ML19323C559
| ML19323C559 | |
| Person / Time | |
|---|---|
| Site: | Maine Yankee |
| Issue date: | 04/12/1980 |
| From: | Beers F Maine Yankee |
| To: | |
| Shared Package | |
| ML19323C556 | List: |
| References | |
| NUDOCS 8005160328 | |
| Download: ML19323C559 (5) | |
Text
S0051603/1!I 8
O v
MAINE YANKEE NUCLEAR POWER STATION MONTHLY STATISTICAL REPORT 80-04 FOR THE MONTH OF APRIL, 1980 l
OPERATING DATA REPORT DOCKET NO. 309 DATE Rnna19 COMPLETED BY F.
G.
Beers TELEPHONE 617-366-9011' X2215 OPERATING STATUS Maine Yankee Notes
- 1. Unit Name:
Power restricted by
- 2. Reporting Period:
April 1980 steam fics through the LP
- 3. Licensed Thermal Power (>!Wt):
2630 Turbine.
864
- 4. Namepiste Rating (Gross 5!We):
825
- 5. Desi n Electrical Rating (Net 31We):
2 850
- 6. 31sximum Dependable Capseity (Gross 31We):
report period.
810
- 7. Sf aximum Dependsble Capacity (Net S!We):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
- 9. Power Level To Which Restricted.If Any (Net 31We):
- 10. Ressons For Restrictions.!f Any:
This 5fonth Yr..to.Date Cumulative 719*
2,903.00
- 11. Hours In Reporting Period
- 12. Number Of Hours Resctor Was Critical 710.93 1.480.50 52.690.50 0.0 0.0 0.0
- 13. Resetor Reserve Shutdown Hours
- 14. Hours Generstor On.Line 707.70 1.350.06 -
50,867'87
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (31WH) 1.719.186.00 2.717.275.00 107.979.358.00
- 17. Gross Electrical Energy Generated (MWH) 57R R10._00 901.170.00 15.47A.550.00 18l Net E!ectrical Energy Genersted (MWH) 552,202.00 855,275.00 33,682,462.00
- 19. Unit Service Fsetor 98.43 46.51 77.63
- 20. Unit Availability Factor 98.43 46.51 77.63
' 21. Unit Capseity Factor (Using 3!DC Net) 94.82 36.37 66.73 j
- 22. Unit Capacity Factor (Using DER Net) 93.09 35.71 64.47 1.57 4.84 6.83
- 23. Unit Forced Outsge Rate
- 24. Shutdowns Scheduled Over Next 6 Stonths (Type. Date.snd Durstion of Each1:
l l
l
- 25. If Shut Down At End Of Report Period. Estimated Dste of Startup:
- 26. Units In Test Ststus (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
'(9/77).
AVERAGE DA!LY UNIT POWER LEVEL
- DOCKET NO.
50-309 UNIT Maine Yankee 800412 DATE F. C. Beers C05fPLETED BY 617-366-9011 X2215 TELEPHONE 5!ONT11 April 1980 DAY AVERAGE DAILY POWER LEVEL
^
DAY AVERAGE DAILY POWER LEVEL (51We-Net)
C.!We Net) 781
- 7 820-2 437 13 822 3
522 19 821 4
_ 804 20 824 5
811 21 816 011 6
22 819 814~.
7 23 821 8
813 24 791 9
All 25 749 10 810 26 634 812 1I 27 628-717 32 814 23 812 13 29 721 34 816 30 714 IS 824 31 16 822 INSTRUCTIONS On this formst. list the aversge daily unit power levelin 31We-Net for each day in the reporting month. Compute to the nearest whole me swatt.
(9/77) 9 0
UNITSilUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-309 UNIT NAME flaine Yankee DATE 800412 COMPLETED fly F.
C.
Beers REPORT MONTil April 1980 TELLPl!ONE 617-166-9011 x2215 "i
.s_
e.
.3m e e
.= c g
m.s x Licensee c-r.
c 7.
Ca.ise & Corrective No.
Date g;
3g
,g g 5 Event g
h Action to
}u Psevent itecursence
[25 5, j5g Report #
in O 6
L.R. ti 3/29/80 F
86.18 11 1
N/A CC ZZZZZ Load reduction to help leach residual 20%
thru chlorides out of the steam generators 4/2/80 4-80-5 4/2/80 F
11.30 A
3 N/A IA INSTRU-T A grounded capacitor in a S/C level transmitter led to a reactor trip during routine RPS surveillance testing.
L.R.
4/24/80 S
157.67 11 1
N/A RC ZZZZZ Load reduction due to increasing to plus core D/P. NII 0ll was added to help 4
75%
remove the apparent buildup of crud on core surfaces.
I 2
3 4
F: Fost ed Iteason:
Method:
Exhibit G -Instructions S: Sdicduled A Equipment Failuie(Explain) 1 Mannal for heparation of Data fl Maintenance of Test 7 Manual Scrain.
Entry Sheets fin I.iecusee C IteIucting 3 Automatic Scram.
Event Itepint (LElt) File INUltEG.
D.Hegulatony itesiriction 4 Other(lixplain) 0161) li Opciator Tsaining & License Examination F Aihninistiative 5
G Operational I not (limplain)
Exhibit I Same Source t's/17)
Il-Othes (limplain)
o DOCKET NO.
50-309 UNIT Maine Yankee DATE 800412 COMPLETED BY F. C. Beers TELEPHONE 617-366-9011 X2215 REPORT MONTH April 1980 SIM!ARY OF OPERATING EXPERIENCES At the beginning of the month the plant was in the process of a slow (1%/hr.) power escalation from N92% to full load following a load reduction to help soak out chlorides in the steam generator.
At 1311 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.988355e-4 months <br /> on 4/2/80, a plant trip occurred (from 96%) during routine RPS surveillance testing. The cause was due to a grounded capacitor in one of the steam generator level transmitters. The reactor was taken critical later that day and the unit was phased to the grid at 0029 ho,urs on 4/3/80.
The plant remained at full load until 4/24/80 when reactor power was reduced to 90%. The reason for the load reduction was due to an increase in the reactor core D/P. It is believed that increased crud deposits on core surfaces have caused the increase in D/P. On 4/25/80, load was dropped from 90% to 75% and NH 0H was added to the RCS in an attempt to 4
remove some of the crud buildup.
Following the NH 0H additions (which were not considered successful 4
as far as crud cleanup considerations), power was raised up.to 85% and held there for the remainder of the month. Preparations were made to take the plant off the line over the 5/3/80-5/4/80 week-end, cool the plant down and add H 0 as a mechanism for core crud removal.
22 e