LER-1979-035, /01T-0 on 790319:valve Weights for 14 Check Valves Supplied by Vendor Were Higher than Originally Specified. Caused by Erroneous Design Specs by Vendor.One Pipe Hanger Identified as Unsatisfactory Will Be Modified |
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North Anna Unit No. 1 License Number NPF-4 Attachment page 1 of 2 Docket Number 50-338 Report Number LER 79-035/OlT-0 Event Date.
March 19, 1979
Description of Event
The licensee was notified by the NSSS vendor for North Anna Unit No. I th at valve weights specified for certain check va!ves, supplied by the in error.
Specifically, 14 check valves originally specified
- vendor,
--.e as weighing 22S pounds each actually weigh 450 pounds each.
Immediately following this notification, the licensee directed the architect engineer for North Anna Unit N 3.
I to reanalyze the port ions of piping systems containing the subject check valves to determine if the design was adequate for the higher valve weights.
Eight individual pipe stress problems we re involved.
In al.1 cases, reanalysis indicated minor increases in pipe stresses due to the heavier valves but all values remained below code allowables (ASME B 31.7).
However, analysis of the 6 inch hot leg safety injection line to "A" reactor coolant loop indicated that one pipe hanger was overstressed. The piping arrangement and overstressed hanger location are shown in Figure 1.
Additionally, five other hangers, while not overstressed, were found to be below the original design margins.
While these hangers require some adjust-ment or modification to restore the original design margin, they would remain functional under all conditions.
Since the overstressed hanger could no longer be considered functional under accident condi icns, the A-E was directed to reanalyze the piping system assuming that the overstressed hanger was not installed. This was to determine the adequacy of the piping and remaining hangers under accident conditions assuming cenplete f ailure of the overstressed hanger.
This approach is conservative since a significant amount of the energy of the initial upset motica would be dissipated in failing the hanger. The results of this analysis indicated that, without the hanger, the piping will be stressed slighti:- 'reycad code allowables in three locations.
The three locations, node prin:s 2, 3, and 21, are indicated on Figure 1.
The stresses calculated from Z;ustion (9) of the code versus the code allowables are listed in Table 1.
The code allowable, 1.5 (Sm), is based on the assumed generic yield s:renz:h for time type of material; specifically, Sm =.9 (yiele st rength).
ke have reviewed the initial material test result s for the specific piping used at North Anna and have calculated an Sm value specifically for :' e caterials used. The resulting allowables based on the n
pipe specific y;e;d strengths are also listed in Table 1 (Column 3).
TABLE 1 Calculated Stress (1.5 Sm)
(1.5 Sm)-
PSI - Eqn (9)
Code-Generic MILL. CERT. SPECIFIC Point 2 25,761 25,620 31,320 Point 3 26,720 25,020 31,320 Point 21 35,215 30,000 34,900
North Anna Unit No. 1 License I: umber NPF-4 Attachnent page 2 of 2 Docket Number 50-338 Re po r t Number LER 79-035/01T-0 Event Date:
March 19, 1979 When the inethodology of the code is applied based on the specific yield strengths for the piping naterials involved, ali points are below 1.5 Sm.
Based on this information it was concluded that the subject piping would remain intact and functional under all accident conditions.
This event is r e p'a r t a b le pursuant to Technical Specificat ion 6,9.1.8.i.
Probable Consequences of Occurrence As described above, reanalysis for the heavier valve weights indicates' that, while minor modifications are necessary to achieve strict code compli-ance, the existing piping system will remain intact and funct ional under accident conditions.
Concurrent with the piping reana hrsis, we conducted a review of the operational implications of any failure in this line.
The subject line is inactive until about 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> following a LOCA, at which time safety injection flow is redirected from the cold legs to the hot legs to prevent precipitation of boron within the system.
Based on analysis completed by the NSSS vendor, if the subject piping segment did rupture sa result of the seismic event and a LOCA occurred concurrent with this rupture, the hot leg recirculation system function would not be degraded below minimum requirements for long term LOCA mitigation.
At the initiation of hot leg recirculation, approximately 250 gpm is required to be deliveced to the core to compensate for boil-off.
Assuming only one hot Icg reeirculation branch path delivers to the core, appcoximately 1000 gpm will be provided to compensate for boil-off. This assumes one branch path spills to the broken loop (LOCA) and one branch path spills as a result of the postulated hot leg branch line rupture.
