LER-1980-017, /01T-0:on 800121,during Startup Physics Testing, F Values Exceeded Design Value Tolerance at hot-zero-power w/D-bank Inserted & Banks C & D at Insertion Limits.Caused by Presence of Quadrant Power Tilt.Safety Evaluation Done |
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| 3381980017R01 - NRC Website |
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NHC FOHM 36G 11 {7)
LICENSEE EVENT REPORT 3
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Virginia Elect ric and Powe r Corpany Attachnent: Page 1 of 1 North Anna Power Station, Unit 1 Docket No. 50-333 Peport No. II.R/R0 80-017/0 lT-0 Desc ript ion of Fven t Du r ing the Startup Physics Testing Progran for " orth Anna Unit i, Cycle 2, the re a su rec' values for F6telta H) exceeded th" desien value tolerance at hot-zero-powe r wi th D-bank inse r ted, and a t 37 pouer with Banks C and D a t th" insert ion limits.
These neasurenents provide a basis for de te rnining that the es:ist ing control rod insertion lini t s given in Technical Specification Figuro 3.1-1 are no longer appropriate for Unit 1, Cycle 2 opera tion.
This event is reportable pursuant to T.S.
6.0.1.8.i.
Probable Consequences of Event The reasured va lues for F(delta H) do not constitute a viola t ion of Technical Specification limits since power was naintained at lecs than 57 of rated the rnal powe r.
'Ih e heal th and sa fe ty of the genera! public were not af fected by this event.
Cause
The cause of the high F(delta H) values is the presence of a quad rant powe r tilt which was identified through incore flux cap analyses.
It is believed that the quad ran t power tilt is being caused by a non-synne tric isotopic dist ribut ion within the irradiated fuel as a result of the quadrant powe r t L i t that uas present during Cycle 1 operation.
Innediate Corrective Action Prior to increaalng reac tor powe r above 57 of rated thernal powe r, a sa fe ty evaluation was perforned to justify power operation uith revised contrel rod inse r t ion 1inits.
A flux nap was taken at approxima tely 3? powe r uith cont rol bank D at its revised insertion linit, and the reasured value for F(delta H) wa s ve ri f ied to be acceptable.
After obtaining PRC concurrence fo r powe r operation in conpliance with the revised insertion limit, which was imple-reni ed adninistratively, reactor power was increased to 307.
k'ith D hank near its revised insertion limit at 30% power, flux nap results again provided an acceptable reasured value for F(delta H).
Scheduled Corrective Action The revised insertion limits along with the supporting safety evaluation vill be subnitted to the NPC as a Proposed Tec.hnical Specification Change for Unit 1, Cycle 2 operation.
An investigation is unde r uay *o de te rnine the prinary cause of the power tilt.
Actione Taken to Prevent Recurrence Once she primary cause of the power tilt has been de terrined, a plan will be developed and inplemented that util either elin'nate the primary cause for the pow r tilt, or acconedate i ts e f fec t s.
1937 31I
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| 05000338/LER-1980-001-01, /01T-0:on 800118,during Review for IE Bulletin 79-14,letdown Lines 3/4-CH-275-1502Q1 & 3/4-CH-123-1502-Q2 Reported Overstressed.Caused by Incorrect Valve Weights Used in Pipe Stress Calculations | /01T-0:on 800118,during Review for IE Bulletin 79-14,letdown Lines 3/4-CH-275-1502Q1 & 3/4-CH-123-1502-Q2 Reported Overstressed.Caused by Incorrect Valve Weights Used in Pipe Stress Calculations | | | 05000338/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000339/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000339/LER-1980-001-03, /03L-0:on 800423,w/unit in Mode 6 Following Fuel Loading,Rhr Sys Inlet Valve MOV-2700 Ran Closed,Causing Loss of Operable RHR Loop.Caused by Blown Signal Comparator Card Power Supply Fuse in Process Control Sys.Card Replaced | /03L-0:on 800423,w/unit in Mode 6 Following Fuel Loading,Rhr Sys Inlet Valve MOV-2700 Ran Closed,Causing Loss of Operable RHR Loop.Caused by Blown Signal Comparator Card Power Supply Fuse in Process Control Sys.Card Replaced | | | 