proceeds from the idle t
pump to the lower plenum of the steam generator where it mixes
- and proceeds back to the reactor vessel through the active RC pump in that loop. About 14% of the RC flow, from the downcomer is directed back in the cold leg. If the flow reverses to the positive direction during the transient the idle pump would act as a free spinning rotor with no power.
Table 1 summarizes the results of the partial loop analysis and compares those results to the worst break reported in BAW-10105. Figures 1 and 2 show respectively peak ruptured and unruptured node cladding temperatures for the hot pin and the core flow for 3-pump operation with the break located 'at the active pump of the loop with an idle pump. The maximum cladding temperature is 167F5 at 12.5 seconds.
Examination of the core flow, Figure 2 of this report and Figure 6-9 of BAW-10105, reveals a distinct difference in the flow transient. With a break at the
~
pump discharge of the active pump, the positive to negative flow occurs earlier, approximately 11 seconds c>mpared to approximately 15 seconds for the 4-pump case. The negative flow is increased due to the decrease fre= 3 to 2 cetive pumpe in, the unbroken cold legs trying to force the flow into the vessel. This large negative flow through the core provides good cooling lowering the cladding temperature to below 1100 F near the E0B, thereby preventing rupture and blockage during the blowdown phase of the LOCA.
The hot pin cladding temperature response, calculated with the i
' THETA code,- predicts rupture after the E0B at 32.0 seconds. The ruptured node cladding temperature decreased rapidly af ter rupture because of the 1
,1
-~
reduced gap heat transfer from the fuel to the cladding and the increase in the, surface area for cooling. The reflooding heat transfer coefficients, which'are higher than those reported in BAW-101C5 due to the lower pin power, are high enough to prevent a rise in the rupture node cladding temperature following rupture. The low cladding temperatures throughout the LOCA produce a smt.11 amount of local rietal water reaction, 0.54%,
which is significantly lower than during 4-pump operation.
The containment building pressure calculated by the CONTEMPT code is similar to the worst case shown in Figure 6-12 of BAW-10105. The cladding temperatures experienced fer the partial loop cases analyzed are considerably lower than those for 4-pump operation reported in BAW-10105. The ma mum cladding temperature for the partial loop LOCA analysis is only 1675F compared to 2066F for the worst 4-pump operation break as reported in Section 6 of BAW-10105.
D,
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TABLE 1
- Comparison of 8.55ft DE break at pump discharge, C =1.0, with D
4 and'3 pumps operating.
3-pumps, break at active pump in loop 4-pumps (BAW-10105) with idle pump Case Number (CRAFT)
T0420 (30)
PP201 (9N)
Per Cent Power (100% Power = 2772) 102 77 Peak Cladding Temp unrupt/ time, F/s 2066/66 1672/12.0 Peak Cladding Temp rupt/ time, F/s 1914/43 1675/12.5 Rupture Time / blockage e/%
16.3/68.6 31.99/70 CFT actuation time, s 16.61 16.73 End of bypass, s 24.62 24.2 End of Blowdown, s 24.62 24.2 End of adiabatic heatup, s 34.02 34.2 Water cassin reactor at end of blowdown, iba 2916 1682 Local metal-water reaction, % 3.11
.545
- Computer codes utili:cd Code Name Version Number Version Date CRAFT CRAFT 2 VERSION SPP 4/17/75 REFLOOD 2
12/20/74 CONTEMPT 15 11/15/74 THETA-1B 6F 1/23/75 l