Thus a coolant flow of 4 times the required flow would remain available ender the worst accident scenario. The re fo re, the health and safety of the general public were not affected.
Cause of Occucrence The weights :riginally specified by the NSSS vendor for the subject check valves were ir error.
The initial pipe stress calculations performed on the piping ecn:aining the check valves was based on the erroneous valve weights.
Reana'_f 5_s was required to determine if the existing piping sys tem was adequate for the heavier valve weights.
Reanalysis identified the inadequate hanger.
Corrective Actier The pipe '.:nger identified as overstressed will be modified to meet all i
code req u i reme n: s by April 16, 1979.
The other bangers will be adjusted or modified to restore original design cargins 22 operations and materials availability permits.
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| 05000338/LER-1979-001-01, /01T-0 on 790115:non-conservatism Identified in Calculations Performed in Monitoring Axial Power Distribution Fj(Z).Caused by Omission of Sys & Procedures Used to Monitor Fj(Z) | /01T-0 on 790115:non-conservatism Identified in Calculations Performed in Monitoring Axial Power Distribution Fj(Z).Caused by Omission of Sys & Procedures Used to Monitor Fj(Z) | | | 05000338/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000338/LER-1979-002, Forwards LER 79-002/03L-0 & 79-003/03L-0 | Forwards LER 79-002/03L-0 & 79-003/03L-0 | | | 05000338/LER-1979-002-03, /03L-0 on 790101:during Normal Operation,Pump 1-RM-P-159A Tripped on Overload.Containment Particulate Sample Flow Was Lost,Rendering Inoperable 1 Reactor Coolant Leak Detection Sys,Due to Deficient Federal 1206LLT Bearing | /03L-0 on 790101:during Normal Operation,Pump 1-RM-P-159A Tripped on Overload.Containment Particulate Sample Flow Was Lost,Rendering Inoperable 1 Reactor Coolant Leak Detection Sys,Due to Deficient Federal 1206LLT Bearing | | | 05000338/LER-1979-003-03, /03L-0 on 790102:during Periodic Test,Noted That Containment Isolation Valve TV-SV-102-1 Would Not Shut Fully.Cause Undetermined | /03L-0 on 790102:during Periodic Test,Noted That Containment Isolation Valve TV-SV-102-1 Would Not Shut Fully.Cause Undetermined | | | 05000338/LER-1979-004-03, /03L-0 on 790108:during 1-PT-36-1(A) Found That Steam Generator 3 Hi Hi Level Test Panel Was Faulty, Preventing Test of This Channel.Caused by Faulty Universal Logic Card on Test Panel | /03L-0 on 790108:during 1-PT-36-1(A) Found That Steam Generator 3 Hi Hi Level Test Panel Was Faulty, Preventing Test of This Channel.Caused by Faulty Universal Logic Card on Test Panel | | | 05000338/LER-1979-005-01, /01T-0 on 790129:mufflers for Emergency Diesel Generators Not Seismically Supported Nor Missile Protected as Required by Fsar.Caused by Const Error | /01T-0 on 790129:mufflers for Emergency Diesel Generators Not Seismically Supported Nor Missile Protected as Required by Fsar.Caused by Const Error | | | 05000338/LER-1979-005, Forwards LER 79-005/01T-0 & 79-008/01T-0 | Forwards LER 79-005/01T-0 & 79-008/01T-0 | | | 05000338/LER-1979-006-03, /03L-0 on 790111:damaged Wiper Seal Found on Hydraulic Suppressor 1-FW-HSS-233.Caused by Poppet Valves Which Control Lock Up Rate Being Improperly Set.Suppressor Replaced W/Operable Spare Suppressor.No Danger to Public | /03L-0 on 790111:damaged Wiper Seal Found on Hydraulic Suppressor 1-FW-HSS-233.Caused by Poppet Valves Which Control Lock Up Rate Being Improperly Set.Suppressor Replaced W/Operable Spare Suppressor.No Danger to Public | | | 05000338/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000338/LER-1979-007-03, /03L-0 on 781116:during Normal Operation,Fire Door S54-5 Between Unit 1 Emergency Switchgear Room & Cable Vault Was Sprung & Would Not Make a Tight Seal,Evidently Due to Attempt to Free It While Stuck | /03L-0 on 781116:during Normal Operation,Fire Door S54-5 Between Unit 1 Emergency Switchgear Room & Cable Vault Was