05000338/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000338/LER-1980-002-01, /01T-0:on 800107,S&W Informed Util That Stress on Vertical Supports RH-R-19 & WS-R-316 & Snubbers SI-HSS-101B,101C & 107A Exceeded Allowable Design Values. Caused by Wrong Valve Weights Used in Design Calculations | /01T-0:on 800107,S&W Informed Util That Stress on Vertical Supports RH-R-19 & WS-R-316 & Snubbers SI-HSS-101B,101C & 107A Exceeded Allowable Design Values. Caused by Wrong Valve Weights Used in Design Calculations | | | 05000339/LER-1980-002-01, /01T-0:on 800429,during Structural Review for IE Bulletin 79-14,S&W Discovered Overstressed Pipe Hangers in Svc Bldg.Caused by Error in Stress Analysis Used to Design Pipe Hanger Supports.Mods Will Be Implemented | /01T-0:on 800429,during Structural Review for IE Bulletin 79-14,S&W Discovered Overstressed Pipe Hangers in Svc Bldg.Caused by Error in Stress Analysis Used to Design Pipe Hanger Supports.Mods Will Be Implemented | | | 05000339/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000339/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000339/LER-1980-003-03, /03L-0:on 800528,2H Diesel Generator Frequency & Voltage Response Was Not Verified Every 8-h,contrary to Tech Spec.Caused by Faulty Lead on Monitoring Instrumentation. Offsite Power Sources Verified & Found Acceptable | /03L-0:on 800528,2H Diesel Generator Frequency & Voltage Response Was Not Verified Every 8-h,contrary to Tech Spec.Caused by Faulty Lead on Monitoring Instrumentation. Offsite Power Sources Verified & Found Acceptable | | | 05000338/LER-1980-003-03, /03L-0:on 800121,nuclear Instrumentation Sys Power Range Channel 4 Declared Inoperable Due to Erratic Power Bistable Operation.Caused by Failed Ion Chamber Detector.Ion Chamber Detector Replaced | /03L-0:on 800121,nuclear Instrumentation Sys Power Range Channel 4 Declared Inoperable Due to Erratic Power Bistable Operation.Caused by Failed Ion Chamber Detector.Ion Chamber Detector Replaced | | | 05000338/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000339/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000339/LER-1980-004-03, /03L-0:on 800519,during Mode 3 Operation,Steam Generator Level Channel LT-2475 Indicated Level 9% Lower than Two Redundant Channels.Caused by Voltage Drift.Channel Was Placed in Trip Mode | /03L-0:on 800519,during Mode 3 Operation,Steam Generator Level Channel LT-2475 Indicated Level 9% Lower than Two Redundant Channels.Caused by Voltage Drift.Channel Was Placed in Trip Mode | | | 05000338/LER-1980-004-03, /03L-0:on 800109,during Test of Equipment Hatch Emergency Escape Lock,Inner Door Seal Found Leaking When Door Opened & Lock Found to Be Under Slight Vacuum.Caused by Frequent Door Operation.Seals Replaced | /03L-0:on 800109,during Test of Equipment Hatch Emergency Escape Lock,Inner Door Seal Found Leaking When Door Opened & Lock Found to Be Under Slight Vacuum.Caused by Frequent Door Operation.Seals Replaced | | | 05000338/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000338/LER-1980-005-03, /03L-0:on 800110,w/unit in Mode 4,main Steam Isolation Trip Valve TV-MS101C Would Not Close Using Train a Push Button.Caused by Open Auxiliary Relay in Circuit. Relay Replaced from Stock & Tested Satisfactorily | /03L-0:on 800110,w/unit in Mode 4,main Steam Isolation Trip Valve TV-MS101C Would Not Close Using Train a Push Button.Caused by Open Auxiliary Relay in Circuit. Relay Replaced from Stock & Tested Satisfactorily | | | 05000338/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000339/LER-1980-005-03, /03L-0:on 800517,2J Emergency Diesel Generator Tripped After Starting & Operability of 2H Diesel Generator Was Not Verified within 1-h.Caused by Existing Procedures Not Specifying Test Connections Required to Test Diesel | /03L-0:on 800517,2J Emergency Diesel Generator Tripped After Starting & Operability of 2H Diesel Generator Was Not Verified within 1-h.Caused by Existing Procedures Not Specifying Test Connections Required to Test Diesel | | | 05000339/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000339/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000339/LER-1980-006-03, /03L-0:on 800520,during Startup Testing in Mode 