ML19318A510

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Quarterly Rept for Jan-Mar 1980
ML19318A510
Person / Time
Site: West Valley Demonstration Project
Issue date: 04/28/1980
From:
EMVNFWV, NUCLEAR FUEL SERVICES, INC.
To:
Shared Package
ML19318A509 List:
References
16440, NUDOCS 8006230247
Download: ML19318A510 (12)


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. TABLE OF CONTENTS ENVIRONMENTAL MONITORING

, LOW LEVEL LIQUID EFFLUENTS GASEOUS EFFLUE,NTS SURVEILLANCE TESTS LOW LEVEL LIQUID WASTE TREATMENT PLANT PERFORMANCE

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TABLE 1 LIQUID EFFLUENTS - 1979 TABLE 1A LIQUID EFFLUENTS - 1980 TABLE 2 GASEOUS EFFLUENTS - 1980 TABLE 3 SURVEILLANCE TESTS TABLE 4 FILTER REPLACEMENT l PROCESSING

SUMMARY

. NUCLEAR FUEL

SUMMARY

. TABLE 5 NUCLEAR FUEL STATUS - MARCH 31, 1980 RADI0 ACTIVE WASTE FACILITY PERFORMANCE AND MODIFICATIONS e

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ENVIRONMENTAL MONITORING As a result of changes in Technical Specifications, sampling milk for 131I~was dis-continued on September 21, 1973.

Thirty-nine (39) samples were obtained durina the first cuarter from the perimeter monitoring stations and were analyzed for alpha and beta activity. The alpha activity ranged from 1.38 (10 16) to 7.72 (10 16) uCi/ml for an average of 2.48 (10 16) uCi/ml.

The beta activity ranged from 1.90(1015)to4.63(1014) uCi/ml with an average of 1.61 (1014) pCi/ml.

LOW LEVEL LIQUID EFFLUENTS The amounts of radioactivity in liquid discharged from the plant curing this period and their relationship to the maximum permissible concentration (MPC) in the Cattaraugus Creek are shown in Table 1.

GASEOUS EFFLUENTS -

The amount of particulcte radioactivity discharged via the plant stack and the relationship to the release limit in the Technical Specifications is shown in Table

2. Change 20 to the Technical Specifications discontinued the recuirements of.

Krypton-85 and Iodine-131 monitoring while plant operations are suspended.

SURVEILLANCE TESTS During this period, tests were performed in accordance with Section 6 of the Technical Specifications. The completion dates are shown in Tables 3 and 4.

LOW LEVEL LIQUID WASTE TREATMENT PLANT PERFORMANCE During this period, the LLWT was.in operation a total of 24 days and treated 1,690,000 gallons of water. Ninety-six (96) drums of concentrated sludge were removed, each having a radiation level of <10 mr/hr. Decontamination of waste water continues to be good. All water discharged has been,below 2.0 x 10~5 pCi Csl37/ml. Average removal factors for this period are shown below.

AVERAGE REMOVAL FACT 0F, _.

Isotope Previous Quarter This Quarter Cs-137 79.6 84.7 Sr-90 99.7 Not Yet Available Ru-Rh-106 Below Detection Limits Below Detection Limits Gross Beta 98.2 98.5 l No significant developments or modifications to the facility have occurred during the past quarter and operation has been routine.

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LIQUID EFFLUENTS--1979 (Curies) a

% MPC Measured 90 129 Month Gross a Gross a Tritium Sr 7 In Cattaraucus Creek c

Jan 0.000001 0.00004 0.0007 0.00001 NR 0.41 Feb 0.000001 0.00001 0.0004 0.00001 NRc 0.38 Mar 0.00013 0.016 3,3 0.0027 0.00010 0.25 Apr 0.000001 0.00003 c 0.0004 0.0001 NR 0.39 0.0d0001 0.00002 c May 0.0001 0.00001 NR -0.27 c

