ML19269E006

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Forwards Rept on Potentially Hazardous Condition Discovered During Performance Check of Analysis Performed on Safeguards Piping Sys
ML19269E006
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 05/11/1979
From: Derienzo P
GIBBS & HILL, INC. (SUBS. OF DRAVO CORP.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
REF-PT21-79-125-000 NUDOCS 7906210435
Download: ML19269E006 (2)


Text

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q q - /a.f- om b Gibbs 8 Hill,Inc.

E NGINE E RS DESIONERS CONSTRUCTORS DIR E C T DIAL E XT E N SION 12121 760-5026 May 14, 1979 Director, Office of Inspection L . ,

and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Ft. Calhoun Nuclear Power Plant Unit #1 Docket No. 50-285 10CFR21 Report of Nonconformance Gentlemen:

At the request of Omaha Public Power District, Gibbs & Hill is performing a check of the analysis performed of the Safeguards Piping Systems for Ft. Calhoun Unit #1. This check is being made by using present day dynamic methods on representative sections of systems designed by static analysis to the plant FSAR requirements. During this check we detected a potentially hazardous condition within the meaning of 10CFR21.

Our report of the item detected is attached herewith.

Mr. Bud Eidem of Omaha Public Power District has been alerted to the existing condition.

If we can be of any further help in this matter please contact me.

Very truly yours, GIBBS & HILL, Inc.

C '. *

-.7 y P.P. DeRienzo Vice President, Consulting Engineering and Quality PPD:paf Assurance 2266 '32 7906210Vff 4 393 SEVENTH AVE NUE NEW YORK. N. Y 10003 CABLE' GIB BS HILL. N E W YORK

J OPD-1 Rev. 1 Page 21 of 25 APPENDIX V REPORT OF NONCONFORMANCE OR DEFECT UNDER 10 CFR PART 21 Evaluation Number: 79-4

'Date: 5/11/79 To: Director, Of fice of Inspection and Enforcement United States Nuclear Regulatory Commission Washington, D.C. 20555 From: Gibbs & Hill, Inc./'

Dravo Utility Constructors, Inc.

393 7th Avenue New York, N.Y. 10001 Facility Name and Location:

Fort Calhoun Unit #1 Blair, Nebraska Licensee: Omaha Public Power District Docket Number: 50-285 Date: 11/28/69 License Type: Operating (Full Power) Da te: 8/9/73 Constructor: (If Applicable) Peter Kiewitt Construction Subcontractor: (If Applicable) Peter Kiewitt - Bergen Paterson Component Vendor: (If Applicable) Dravo Corp. (Ripe)

Component Subvendor: (If Applicable)

Description of Failure to Comply or Defect:

The removal of a lateral seismic restraint on certain Auxiliary Coolant piping violates the Fort Calhoun I - FSAR criteria for seismic support of piping. This failure to comply with FSAR, Appendix F, 2.2.2, page F-7a, is considered to have a possible impact on the ability to mitigate an accident.

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OPD-1 Rev. 1 Page 22 of 25 Description of Safety Hazard:

A possible failure of the Aur.iliary Coolant piping may result during a seismic event. The loss of this piping will result in loss of system operability and may reduce containment cooling capacity. -

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Defective Basic Component Number: Auxiliary Coolant Piping System Supports

-In use: Fort Calhoun - Unit #1 At: Blair, Nebraska

-Supplied for use:

At:

-On Order:

For:

_ Corrective Action By:

Organization - Omaha Public Power District Individual -

Advice to Purchaser or Licensee:

Review Auxiliary Coolant Piping System supports for conformance to the requirements of Ft. Calhoun Unit #1 FSAR, Appendix F, 2.2.2, Page F-7a. Addition of appropriate lateral seismic restraints in accordance with the above FSAR requirements will serve to correct this condition.

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W/ J 5/ ff GtH Vice PreAident, Copsulti69 and QA Date '

(Designated Responsible Officer) 2266 ;34 d

ATTACED IS A PART 21 REPORT FROM IE f%1L UNIT - ROOM 359Eh!

~6:!: . PART 21 IDBRIFICAiIm idIb/4~r-e a COWANY tWEAA 4 h #

DATE OF ETTER #d//79-

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AD/FRSI - AD/SG-IE liRR/DR1 (BOYD) NASS/ FOS AD/RDI AD/RDI ( 2 ) REGIONS REGIONS AD/RCI IEFILES f1RR/DDR ( STB 10)

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CENTPAL FILES - SS-395 BOB D3 DIG, f1PA ACTION:

FRELIMINARY EVUALATION OF THE ATTACHED REPORT It01 CATES LEAD RESPONSIBILITY FOR i

FOLLGf-UP AS SHOWN BElEW:

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