ML19326C778

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Submits Info Re ECCS Small Break Analysis Per NRC Request. Full Power Operation W/One Operating Makeup Pump Combined W/ Proposed Interim Fix Considered to Provide Substantial Margin to 10CFR50.56.Tech Specs Change to Be Requested
ML19326C778
Person / Time
Site: Arkansas Nuclear 
Issue date: 04/21/1978
From: David Williams
ARKANSAS POWER & LIGHT CO.
To: Reid R
Office of Nuclear Reactor Regulation
References
1-048-15, 1-48-15, NUDOCS 8004280713
Download: ML19326C778 (2)


Text

NR0 '" r.M 495 U.S. NUCLEAR CEGULATORY (

WSSION OCCKET NUMIE R 12 7ei SD 3/3 NRO DISTRIBUTION roR PART 50 DOCKET MATERIAL lTO:

Mr. R.W. Reid FROM: Ark. Power & LLight Co.

DATE F0 UMENT f

Little Rock, Ark.

72203 D. H. Williams DATE El O

25.ETTE n CNoToRtzED PROP INPUT FORM NUMBER OF CDPtES RECEIVED CORio:NAL MC LAS$1FIE D WC0" t

reL2W cEsCRIPTION Ltr furn addl inf0 On ECCS small ENCLCSURE l

break analysis interim solution....1P 3

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THis DOCUMENT CONTAlNS POOR QUAUTY PAGES E

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April 21, 1978 I

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L 1-m e-is li Director of Nuclear Reactor Regulation ATT't:

Mr. R. W. Ruid, Chief f

Operating Reactors Branch f4 l

l1. S. Nuclear Regulatory Co:rission

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Washington, D. C.

20535 i

Subject:

Arkansas Nuc1 car One-Unit 1 Docket No. 50-313 j,

1,1 cense No. DPR-51

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h Raportable occurrence No. 50-313/78-9 ECCS Scall Break Analysis i

Interim Solution (File: 0520)

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centie:.en:

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As a followup to Mr. Ruater's letter on the above captioned i

subject earlier today, the following infor ation is provided in response j

to Mr. Vissing's requests for additional information.

p Based on cos:unication with BW ve believe that 100% Tull Powar (FP) op.: ration with one :sakeup pump in operation co.nbined with our proposed lateria fix provides substantial margin to 10CFR50.46.

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  • te vill submit the results of the Br4 analysis including break spectru:n, h,

identification of worst break, justification for adequacy of core uncovery F

ta=peratures, and justification that ti=c scale for operator is within y

analysis assu=ptions, as soon as they are available.

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'Je will subnit a Technical specification change request (per your request) as appropriate to imple=ent the interim fix.

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We v111 submit a proposal for a 1cng term fix, with 1sss ra11ance on a g ']

high state of operator readiness, within three (3) ::enths of this date.

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Very truly yours.

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S Daniel H. Wil11ans f

Manager, Licensing DW:J!Et tv c

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