ML19309F835

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LER 80-019/03L-0:on 800327,operation in Degraded Mode of Limiting Condition 4.2.10 Occurred on Six Occasions & Reactor Dewpoint Limit of Limiting Condition 4.2.11 Was Exceeded Once.Caused by Problem W/Buffer Helium Sys
ML19309F835
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 04/25/1980
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19309F830 List:
References
LER-80-019-03L, LER-80-19-3L, NUDOCS 8005010401
Download: ML19309F835 (1)


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NRC FORM 366 U.S. NUCLEAR RECn .TCRY COMMISSION LICENSEE EVENT REPORT 800 5010 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) l CONTROL BLOCK: l 8

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f EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l Io l2l l During the period from March 27, 1980, through April 16, 1980, operation in a de- l

[ol3l l graded mode of LCO 4.2.10 occurred on six separate occasions, and the reactor dew- 1 l I o 14 l l point limit of LCO 4.2.11 was exceeded once. Reportable per Fort St. Vrain Technical i ITTT1 1 Specification AC 7.5.2(b)2. No affect on public health and safety. Similar occur- l 10 l61 l rences reported in RO's 80-11, 79-53. 79-45. 79-43. 79-31. 79-30. 79-24. 79-01. 78-39.1

IoI7i l 78-37, 78-18, 78-16, 78-12, 78-01, 77-36, 77-13, 77-02, and 76-06. I I

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44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i l 0 l l Prime cause of oxidant and moisture levels was problems with buffer helium system. I g l Corrective action was reduction of reactor powe.- level, which reduced average core i g l outlet temperature belou the limit. In one case, the primary coolant oxidants were I g ] reduced below the limit. No further corrective action is anticipated or required.

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AME OF PREPARER ' PHONE: (303) 785-2253