05000338/LER-1980-015-03, /03L-0:on 800116,during Reactor Physics Testing Following Refueling Outage,Reactor Was Critical W/Rcs Tavg Under 541 F.Caused by Cooldown While Attempting to Maintain RCS Temp During Testing.Heat Release Valve Closed

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/03L-0:on 800116,during Reactor Physics Testing Following Refueling Outage,Reactor Was Critical W/Rcs Tavg Under 541 F.Caused by Cooldown While Attempting to Maintain RCS Temp During Testing.Heat Release Valve Closed
ML19260D969
Person / Time
Site: North Anna Dominion icon.png
Issue date: 02/11/1980
From:
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19260D965 List:
References
LER-80-015-03L, LER-80-15-3L, NUDOCS 8002120681
Download: ML19260D969 (1)


LER-1980-015, /03L-0:on 800116,during Reactor Physics Testing Following Refueling Outage,Reactor Was Critical W/Rcs Tavg Under 541 F.Caused by Cooldown While Attempting to Maintain RCS Temp During Testing.Heat Release Valve Closed
Event date:
Report date:
3381980015R03 - NRC Website

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EVENT CATE 74

'S REPORT CATE 83 EVENT OESC6tPTION AND PRCBAOLE CONSEQUENCES h o 12. l During reactor physics testing following the refueling outage. the reactor as ertticall a,3 ; lwith RCS TAVG less than 541*F.

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The RCS TAVG l 0,4 was restored to greater than 541*F within the 15 minute time allowance of the action I

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