ML19325E678

From kanterella
Jump to navigation Jump to search
Part 21 & Deficiency Rept Re Broken Swing Arm in High Pressure Swing Check Valve at Plant.Initially Reported on 890620.Failure Analysis on Broken Swing Arm Being Performed
ML19325E678
Person / Time
Site: Comanche Peak  
Issue date: 10/02/1989
From: Godwin G
BW/IP INTERNATIONAL, INC. (FORMERLY BYRON JACKSON
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
REF-PT21-89, REF-PT21-89-192-000 CFRN-8901, PT21-89-192, PT21-89-192-000, NUDOCS 8911080240
Download: ML19325E678 (5)


Text

_- w pg,

p j.;

svF,,,.

l BW/IP htern:ti:n:1, Inc.

.e.

I

' P O Dok Los Angeles Telephone l

p P01F Cahlornia F13 6B7 (,171 me i

lorminal 90051 Teles pg,

Annen c.rnas Ceestrifugal yg3 99 p:q)g Pumps Pung Omskm

.2 October 1989 l"

i Administrator, Office of Inspection c

and Enforcement, Region V L

U. S. Nuclear Regulatory Commission F

1450 Maria Lane, Suite 210 Walnut Cteek, California 94596 Gentlemen:

i This letter transmits a notification of defects, and nonconformances I

required by 10CFR - Part 21. The attached notificatAon, CFRN-8901, reports a condition which occurred st Texas Utilities Comanche Peak Steam Electric Station.

Very'truly yours, G. C. G dwfn Manager Los Angeles Operations CCG/ah P

Attach:

3 Copies of Notification i

cc:

Mr. F. J. Borgers, Vice President Operations Mr. E. B. Fiske, Directer of ngineering Mr. R. D. Ham, Manager of Quality Dr. S. Gopalakrishnan, Manager of Engineering 9

D S 100 60 Dr. K, A. Huber, Technical Liaison Mr. W. A. Klenner, Project Manager A N01038 CUN 03Al3038 9911080240 891002

{

'\\

PDR ADOCM 05000445 S

PNU E

IL~

I3

q' l T Q N '. 'qm;. Mv'

.. g 1

,;o
3. j ; ys e;s

,c

v.

9<

...r-

,y>

.F,-

N.

'i' h(

10 CFR PART 21 NOTIFICATION ~

f 3

%

  • q?l (Reference No..CFRN-8901)'

NAME AND ADDRESS-OF THE INDIVIDUAL' OR INDIVIDUALS INFORMING THE COMMISSION: ~-

,x

.v>

Mr. G,-C.'Godwin

[W'

' BW/IP' International, Inc.

[

<O.,

. Pump. Division Los Angeles'0peration

'2300-E. Vernon Avenue

,g

' Ve'rnon, ; CA, 90058.-

s 5

(213) 587,,171 4

lf For Technical Information

Contact:

Dr. Kent Huber i

'.6 -.

IDhNTIFICATIONOFTHEFACILITY,THEACTIVITY,ORTHEBASICCOM-i l'

PONENT SUPPLIED FOR SUCH FACILITY OR SUCH ACTIVITY WITHIN THE. UNITED.

' STATES WHICH FAILS TO COMPLY OR CONTAINS A DEFECT:

1 y,

7 s

Texas Utilities, Comanche Peak Steam Electric. Station.

'f y.-

Basic Component, High Pressure Swing Check Valve. Serial No'..17145 i

q.

Drawing No. 76490.- Texas Utilities Tag'No. lSW-048.

i i

.1

^

i s,.

[

7-6

^

U (IDENTIFICATION OF THE FIRM CONSTRUCTING THE FACILITY OR SUPPLYING THE BASIC COMPONENT WHICH FAILS TO COMPLY OR CONTAINS A DEFECT:

i g

BW/IP International, Inc.

?

Successor to:

(

Borg-Warner Nuclear Valve Division

(

g..

7500 Tyrone Avenue

?

Van Nuys, CA 91409

.7 c

l-E

.g I I I

<..,).

Paco 1 of 3 1,

4 p

cu

-,7

.---w 3--

?

(fll llI' o-

  • <-J :s,s c

i2

5l:,

10' CFR, Pirt ' 21, NotificOtion t

[p,

  • R.

