05000267/LER-1980-017-03, /03L-0:on 800311,w/plant Shut Down Due to Loss of Main Cooling Water Return Line,Plant Liquid Effluent Sample Required by SR Nr 1.1 Not Taken.Caused by Preempted Time Due to Plant Upset.Sampling Resumed on Next Shift

From kanterella
(Redirected from ML19323A516)
Jump to navigation Jump to search
/03L-0:on 800311,w/plant Shut Down Due to Loss of Main Cooling Water Return Line,Plant Liquid Effluent Sample Required by SR Nr 1.1 Not Taken.Caused by Preempted Time Due to Plant Upset.Sampling Resumed on Next Shift
ML19323A516
Person / Time
Site: Fort Saint Vrain 
Issue date: 04/09/1980
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19323A513 List:
References
LER-80-017-03L, LER-80-17-3L, NUDOCS 8004210296
Download: ML19323A516 (1)


LER-1980-017, /03L-0:on 800311,w/plant Shut Down Due to Loss of Main Cooling Water Return Line,Plant Liquid Effluent Sample Required by SR Nr 1.1 Not Taken.Caused by Preempted Time Due to Plant Upset.Sampling Resumed on Next Shift
Event date:
Report date:
2671980017R03 - NRC Website

text

. _ _ _

l NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (7 77)

LICENSEE EVENT REPORT CONTROL BLOCK: l l

l l

l l

lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) l 6

f0Til Ic lo ir IS Iv 11 l@l ol ol -l of ol ol ol ol -l of al@l4 11 11 12 lo l@l l

l@

7 8 3 LICENSEE CODE 14 15 uCENSE NuM8ER 25 26 UCENSE TYPE JO

$7 CAT $8 CON'T IOI1l Eu'RC lL ]@l0 l5 l0 l0 l0 l216 l7 @lo 13 l1 l1 l8 lo l@l0 l4 lo l9 l8 l0 l@

I 8

60 61 DOCK ET NUM8ER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l o 12 l l On March 11, 1980, with the plant shutdown, due to the loss of a main cooling water l

I o 13 l l return line, plant liquid effluent sample required by SR NR 1.1 was not taken. Therel I o 14 l l was no effect on public health or safety, and no related reports.

l Io Isl I I

lo is i l l

I o 17 I I I

I o la i i I

80 7

8 9 E

ODE SU C E COMPONENT CODE SU8C O'E SU E

ITTTI l a l F l@ yh W h l P l I l P l E l X l X lh Wh [Z_j h 7

8 9

10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LER EVENT YEAR R EPORT NO.

CODE TYPE NO.

@ sug/RO 18 10 I l-l I o f 1171 1/l 10131 It I l-l L.o_J as

_ 21 22 23 24 26 27 N

N 30 31 32 K N AC O O P NT ME HOURS S8 i FOR 8.

SUP L E MANUF RER LxJ@L7J@

LzJ@

L7J@

l n' of ol of LtJ@

W@

Ld@

lsiol8I91@

33 34 JS 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l i l o l l operations personnel did not take a required plant liquid effluent sample because l

g[ their time was preempted by a plant upset. Sampling was resumed on the next shif t.

l

,, i 21 i No other corrective action is anticipated or required.

I lii3i l l

I i 14 I I l

7 8 9 80 SYA

% POWER OTHER STATUS iS RY OISCOVERY DESCRIPTION Ii I 5 I I X lh l 0 l 0 l 0 l@l N/A I

l A l@l operator observation i

ACTIVITY CO TENT RELEASED OF RELEASE AMOUNT CF ACTIVITY LOCATION OF RELEASE y lZ l @ l Zl@l N/A l

l N/A I

PERSONNEL ExPOSMES oESCR,, TION @

NuM8ER Tv,E l i l 71 l o l o l o l@l Z l@l N/A l

PERSO~~E'L i~;UWiES DESCRIPTION @

~uM8ER li Ia i lo I o Io l@l N/A l

F 8 9 11 12 80 LOSS OF OR OAMAGE TO FACluTY Q TYPE

DESCRIPTION

v li 191 l Z l@l N/A l

7 8 3 10 80 ISSU E DE CRIPTION 12 I ol lN fhl N/A l

lllllIIIIIIll}

" 5

/ j/g' /

8 0 04210 $

(303) 785-2253 i

NAME OF PREPARER

' NE:

~