Sprung & Would Not Make a Tight Seal,Evidently Due to Attempt to Free It While Stuck | | | 05000338/LER-1979-008-01, /01T-0 on 790129:design Flow of 37 Gpm to Charging Pump Coolers Could Not Be Met.Caused by 2 Inch Carbon Steel Piping & Charging Pump Skid Piping Being Too Large to Allow Adequate Flow | /01T-0 on 790129:design Flow of 37 Gpm to Charging Pump Coolers Could Not Be Met.Caused by 2 Inch Carbon Steel Piping & Charging Pump Skid Piping Being Too Large to Allow Adequate Flow | | | 05000338/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000338/LER-1979-009-03, /03L-0 on 790212:during Normal Operation,Snubber Support for C Steam Generator Atmosphere Discharge Line Found Damaged.Caused by Use of Support as Anchor for Chain Fall.Support Replaced | /03L-0 on 790212:during Normal Operation,Snubber Support for C Steam Generator Atmosphere Discharge Line Found Damaged.Caused by Use of Support as Anchor for Chain Fall.Support Replaced | | | 05000338/LER-1979-010-03, /03L-0 on 790127: During Calibr of Containment Particulate Monitor RMS159 in Mode 1, Instrument Read Low for Known Radiation Level. Caused by Detector High Voltage Setting Being Set Too Low | /03L-0 on 790127: During Calibr of Containment Particulate Monitor RMS159 in Mode 1, Instrument Read Low for Known Radiation Level. Caused by Detector High Voltage Setting Being Set Too Low | | | 05000338/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000338/LER-1979-011-03, /03L-0 on 790126:fire Door SS54-9 Was Nonfunctional.Caused by Removal of Latch from Door by Person or Persons Unknown | /03L-0 on 790126:fire Door SS54-9 Was Nonfunctional.Caused by Removal of Latch from Door by Person or Persons Unknown | | | 05000338/LER-1979-012-03, /03L-0 on 790127: Unidentified Primary Coolant Leakage Greater than 5 Gpm Noted. Caused by Blown Packing on Residual Heat Removal Isolation Valve MOV-1700 & Packing Leak on Pressurizer Spray Valve PCV-1455A | /03L-0 on 790127: Unidentified Primary Coolant Leakage Greater than 5 Gpm Noted. Caused by Blown Packing on Residual Heat Removal Isolation Valve MOV-1700 & Packing Leak on Pressurizer Spray Valve PCV-1455A | | | 05000338/LER-1979-013-03, /03L-0 on 790214:during Normal Operation,Fire Door S71-7 Between Auxiliary Bldg & Health Physics Found non- Functional.Caused by Bent Phaser on Left Door.Phaser Taped Out of Way & New Phaser Installed | /03L-0 on 790214:during Normal Operation,Fire Door S71-7 Between Auxiliary Bldg & Health Physics Found non- Functional.Caused by Bent Phaser on Left Door.Phaser Taped Out of Way & New Phaser Installed | | | 05000338/LER-1979-014-03, /03L-0 on 790202:pressurizer Level Indicator Indicated High Over Allowable Range.Caused by Voltage Drift in Associated Level Transmitter.Appropriate Channel Placed in Trip Condition & Transmitter Recalibr | /03L-0 on 790202:pressurizer Level Indicator Indicated High Over Allowable Range.Caused by Voltage Drift in Associated Level Transmitter.Appropriate Channel Placed in Trip Condition & Transmitter Recalibr | | | 05000338/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000338/LER-1979-015-03, /03L-0 on 790204:rod F08 Indicators in Disagreement.Caused by Voltage Drift in Signal Conditioning Card.Card Recalibrated & Functional Checks Performed Satisfactorily | /03L-0 on 790204:rod F08 Indicators in Disagreement.Caused by Voltage Drift in Signal Conditioning Card.Card Recalibrated & Functional Checks Performed Satisfactorily | | | 05000338/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000338/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000338/LER-1979-016-03, /03L-0 on 790213:main Steam trip,TV-MS-111A,valve Opened to Only 75% Capacity.Caused by Improperly Positioned Needle Valve Which Supplied Air to Valve Actuator.Valve Repositioned & Operation Restored | /03L-0 on 790213:main Steam trip,TV-MS-111A,valve Opened to Only 75% Capacity.Caused by Improperly Positioned Needle Valve Which Supplied Air to Valve Actuator.Valve