Jun 0.000001 0.00003 0.0008 0.00001 NR 0.48 c

Jul 0.000001 0.00005 0.0008 4 0.00001 NR 0.52 1 Aug 0.00033 0.031 3.0 0.0024 0.00012 0.56 l 0.000001 c Sep 0.00006 0.0004 0.00001 NR 0.52 Oct 0.000001 0.00004 c 0.0006 0.00001 NR 0.41 Nov 0.000001 0.00004 0.0009 c 0.00001 NR 0.47 Dec 0.00017 0.019 1.8 0.0015 0.00008 0.49 1979 0.00064 0.066 2.1 0.0068 0.00030 0.43 a

MPC (s) = 3.0 (10 7) pCi/mi when Sr90 analyses are not available MPC (8) = 1.0 (10 s) uCi/ml when Sr90 analyses are included separately MPC (a) = 5.0 (10 6) pCi/ml c

Not required; there were no lagoon 3 effluent releases for the month l

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, LIQUID EFFLUENTS--1980 (Curtes) 8

% MPC Measured M_onth Gross a Gross 8 . Tritium Sr 90 I 129 In Cattarauous Creek 1 c b Jan 0.000001 0.00002 0.0010 0.00001 NR NA b c b Feb 0.000001 0.00002 0.0007 t1A NR NA b c b Mar 0.000001 0.00002 0.0006 NA NR NA d c b 1980 0.000003 0.00006 0.0023 0.00001 NR 'flA 1

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MPC (s = 3.0 (10 7) pCi/ml when Sr90 analyses are not available MPC (8 = 1.0 (10 s) pCi/ml when Sr90 analyses are included separately MPC(a = 5.0 (10 6) pCi/ml i b

Not yet available' c

Not required; there were no lagoon 3 effluent releases for the month d

Release through January,1980 l

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Table 2 PARTICULATE GASE0US EFFLUENTS Month Curies  % Monthly Limit January .00012 0.04 February .00010 0.04 -

March .00008 0.03 1980 .00030 0.036 i .

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Table 3 SURVEILLANCE TESTS. .

Spec. # Subject Comoleted This Quarter Comments 6.1 Raschig Ring Tanks Tanks are to be scheduled prior to next processing use 6.2 Sump Alarms and Eductors XC-2 1-1, 1-22, 2-12, 3-5, 3-25 Satisfactory XC-3 1-1, 1-22, 2-12, 3-5, 3-25 Satisfactory PPC 1-1, 1-22, 2-12, 3-5, 3-25 Satisfactory 6.3 Waste Storage Tank Pan Instrumentation 8D-1, 80-2 1-22, 2-11, 3-3, 3-24 Satisfactory' 8D-3, 8D-4 1-22, 2-15, 3-4, 3-25 Satisfactory 6.4 Emergency Utility Equipment 30T-l 1-8 Satisfactory 31K-1 1-8 Satisfactory 32G-4B 1-8 Satisfactory 31G-2, 2A 2-12 Satisfactory 31K-2, 2A 2-13 Satisfactory 32G-2A, 28 2-12 Satisfactory Diesel Fuel . 1-7, 1-14, 1-21, 1-28, 2-4, 2-11, 2-18, 2-25, 3-3, 3-10, 3-17, 3-24, 3-31 Satisfactory Propane Fuel 1-8, 1-21, 1-29, 2-6, 2-11, 2-19, 2-22, 3-3, 3-10, 3-17, 3-24, 3-31 Satisfactory 15K-10A '

1-8 Satisfactory Satisfactory 15F-21 1-8 6.5 Filters 1-3, 1-17, 1-22, 2-1, 2-5, 2-15, 2-20, 2-26, 3-4, 3-11, 3-19, 3-28 Satisfactory 6.6 Dilution Air Not required this period 6.7 ~ Boric Acid . Not required this period 6.8 Locking Out Not required this period 6.9 Water Activity Alarms 3-31 Satisfactory 6.10 Poisoned Dissolver Baskets Not required this period 6.11 Solvent Analysis Not required this period

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Table 4 FILTER REPLACEMENT There were no filter replacements during this reportir.g -

period.

