ML19276G876

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RO 78-62/1P,confirming 781019 Telcon:Limiting Condition for Operation Was Not Invoked When Surveillance Procedure 2301-3D1,using Data of 781016,showed Unidentified Leakage of 2.6g/minute
ML19276G876
Person / Time
Site: Crane 
Issue date: 10/19/1978
From: Seelinger J
METROPOLITAN EDISON CO.
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19276G875 List:
References
RO-78-62-1P, NUDOCS 7908280521
Download: ML19276G876 (1)


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,7 Post Cffice Sox 480 Micaletown, Pennsylvr1ia 17057 717 M44041 October 19, 1978 Mr. Soyce H. Grier Director of Regulatory Operations Region I Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406 Operating License:

DPR-73 Occket:

50-320

Subject:

Reportable Occurrence No. 7S-62/IP Cear Mr. Grier:

This telegram is to confirm the conversation between Mr. J.L. Seelinger, Unit 2 Superintendent Technical Support, and Mr. D. Haverkamp, Region I NRC at 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br /> on October 19, 1978.

A situation considered reportable under technical specification 6.9.1.3.5 was discovered at 1000 hcurs on October 19, 1978, when it was determined tnat the limiting condition for operation (LCO), action b, for T.S. 3.1.6.2 was not invoked when surveillance procedure, 2301-301, data obtained at 1935 on 10-16-78 showed an Unidentified Leakage greater than 1 gpm (2.6 gpm actual unidentified leakage).

This event cccurred due to personnel errors in interpreting both the LCO and surveillance performance requirements of T.S. 3.4.6.2.

Unidentified leakage was reduced to T.S. limits at 0735 on 10-18-73.

Further cetails and corrective action will be discussed in the followup report.

o J.L. Seelinger df Unit 2 Superintendent /

Technical Succort JLS:bli

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