Repositioned & Operation Restored | | | 05000338/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000338/LER-1979-017-01, /01T-0 on 790212:during Axial Power Distribution Monitoring Sys Failure on 790206,FQ Survey Computer Program Could Not Monitor Axial Power Distribution.Caused by Incorrect Power Inputs from Process Computer | /01T-0 on 790212:during Axial Power Distribution Monitoring Sys Failure on 790206,FQ Survey Computer Program Could Not Monitor Axial Power Distribution.Caused by Incorrect Power Inputs from Process Computer | | | 05000338/LER-1979-018-03, /03L-0 on 790214:during Mode 1 Operation at 98% Power,Main Steam Trip Valve 1-TV-MS-111B Leaked Excessively & Was Isolated for Repair.Caused by Deteriorated Internal Gasket.Valve Isolated & Gasket Replaced | /03L-0 on 790214:during Mode 1 Operation at 98% Power,Main Steam Trip Valve 1-TV-MS-111B Leaked Excessively & Was Isolated for Repair.Caused by Deteriorated Internal Gasket.Valve Isolated & Gasket Replaced | | | 05000338/LER-1979-019-03, /03L-0 on 790216:during Surveillance,Emergency Diesel Generator 1H Did Not Reach 900 Revolutions Per Minute in Required 10-s.Probable Cause Was Low Ambient Air Temp. Conditions of First Start Were Not Reproducible | /03L-0 on 790216:during Surveillance,Emergency Diesel Generator 1H Did Not Reach 900 Revolutions Per Minute in Required 10-s.Probable Cause Was Low Ambient Air Temp. Conditions of First Start Were Not Reproducible | | | 05000338/LER-1979-020-03, /03L-0 on 790131:fire Door S54-9 Was Found to Be non-functional.Caused by Recently Installed Electric Door Strike Slipping Out of Adjustment | /03L-0 on 790131:fire Door S54-9 Was Found to Be non-functional.Caused by Recently Installed Electric Door Strike Slipping Out of Adjustment | | | 05000338/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000338/LER-1979-021-99, /99T-0 on 790212:meterological Air Temp Change in Temp Indication Was Observed to Be off-scale Low.Caused by Faulty Resistance Temp Detector.Temp Element Replaced | /99T-0 on 790212:meterological Air Temp Change in Temp Indication Was Observed to Be off-scale Low.Caused by Faulty Resistance Temp Detector.Temp Element Replaced | | | 05000338/LER-1979-021, Forwards LER 79-021/99T-0 | Forwards LER 79-021/99T-0 | | | 05000338/LER-1979-022-03, /03L-0 on 790227:power Supply to Post DBA H Recombiner Deenergized Rendering Recombiner Inoperable for 4-h.Caused by Deenergizing of Motor Control Center to Perform Voltage Measurements | /03L-0 on 790227:power Supply to Post DBA H Recombiner Deenergized Rendering Recombiner Inoperable for 4-h.Caused by Deenergizing of Motor Control Center to Perform Voltage Measurements | | | 05000338/LER-1979-023, Forwards LER 79-023/03L-0,79-025/03L-0 & 79-031/03L-0 | Forwards LER 79-023/03L-0,79-025/03L-0 & 79-031/03L-0 | | | 05000338/LER-1979-023-03, /03L-0 on 790303:disagreement Noted Between Group & Individual Indication for Rod D-10.Caused by Voltage Drift in Conditioning Card.Calibr & Functional Checks Were Performed | /03L-0 on 790303:disagreement Noted Between Group & Individual Indication for Rod D-10.Caused by Voltage Drift in Conditioning Card.Calibr & Functional Checks Were Performed | | | 05000338/LER-1979-024, Forwards LER 79-024/43X-1 | Forwards LER 79-024/43X-1 | | | 05000338/LER-1979-024-43, /43X-1:on 790228,radwaste Release Occurred Unexpectedly During Pumping of Unit 2 Containment Sump Via Temporary Pump to Storm Drain Sys.Caused by Pressure Relief Valve Leaks in Units 1 & 2 Purge Headers | /43X-1:on 790228,radwaste Release Occurred Unexpectedly During Pumping of Unit 2 Containment Sump Via Temporary Pump to Storm Drain Sys.Caused by Pressure Relief Valve Leaks in Units 1 & 2 Purge Headers | | | 05000338/LER-1979-025-03, /03L-0 on 790228:power Range Channel N42 Placed in Tripped Condition.Caused to Allow Replacement of Erratic Delta Flux Indicator.Indicator Replaced & Power Range Detector Returned to Svc | /03L-0 on 790228:power