3, B Steam Generator Narrow Range Level Channel III Was Observed Reading Below Redundant Level Channels & Drifting Low.Caused by Air Pocket in Steam Generator Sensing Line | /03L-0:on 800520,during Startup Testing in Mode 3, B Steam Generator Narrow Range Level Channel III Was Observed Reading Below Redundant Level Channels & Drifting Low.Caused by Air Pocket in Steam Generator Sensing Line | | | 05000338/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000338/LER-1980-006-03, /03L-01:on 800111,w/unit in Mode 3,casing Coolant Pump Discharge Valve MOV-RS-100A Was Discovered to Be Inoperable.Caused by Removal of Casing Cooling Tank Level Transmitter LT-RS103A During Execution of Design Change | /03L-01:on 800111,w/unit in Mode 3,casing Coolant Pump Discharge Valve MOV-RS-100A Was Discovered to Be Inoperable.Caused by Removal of Casing Cooling Tank Level Transmitter LT-RS103A During Execution of Design Change | | | 05000338/LER-1980-007-03, /03L-0:on 800111,during Mode 3 Reactor Heating Containment Average Temp Decreased to 85 F,Less than Tech Specs.Caused by Insufficient Procedural Precautions. Removed Chiller from Svc.Monitored Temp | /03L-0:on 800111,during Mode 3 Reactor Heating Containment Average Temp Decreased to 85 F,Less than Tech Specs.Caused by Insufficient Procedural Precautions. Removed Chiller from Svc.Monitored Temp | | | 05000339/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000339/LER-1980-007-03, /03L-0:on 800521,during Mode 3 Operation,Channel in Tave Protection Loop 2 Failed in High Direction.Cause Is Unknown.Failed Channel Was Removed from Svc & Replaced by Spare | /03L-0:on 800521,during Mode 3 Operation,Channel in Tave Protection Loop 2 Failed in High Direction.Cause Is Unknown.Failed Channel Was Removed from Svc & Replaced by Spare | | | 05000339/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000338/LER-1980-008-01, /01T-0:on 800111,during Review for IE Circular 78-08,S&W Found Control Room Air Conditioning Chiller Units Control Panel Not Qualified to Seismic Category I Requirements.Cause Unknown.Vendor Reviewing Components | /01T-0:on 800111,during Review for IE Circular 78-08,S&W Found Control Room Air Conditioning Chiller Units Control Panel Not Qualified to Seismic Category I Requirements.Cause Unknown.Vendor Reviewing Components | | | 05000339/LER-1980-008-03, /03L-0:on 800521,during Mode 3 Operation,Redundant Channel Protection Was Lost.Caused by Personnel Not Placing Tave Protection Loop Failed Channel in Trip Mode within Required Time.Failed Channel Placed in Trip Mode | /03L-0:on 800521,during Mode 3 Operation,Redundant Channel Protection Was Lost.Caused by Personnel Not Placing Tave Protection Loop Failed Channel in Trip Mode within Required Time.Failed Channel Placed in Trip Mode | | | 05000338/LER-1980-009-03, /03L-0:on 800111,while Performing Periodic Test on Main Steam Safety Valves,Found Valves SV-MS-101-A & C, SV-MS-102-A & B & SV-MS-105-A & C Did Not Lift at Pressure Setpoints Per Tech Specs.Caused by Setpoint Drift | /03L-0:on 800111,while Performing Periodic Test on Main Steam Safety Valves,Found Valves SV-MS-101-A & C, SV-MS-102-A & B & SV-MS-105-A & C Did Not Lift at Pressure Setpoints Per Tech Specs.Caused by Setpoint Drift | | | 05000339/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000339/LER-1980-009-03, /03L-0:on 800522,power Supply for Main Steam Pressure Protection Channel III Failed High,Causing Steam Line Pressure Mismatch.Caused by Failed Card in Power Supply.Card Was Replaced & Calibr | /03L-0:on 800522,power Supply for Main Steam Pressure Protection Channel III Failed High,Causing Steam Line Pressure Mismatch.Caused by Failed Card in Power Supply.Card Was Replaced & Calibr | | | 05000338/LER-1980-010-01, /01T-0:on 800111,during Review for IE Bulletin 79-14,S&W Found Stress on Vertical Rod Hangers SW-H-162A & SW-H-160A to Be Over Design Allowable.Caused by Incorrect Valve Weights Used in Pipe Support Design Calculations | /01T-0:on 800111,during Review for IE Bulletin 79-14,S&W Found Stress on Vertical Rod Hangers SW-H-162A & SW-H-160A to Be Over Design Allowable.Caused by Incorrect Valve Weights Used in Pipe Support Design