ML19323B465
| ML19323B465 | |
| Person / Time | |
|---|---|
| Site: | Trojan File:Portland General Electric icon.png |
| Issue date: | 05/05/1980 |
| From: | Bair G PORTLAND GENERAL ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML19323B462 | List: |
| References | |
| NUDOCS 8005120405 | |
| Download: ML19323B465 (4) | |
Text
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i 80051A0'/45 OPERATING DATA REPORT DOCKET NO.
- n v. /.
DATE 5-5-80 C051PLETLD 3Y l'
'ir TELEPil0NE W 7 ' "
Ext. 234 OPERATING STATUS Notes Troian Nuclear Plant
- 1. Unit Name:
April 1980 4
- 2. Repo tin; Period:
34Il
- 3. Lbnsed Thermal Power i.NIWtl:
1216
- 4. Nameplate Rating (Gross 31Wel:
1130
- 5. Desi;n E!eetrical Ratmg (Net 5the):
11 ~ '
- 6. Staximum Dependable Capacity (Gross SlWe):
1080
- 7. Staximum Dependable Capacity (Net 5the):
- 8. If Changs Occur in Capacity Ratin;s (Items Number 3 Through 7) Since Last Report.Give Reasons:
- 9. P: wer Lesel To Which Restricted. If Any (Net 5!We):
- 10. Reasons For Restrictions. If Any:
l This Sionth Yr to-Date Cumulatise 719 2903 32111
!!. Ifours 1:. Reterting Pe iod 257.7 2422 18720
- 12. Number Cf !!oun Reactor Was Critical 0
0 2171.8
- 13. ".eactor Resene Shutdown Haurs 257.4 2416.7 18044.5
- 14. Ilours Genrrator On Li. e 0
0 1508.7
- 15. Unit Resene Shu:down liours 560119 6839434 55735043
- 16. Gross Thermal Energy Generated (5thil) 178165 2203790 18189205
- 17. Gross Electrical En:+:y Generated (StWH) 164714 2094975 17128294
- 18. Net Electrical Energy Generated (51WH) 35.8 83.3 56.2
- 19. Unit Sen-ice Factor 35.8 83.3 60.9
- 20. Unit Avai! ability Factor 21.2 66.8 49.4
- 21. Unit C.,r1 city Factor (Using AIDC Net) 20.3 63.9 47.2
- 22. Unit Caracity Factor (U>ing DER Net) 0 1.0 27.8
- 23. Unit Forced Outa:;e Rate
- 24. Shutduwns Scheduled Over Next 611onths 1 Type. Date.and Duration of Each):
1 June 1980 f
- 25. If Shut Down At End of Rc;iort Period. Estimated Date of Startup:
- 26. Units in Test Status tPrior to Commercial 0peration):
Forecast Achiesed NA NA INITIA L C:tITICALiTY MA NA INITIAL ELECTR! CITY CONINIERCl NL 0;'ER ATION NA NA i
6/77) l w
..-_y.
. _ = _ _.
i t
APPENDIX B
[
AVERAGE DAILY UNIT l'OWER LEVEL l
i DOCKET NO.
50-344 UNIT TrM an DATE 5-5-80 COhlPLETED BY c. G. Bair TELEPilONE 556-3713 Ext. 234 hlONT!!
April 1980 l
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL
($1We-Net)
(SIWE-Net) 1 648 17
-3 647
-3 2
18 3
654
-3 is 651'
-3 4
20 g
655 21
-3
'\\
G
-656 22
-2 j
f 7
654
-2 23 8
650 j
24
-3 3
g 648 25
-3 645
-2 10 26 gg 442
-2 27
-17
-2 12 28 13
-7
-3 29 14
-10 30
-3 15
-8 31 NA 16
-9 4
INSTRtJCTIONS On this form, hst the average daily unit power level in 51We Net for each day in the reporting month. Compute to the nearest whole megawatt.
l
'lhese figures udl be used to plot a graph for eJeh reportinj month. Note t lat when nuumum dependable caluelty is T
i l
used for the net c!cettical ratmr. ol' the unit. thae may be occasions when the d.nly averare power lesci exceeds the j
100'J. hne (oi th. restristed power level i:ne). In sush cases, the average dady umt power output >heet should be footnoted to esplain the apparent anonuly l
1.16 3 l
i
DOCKET NO.