Range Channel N42 Placed in Tripped Condition.Caused to Allow Replacement of Erratic Delta Flux Indicator.Indicator Replaced & Power Range Detector Returned to Svc | | | 05000338/LER-1979-026-03, /03L-0 on 790306:RHR Discharge Valve Opened Accidentally Causing Loop C Accumulator Level to Drop Below Min Volume Required.Caused by Accidental Operation of MOV-1720B.Valve Closed & Loop Accumulator Level Restored | /03L-0 on 790306:RHR Discharge Valve Opened Accidentally Causing Loop C Accumulator Level to Drop Below Min Volume Required.Caused by Accidental Operation of MOV-1720B.Valve Closed & Loop Accumulator Level Restored | | | 05000338/LER-1979-027-03, /03L-0 on 790225:axial Flux Difference Deviated Greater than 5% from Target.Caused by Xenon Transient Occurring During Startup Operation.Corrected by Boration by Reactor Operator | /03L-0 on 790225:axial Flux Difference Deviated Greater than 5% from Target.Caused by Xenon Transient Occurring During Startup Operation.Corrected by Boration by Reactor Operator | | | 05000338/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000338/LER-1979-028-03, /03L-0 on 790225:greater than 12-step Disagreement Noted Among Rod Position Indication,Computer Position Indication & Demand Signal Indication for Rod 9.Caused by Voltage Drift in Signal Conditioning Card | /03L-0 on 790225:greater than 12-step Disagreement Noted Among Rod Position Indication,Computer Position Indication & Demand Signal Indication for Rod 9.Caused by Voltage Drift in Signal Conditioning Card | | | 05000338/LER-1979-030-03, /03X-1 on 790308:nonconservative Gain Setting on delta-flux Signal Feeding Overpower Delta T Protection Circuitry Observed.Caused by Improper Setting of delta-flux Gain.Signal Recalibr | /03X-1 on 790308:nonconservative Gain Setting on delta-flux Signal Feeding Overpower Delta T Protection Circuitry Observed.Caused by Improper Setting of delta-flux Gain.Signal Recalibr | | | 05000245/LER-1979-030-03, /03L-0 on 790308:calibr Procedure Revealed Nonconservative Gain Setting on delta-flux Signal Feeding Overpower Delta T Protection Circuitry.Caused by Improper Setting of delta-flux Gain.Signal Recalibrated | /03L-0 on 790308:calibr Procedure Revealed Nonconservative Gain Setting on delta-flux Signal Feeding Overpower Delta T Protection Circuitry.Caused by Improper Setting of delta-flux Gain.Signal Recalibrated | | | 05000338/LER-1979-031-03, /03L-0 on 790302:surveillances of Engineered Safety Feature Pumps Not Performed within Interval.Caused by Personnel Error Due to Long Period from Preoperational Tests to Operation.Surveillances Will Be Performed | /03L-0 on 790302:surveillances of Engineered Safety Feature Pumps Not Performed within Interval.Caused by Personnel Error Due to Long Period from Preoperational Tests to Operation.Surveillances Will Be Performed | | | 05000338/LER-1979-032-03, /03L-0 on 790312:containment Vacuum Pump Suction Valve TV-CV150A Would Not Remain Closed When Operated from Control Room.Caused by Relay Sticking in Energized Position.Relay Repaired & Tested Satisfactorily | /03L-0 on 790312:containment Vacuum Pump Suction Valve TV-CV150A Would Not Remain Closed When Operated from Control Room.Caused by Relay Sticking in Energized Position.Relay Repaired & Tested Satisfactorily | | | 05000338/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | | | 05000338/LER-1979-033, Forwards LER 79-033/03L-0,79-036/03L-0,79-037/03L-0 & 79-038/03L-0 | Forwards LER 79-033/03L-0,79-036/03L-0,79-037/03L-0 & 79-038/03L-0 | | | 05000338/LER-1979-033-03, /03L-0 on 790321: C Steam Generator Narrow Range Level Indicator LI-1496 Gave Readings w/20% Disagreement W/Two Other Channels.Caused by Steam Leak in One Sensing Line Isolation Valve | /03L-0 on 790321: C Steam Generator Narrow Range Level Indicator LI-1496 Gave Readings w/20% Disagreement W/Two Other Channels.Caused by Steam Leak in One Sensing Line Isolation Valve | |
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