05000267/LER-1980-011-03, /03L-0:on 800306-21,reactor Dewpoint Limiting Conditions for Operation Were Exceeded on One Occasion & Operation in Degraded Mode Occurred on Three Occasions. Caused by Problems W/Buffer Helium Sys

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/03L-0:on 800306-21,reactor Dewpoint Limiting Conditions for Operation Were Exceeded on One Occasion & Operation in Degraded Mode Occurred on Three Occasions. Caused by Problems W/Buffer Helium Sys
ML19309C374
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 04/02/1980
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19309C367 List:
References
LER-80-011-03L, LER-80-11-3L, NUDOCS 8004080512
Download: ML19309C374 (1)


LER-1980-011, /03L-0:on 800306-21,reactor Dewpoint Limiting Conditions for Operation Were Exceeded on One Occasion & Operation in Degraded Mode Occurred on Three Occasions. Caused by Problems W/Buffer Helium Sys
Event date:
Report date:
2671980011R03 - NRC Website

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8 60 61 DOCKET NUMBER 68 69 EV ENT DATE 74 75 REPORT CATE 80 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES Oto lol2Jl During the period from March 6, 1980, through March 21, 1980, reactor dewpoint limits l [o13l l of LCO 4.2.11, Figure 4.2.11-1 were exceeded on one occasion, and operation in a de-l l0t4l l graded mode of LCO 4.2.10 occurred on three separate occasions. Recortable ner For* l [Otsl l St. Vrain Technical Specification AC 7.5.2(b)2.

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