50- W UNIT SI'UTDOWNS AND POWER REDUCTIONS UNIT N A*.!E l'":"
DATE 5-5-80 CO3tPt. Ell D I;Y C t'-
REPORT MON 111 Anri1
) ;1,,,llON E W ;
1 Ext. J 'l '.
w.
E E
.$ E 3
f.Eii Licensee E 3,
[*'.,
Cause & Coere. tise Nis.
DJte i
E?
si
.3 s s Esent 3?
9-8 Attion to H
fE 3 ;f3 g Reporl #
'N O SU Pievent Recurrence e
O O
80-04 800411 S
461.6 C
1 NA NA NA NA I
2 3
4-F: Forced Reason:
Method:
Exhibit G-Instructions S: Scheduled A.I'eguipment Failure (Explain)
I-Manual for Preparation of Data B. Maintenance of Test 2 Manual Scram.
Entry Sheets for Licensee C-Refueling 3 Autonutic Sc.am.
Event Repost (LER) File (NUREG-D Rei.utatory Restriction 4-Other (Explain) 0161) l~ Opesator Training 1 Ucense Examination F-Admir.ht ra:ive 5
G-Ores.itienal Es ros (Explain)
Exhibit I-Same Source 0;f77)
Il Oshes (Expl.ti:0
DOCKET NO:
50-344 i
j DATE:
5-5-80 i
COMPLETED BY:
G. G. Bair TELEPHONE:
503-556-3713 l
Ext. 234 I
SUMMARY
OF OPERATING EXPERIENCE OPERATION:
The plant began the month at reduced power coastdown as required to reach the refueling date. The plant shutdown on 4-11-80 for the Cycle 2-3 refueling.
The fuel movement began on 4-24-80.
The spent fuel examination program discovered two fuel assemblies (D38 and C18) that sustained extensive fuel damage to a single rod in each assembly.
l The fuel rod damaged was located at the third pin position in from the corner and was immediately facing the outside core baffle plate joint.
It is speculated that the internals baffle plate joint gaps are slightly open permitting water-jet impingement on a single fuel rod of certain perimeter assemblies.
3 MAJOR SAFETY-RELATED MAINTENANCE:
Work continued on improvement modifications to the Plant Security and Fire Protection Systems.
Work began on the removal for analysis of 29 steam generator D Row 1 tubes.
1 Work began on Inservice Inspection of Class 1, 2 and 3 equipment.
Work began on Local Leak Rate Testing.
I
- )
Work continued on radiographic examination of feedwater lines for cracks.
Work continued or. modification of piping systems restraints and supports.
Work began on several TMI-related design modifications (RV head vent, RV water level, containment water level, post LOCA environment electrical equipment assessment, safe shutdown remote instrumentation and decouple switches, separate power supply to steam PORV and AFWP pressure instrument).
Work continued on masonry wall inspection, review and repair.
Work began on MSIV inspection and investigation.
LICENSE CHANGES:
Amendment #43, LCR-TNP-80-02, LCA-59; Changed temporarily the surveillance interval associated with control rod drop testing to permit an extension of two days.
MISCELLANEOUS:
Small amounts of tremors and volcanic activity continued at Mt. St. Helens sporatically throughout the month.
Though no lava has been discharged, local mountain deformations and tremors ranging up to 4.5 Richter have occurred. No plant seismic movements have been measured.
The ASLB hearings on the Control Building seismic modifications recommenced on 4-16-80 and concluded on 4-17-80.
The NRC Staff agrees with PCE's analysis of the adequacy of the proposed modifications.
Turbine-generator high pressure cell inspection and CV overhaul began.
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