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PROCESSING

SUMMARY

During this period there was no proce'ssing of fuel. .

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J NUCLEAR FUEL SU!HARY The following information is based upon nuclear material accountability records and indicates the disposition of nuclear material in fuel at the reprocessing plant.

A. INVENTORY The total on-site inventory on March 31, 1980 was 166,759 kilograms of uranium and 1,039,827 grams of plutonium. An inventcry description by source and material type is presented in Table-5.

B. RECEIPTS AND SHIPMENTS During the quarter, there were no shipments or receipts of spent fuel assemblies at the West Valley site.

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C. MEASURED WASTE AND ADJUSTMENTS There was no loss of uranium or plutonium during the reporting period as measured waste.

No adjustments for uranium and plutonium to NFS Lot 27A were required.

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D. LOSS ON DECAY During the period 9/30/79 - 3/31/80, there was a reduction of 1,933 grams of plutonium in stored fuel due to the radioactive decay of the Pu-241 isotope.

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e Table 5 NUCLEAR FUEL STATUS AS OF MARCH 31, 1980 Kilograms Grams l Total U U-235 U-233 Total Pu I. INVENTORY (1/1/80) ,

NFS 3,271 8.01 --

306 Dresden-1 20,429 144.03 0.30 117,122 RG&E 46,156 722.48 -- 286,315 Consumers 11,130 238.68 -- 64,199 WEPC0 43,017 462.61 -- 339,154 Jersey Central 42,756 463.42 -- 234,664 TOTAL 166,759- 2,039.23 0.30 1,041,760 II. RECEIPTS (1/1/80-3/31/80) No receipts during this period.

III. REMOVALS (1/1/80-3/31/80)

A. Measured Waste Lo.t 27A ,

0 0 0 0 B. Adjustnents Lot 27A 0 0 0 0 C. Loss on Decay 0 0 0 1,933 TOTAL 0 0 0 1,933 IV. INVENTORY

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NFS 3,271 8,01 --

306 Dresden-1 20,429 144.03 0.30 116,887 RG&E 46,156 722.48 -- 285,787 Consumers 11,130 238.68 -- 64,118 WEPC0 43,017 462.61 -- 338,394 Jersey Central - 42,756 463.42 -- 234,335 TOTAL 166,759 2,039.23 0.30 1,039,827

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RADI0 ACTIVE WASTE, A. Solid Waste The radioactive plant waste buried during this quarter consisted of 1,293.53 cu ft containing 49.636 curies. This material was buried in the NRC-licensed burial area. ,

B. High Level Liouid Waste As of March 31, 1980, the high level storage tank 8D-2 contained 544,200 gallons of neutralized waste with an activity of 4,675 pCi Cs-137/mi and 69 pCi Cs-134/ml.

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. FACILITY PERF0Pf4ANCE AND MODIFICATIONS This section describes:

1.0 Major modifications that were either initiated or completed at the processing plant during the reporting period.

1.1 A new 6" steam line was installed which connects the discharge of a temporary boiler to the 150# steam header in the Utility Room. (See Section 2.1 below.)

2.0 A description of malfunctions of any equipment listed in Appendices 5.2. 9.51, 9.53 and 9.56 of the Final Safety Analysis Report which ,

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2.1 On January 14 at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, the north boiler experienced an l explosion in the fire box which damaged the boiler and the

, associated piping which was common to both boilers. Piping repairs were started immediately so that by 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> the south boiler was producing steam.

On January 23, a rental boiler was received and set in place.

Installation and testing of the rental boiler were complete by February 12.

2.2 On March 3, the south boiler shut down at approximately 1545 hours0.0179 days <br />0.429 hours <br />0.00255 weeks <br />5.878725e-4 months <br /> due to a shorted alternator which supplies power for the boiler circuitry. The rental boiler was placed on line until temporary repairs were made to the south boiler to get it back on line at 2210 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.40905e-4 months <br />.

On the following day the rental boiler was again placed on line until permanent repairs were made to the south boiler.

The south boiler was back on normal service at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />.

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