05000338/LER-1979-039-03, /03L-0 on 790325:during Normal Operation,Power Supply to Hydrogen Recombiner Deenergized & Recombiner Inoperable for 10-h.Unit 2 Emergency Bus Degraded Voltage Protection Modified & Reenergized

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/03L-0 on 790325:during Normal Operation,Power Supply to Hydrogen Recombiner Deenergized & Recombiner Inoperable for 10-h.Unit 2 Emergency Bus Degraded Voltage Protection Modified & Reenergized
ML19274E786
Person / Time
Site: North Anna Dominion icon.png
Issue date: 04/19/1979
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19274E784 List:
References
LER-79-039-03L, LER-79-39-3L, NUDOCS 7904240411
Download: ML19274E786 (1)


LER-1979-039, /03L-0 on 790325:during Normal Operation,Power Supply to Hydrogen Recombiner Deenergized & Recombiner Inoperable for 10-h.Unit 2 Emergency Bus Degraded Voltage Protection Modified & Reenergized
Event date:
Report date:
3381979039R03 - NRC Website

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' LVENT DATE

/4 lb HLPOHT DAT E 80 EVENT DESCRIPTION AND PROGABLE CONSEQUENCES h [During normal power operations, the power supply to the Unit 2 post DBA Hydtngon

___j o 2 go]3i lRecombiner was deenergized.

This action rendered the Hydrogen Recombiner. 2-HC-HC-1.

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[ inoperable for ten hours. This event did not jeopardize the health and safety _of tho I

O 4 lO is i [ general public since the Unit 1 Hydrogen Recombiner,1-HC-HC-1 was still available.

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40 41 42 43 44 47 CAUSE DESCRIPTIGN AND CORRECTIVE ACTIONS [Necessary modifications to the Unit 2 Emergency Bus Deoraded Voltage Protection Svstom I i

o ti li l required the comrlete deenergization of the 2H 4160 volt bus and thornfnen thn opn uniti il i7; [ bus which supplies power to 2-HC-HC-1.

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W. R. Cartwright psoNe:

NAME of PREPAftEft