05000269/LER-1977-030-03, /03L-0:on 771220,2.8 Gallon Per Minute Leak Indicated by Reactor Bldg Normal Sump Level rate-of-change Monitor.Caused by Valve 1RC-2 Packing Failure.Valve Repacked & Tested Using PT/1/600/10 RCS Breakage

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/03L-0:on 771220,2.8 Gallon Per Minute Leak Indicated by Reactor Bldg Normal Sump Level rate-of-change Monitor.Caused by Valve 1RC-2 Packing Failure.Valve Repacked & Tested Using PT/1/600/10 RCS Breakage
ML19316A485
Person / Time
Site: Oconee 
Issue date: 01/19/1978
From: Ken Wilson
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19316A483 List:
References
LER-77-030-03L, LER-77-30-3L, NUDOCS 7912110820
Download: ML19316A485 (1)


LER-1977-030, /03L-0:on 771220,2.8 Gallon Per Minute Leak Indicated by Reactor Bldg Normal Sump Level rate-of-change Monitor.Caused by Valve 1RC-2 Packing Failure.Valve Repacked & Tested Using PT/1/600/10 RCS Breakage
Event date:
Report date:
2691977030R03 - NRC Website

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