Calculations | | | 05000339/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000339/LER-1980-010-01, /01T-0:on 800523,during Review of ECCS Piping for Fluid Temp Below 70 F,Determined That Loadings on Both Low Head Safety Injection Pump Nozzles Exceeded Design Stress Allowables.Caused by Deficiency in Sys Stress Analysis | /01T-0:on 800523,during Review of ECCS Piping for Fluid Temp Below 70 F,Determined That Loadings on Both Low Head Safety Injection Pump Nozzles Exceeded Design Stress Allowables.Caused by Deficiency in Sys Stress Analysis | | | 05000339/LER-1980-011-03, /03L-0:on 800520,personnel Air Lock Doors Would Not Seal Completely,Causing Air Leakage While Performing Surveillance Test 2-PT-62.4.Caused by Leakage Past Seals on Inner & Outer Doors.New Seals Were Installed | /03L-0:on 800520,personnel Air Lock Doors Would Not Seal Completely,Causing Air Leakage While Performing Surveillance Test 2-PT-62.4.Caused by Leakage Past Seals on Inner & Outer Doors.New Seals Were Installed | | | 05000339/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000338/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000338/LER-1980-011-03, /03L-0:on 800115,when Sys Sample Monitoring Pumps Were Removed from Svc,Ventilation Vent Stack B Particulate & Gas Radiation Monitors RM-VG112 & 113 Were Rendered Inoperable.Design Changes Will Add High Range Monitor | /03L-0:on 800115,when Sys Sample Monitoring Pumps Were Removed from Svc,Ventilation Vent Stack B Particulate & Gas Radiation Monitors RM-VG112 & 113 Were Rendered Inoperable.Design Changes Will Add High Range Monitor | | | 05000339/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000339/LER-1980-012-03, /03L-0:on 800618 While in Mode 2,control Rod Demand Position Indication Noted 19 Steps Higher than Associated Rod Position Indication.Caused by Drift of Rod Position Indicator Channel.Channel Recalibr | /03L-0:on 800618 While in Mode 2,control Rod Demand Position Indication Noted 19 Steps Higher than Associated Rod Position Indication.Caused by Drift of Rod Position Indicator Channel.Channel Recalibr | | | 05000338/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000338/LER-1980-012-03, /03L-0:on 800111,during Testing in Mode 3 to Verify Main Steam Trip Valve Closure Time,Trip Valve Failed to Close Fully within Required Five Seconds.Cause Unknown. Valve Was Retested.Closure Time within Acceptable Limits | /03L-0:on 800111,during Testing in Mode 3 to Verify Main Steam Trip Valve Closure Time,Trip Valve Failed to Close Fully within Required Five Seconds.Cause Unknown. Valve Was Retested.Closure Time within Acceptable Limits | | | 05000338/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000338/LER-1980-013-03, /03L-0:on 800114,while Using Steam Driven Feedwater Pump 1-FW-P-2 to Add Feedwater to Steam Generator A,Water Leaked from Pump Oil Cooler Gasket.Caused by Blown Gasket.Gasket Replaced | /03L-0:on 800114,while Using Steam Driven Feedwater Pump 1-FW-P-2 to Add Feedwater to Steam Generator A,Water Leaked from Pump Oil Cooler Gasket.Caused by Blown Gasket.Gasket Replaced | | | 05000339/LER-1980-013-03, /03L-0:on 800520 & 27,w/unit in Hot Standby, Samples of Boron Injection Tank & C Boric Acid Storage Found to Contain Less than 20,000 Ppm Boron.Caused by Leaks Past Inlet Valves MOV-2867 a & B.Switch Settings Increased | /03L-0:on 800520 & 27,w/unit in Hot Standby, Samples of Boron Injection Tank & C Boric Acid Storage Found to Contain Less than 20,000 Ppm Boron.Caused by Leaks Past Inlet Valves MOV-2867 a & B.Switch Settings Increased | | | 05000339/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000338/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000338/LER-1980-014-03, /03L-0:on 800113,during Insp of Auxiliary Feedwater Pump 1-FW-P-2 Outboard Bearing,Discovered Inboard Side of Thrust Bearing Had Been Wiped.Caused by Lack of Oil. Bearing Replaced & Pump Returned to Svc | /03L-0:on 800113,during Insp of Auxiliary Feedwater Pump 1-FW-P-2 Outboard Bearing,Discovered Inboard Side of Thrust Bearing Had Been Wiped.Caused by Lack of Oil. Bearing Replaced & Pump Returned to Svc | |
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