(Ref. No..CFRN-8901) vi i2 C

NATURE OF THE' DEFECT 'OR' FAILURE 'ID COMPLY AND THE SAFETY HAZARD WilICH plh IS CREATED OR COULD'BE CREATED BY SUCH DEFECT OR FAILURE TO COMPLY:

' Nature of Defect:

.The' swing arm in,the valve was found broken-during an inspection at the.

Comanche Peak Steam Electric Station.

Safety hazard whichfiw created or

could'be created is' unknown, due to insufficient knowledge of component S'

. service and. mode ofLoperation.

U' w

Y (E 1.

. ). '

F*

h THE DATE ON WHICH THE INFORMATION OF' SUCH DEFECT OR FAILURE' TO COMPLY D

WAS OBTAINED:

1 g

The incident was intially reported to BW/IP-International'on.

20 June 1989. Additional information concerning the failure has K

't

' subsequently.been: supplied by Texas Utilities.

i'

[-

l r

p u

.IN THE CASE OF A BASIC COMPONENT WHICH CONTAINS A DEFECT OR FAILS TO COMPLY, THE NUMBER AND LOCATION OF ALL SUCH COMPONENTS IN USE AT, SUPPLIED FOR, OR BEING~ SUPPLIED FOR ONE OR MORE FACILITIES OR ACTIVITIES SUBJECT TO THE REGULATIONS IN THIS PART:

Initial investigation of the failed component has indicated no defects or failure to comply, nor has BW/IP received any notification of similar failures in.like components in operating plants with many years of service (see' Attachment A).

l l

I b

4 Page 2 of 3 i

i e

l j

S

~ j,

{ww"J.,- q; 10: CFR, P2rt 21,[Notificitions w'. :

P

. Di (Ref. No. CFRN-8901)=

{g I

c f

itl,

[

THE CCRRECTIVE' ACTION '!HICH HAS-BEEN, IS BEING, OR WTLL DE TAKEN; THE HAME. O.t THE INDIVIDUA*a OR ORGANIZATION RESPONSIBLE FOR TIIE ' ACTION; AND' Td? if7A' OF TE4E THAT HAS BEEN OR WILL BE TAKEN TO COMPLETE THE K

.a :

- ACTION:-

"c, Texas Utility.is performing a failure analysis on the broke" arm. As i*

' ~

W <of this date BW/IP-International has not completed'their review of.

this effort'. After the review is complete, BW/IP.will perform an

. independent evaluation as appropriate.-

\\

t

,4 s

4 t

m F
e r

l.

A1:Y ADVICE RELATED TO THE DEFECT OR FAILURE TO COMPLY ABOUT THE FACILITY.t ACTIVITY, OR BASIC COMPONENT THAT HAS BEEN,' IS BEING, OR WILL BE GIVEN' TO PURCHASERS OR LICENSEES:-

To date this is the only known instance of a swing check valve arm-f ailure of any. Borg-Warner Nuclear Valve.

However, BW/IP will inform customers of this failure.

p F

(1 )

{

Pace 3 of 3 y

g; J*:

ygt ;

i jc,

$ k l

, e j

0..p a

'j f.

'i

\\

k't*

E ATTACHMENT A u

I g,

4 TO I

('

10CFR, PART 21 S

(REF. No. CFRN 8901) l L~

P i

) -.

(L.

'1.-

Florida Power & Light, St. Lucie Station U

i 2.

Texas Utilities Generating Co., Comanche Peak Station 3.

Washington Public' Power Supply System, WNP 3 SATSOP l

b 4

~ Tennessee Valley Authrity. Browns Ferry Station

}

-f i.

5.

Tennessee Valley Authority, Watts Bar Station i.

6.

Arkansas Power and Light, ANO-1 I

(;

7.

Arizona Public Service Co., Palo Verde Station i'

8.

Cleveland Electric Illuminating Co., Perry Nuclear Station i

i 9.

Duke Power Company,!!cGuire Station 10.

Duke Power Company, Catawba Station 11.

Societe Belgo-Francaise d'Energie, Tihange Station

'[

12.

Taiwan Power Company, Maanshan Station l

13.

Nuklearna Elektrana Krsko, Krsko Station P

'h e

(

i.

k

(

-P t

M-I,