05000259/LER-1980-007-03, /03L-0:on 800125,while Performing SI 4.2.A-16, Calibr Reactor Bldg Isolation &/Or Logic Timers,B Logic Channel Did Not Isolate.Caused by Intermittent Sticking of Relay R1B Resulting in Time Delay Contacts Being Closed

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/03L-0:on 800125,while Performing SI 4.2.A-16, Calibr Reactor Bldg Isolation &/Or Logic Timers,B Logic Channel Did Not Isolate.Caused by Intermittent Sticking of Relay R1B Resulting in Time Delay Contacts Being Closed
ML19296C558
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 02/22/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19296C556 List:
References
LER-80-007-03L, LER-80-7-3L, NUDOCS 8002260642
Download: ML19296C558 (2)


LER-1980-007, /03L-0:on 800125,while Performing SI 4.2.A-16, Calibr Reactor Bldg Isolation &/Or Logic Timers,B Logic Channel Did Not Isolate.Caused by Intermittent Sticking of Relay R1B Resulting in Time Delay Contacts Being Closed
Event date:
Report date:
2591980007R03 - NRC Website

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4 EVENT DESCRIPTION AND PRC8ABLE CONSEQUENCES h o12 l During refueling outage while performing SI 4.2.A-16 " Calibration Reactor Building l

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4 l " RIB" was found to be sticking part of time resulting in "B" logic channel not o13) I lating. Reference T. S. 3.2.A.

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Tennessee Valley Authority Form BF-17 Browns Ferry Nuclear Plant BF 15.2 1/10/79 LER SUPPLEMENTAL INFORMATION BFRO-50 259 / _8007 Technical Specification Involved 3.2.A.

Reported Under Technical Specification _6.7.2.b.2 Date of Occurrence _1/25/80 Ti:ne of Occurrence 1030 Unit 1

Identificadon and Descriptien_of Occurrence:

Wile performing " Calibration Reactor Building Isolation and/or Logic Timers" "B"

logic channel did not isolate.

Conditions Prio.r_to Occurrence:

Unit 1 @ 0% refueling outage.

Unit 2 @ 77%.

Unit 3 0 98%.

Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment.

Describe.

NA Apparent Cause of Occurrence:

Relay "RlB" was found to be sticking part of the time resulting in the time delay contacts remaining closed.

Analve.is of Occurrence:

There was no damage to plant equipment. There was no activity release, no personnel exposure or injury and no danger to health or safety of the public.

Corrective Action

The relay was replaced and SI 4.2. A-16 was completed.

p_ailure Data:

NA

  • Retention:

Period - Lifetime; Responsibility - Administrative Supervisor

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  • Revision :

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