ML19323J319

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Part 21 Rept Re Failed Engine Thrust Bearing.Diesel Generator Sets Were Inspected in Accordance W/Written Procedures & Revised Drawings.Generators Are Free of Reported Potential Defect
ML19323J319
Person / Time
Site: Summer 
Issue date: 06/06/1980
From: Moriarty J
COLT INDUSTRIES, INC.
To:
References
REF-PT21-80-191-005 NUDOCS 8006200012
Download: ML19323J319 (2)


Text

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ATTACHED IS A PART 21 REPORT FROM IE f%IL [ BIT - ROOM 359E/W 3

PART 21 IDENTIFICATION [0, 76-/9/-oor COMPANY llVE 044/ cLaa&u:,

DATE OF ETTER 6/AI/#

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DATE DISTRIBlITED tho/ ro ORIGINALREPORT SUPRHERARY Z DISTRidfTION:

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REACTOR (R)g FUEL CYCE &

SAFEGUARDS (S) f%TERIALS(M)

NRR/ DOR, DIRECTOR (2)

AD/FFMSI AD/SG-IE NRR/DRi DIECTOR (2)

NES/FCMS AD/RDI AD/ROI ( 2 )

EGIONS REGIONS AD/RCI IE FIES NRR/ DOR, DIRECTOR

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REGIONS PDR NMSS/SG SS-881 IE FIES LPDR PDR CENTP/L FIES CENTRAL FIES-SS-396

[PDR CBURAL FIES (CHR0iO TERA CBITgAL FIES(CHRON)

(016 PDR IE FIES (2)

IfDR CENTRAL FIES 016 Qg)

L0EB/fPA NB 5715 CENTRAL FIES (CHRON)

AE0D - MBB-7602 CBERAL FIES - SS-396 E/fPA' MB 57E AE0D PTBB-7602 LDEB/fPA N B 5715 AE0D MD3-7602 ACTION:

PRELIMINARYEVUALATIONOFTHEATTACHEDREPORTINDICATESLEADRESPONSIBILITYFOR FOLLOW-UP AS SH0hN BELGV:

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Colt industries

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608<364 441I aasac.3 ilune 6,1980 g,,g,g Office of Inspection & Enforcement g _ ) cf f-o oy U. S. Nuclear Regulatory Comission 199 Roosevelt Road Glen Ellyn, Ill. 60137 i

Attention: Mr. James G. Keppler, Director, Region III

Subject:

Colt Industries-Fairbanks Morse Engine Division Enwrgency Diesel Generators SNUFPS Contract Part 21 Paco-t-Failed Engine Thrust Bearing Supplement No.1-South Carolina Electric &

Gas Co.-Sumer Station Gentlemen:

We have completed our inspection of the two Colt-Pielstick Type PC-2 Diesel Generator Sets installed at South Carolina Electric & Gas Co.-Surnmer Station. These inspections were made to written procedures utilizing the j

revised drawings mentioned in our May 2,1980 report which provide adequate clearance. Both units are in compliance with the ins [ection procedure and are free of the reported potential defect.

A copy of this report is being forwarded to the utility involved.

Very truly yours, f

. M.

ty MANAGER UTILIT JMM:je i

cc: South Carolina Electric & Gas Co.

P. O. Box 764 Columbia, South Carolina 29218 Attention: Mr. Dan Nauman Manager, Quality Assurance & Security U. S. Nuclear Regulatory Commission c/o Document Management Branch g

91980 Washington, D. C. 20555

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