ML19259B213

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IE Insp Rept 50-267/78-19 on 781113-16.Noncompliance Noted: Failure to Address Areas in Subsequent Training Lectures for Which Scores Less than 80% Had Been Obtained
ML19259B213
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 12/04/1978
From: Dickerson M, Johnson E, Madsen G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML19259B188 List:
References
50-267-78-19, NUDOCS 7901170171
Download: ML19259B213 (7)


See also: IR 05000267/1978019

Text

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U. S. flUCLEAR REGULATORY COMMISSION

OFFICE OF ItiSPECTI0il AND ENFORCEMEflT

REGION IV

IE Inspection Report No. 50-267/78-19

Docket flo. 50-267

License No. DN1-34

Licensee:

Public Service Company of Colorado

P. O. Box b40

Denver, Colorado

80201

Facility Name:

Fort St. Vrain fiuclear Generating Station

Inspection At:

Fort St. Vrain Si te, Platteville, Colorado

Inspection Conducted:

November 13-16, 1978

Inspectors:

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M. W. Dickerson, Reactor Inspector

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E. II. Johnson, Reactor Inspector

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Accompanying

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Personnel:

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G.11. Verduzcd Reactor Inspector (Training)

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Approved by:

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G. L. Madsen, Chief, Reactor Operations

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and Nuclear Support Branch

Inspection Summary

Inspection on November 13-16, 1978 (Report No. 50-267/78-19)

Areas Insp_ected:

Routine, unannounced inspection of training; requalifica-

tion training; reserve shutdown system; review of plant operations; and

follow-up on inspector identified and unresolved problems.

The inspection

involved fifty-six (56) inspector-hours on-site by two (2) NRC inspectors.

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DETAILS

1.

Persons Contacted

Public Service Company of Colorado

  • L. Brey, QA Manager

M. Bruxvort, Electrician

R. Erwin, Junior Storekeeper

D. Evans, Reactor Operator

W. Franek, Results Supervisor

M. Ferris, Engineer Technical Services

D. Frye, Plant Mechanic

  • J. Gamm, Supervisor Technical Services
  • E. Hill, Supervisor Operations
  • W. Hillyard, Administrative Services Manager

D. Hood, Shift Supervisor, Operations

J. Hunter, Reactor Operator

  • F. Mathie, Operations Manager

S. Shaeffer, Reactor Operator

L. Singleton, Shift Supervisor, Operations

J. Solakiewicz, QA Engineer

M. Thiel, Temporary Employee

D. Warembourg, Manager, Nuclear Production

R. Wadas, Training Supervisor

V. Wetzbarger. Supervisor QC and Scheduling

  • Attended exit interview.

2.

Licensee Action on Previous Inspection Findings

(Closed) Unresolved Item (50-267/78-08):

Inconsistencies in procedure

SR 5.3.5-A.

Surveillance procedure SR 5.3.5-A, " Hydraulic Power

System Calibration," was revised and approved on October 30, 1978, to

resolve the inconsistencies.

3.

Review of Plant Operations

During the inspection, the conduct of plant operations was reviewed

to determine that they confonn to requirements of the facility license

and the licensee's procedures.

Included in the review were observation

of control room activities, logs, and records.

In addition, the

inspector completed a tour of accessible areas.

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Results:

Of the five (5) areas inspected, one (1) item of noncompliance

iiaiToiind during the review of requalification training (Deficiency-

Failure to address areas in subsequent training lectures for which scores

less thari 807, had been obtained - paragraph 6).

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The inspector's review of this area included:

Shift Supervisor's Log (September 13 - November 12,1978)

Reactor Operator's Log (September 13 - November 12,1978)

Surveillance Logs 1-3 (September 13 - November 12,1978)

Operations Order Book

Form l's (Jumper Log)

Plant Trouble Reports

a.

Tour

During the tour of the facility, observations were made in the

following areas:

Monitoring Instrumentation

Radiation Controls

Housekeeping

Fluid Leaks

Piping Vibrations

Hanger / Seismic Restraints

Clearance Tags

Annunciators

Control Room Manning

During this tour, the inspector identified several areas which

require some remedial action.

Included were several snubbers

which appeared low on oil; greater than normal oil which had

collected under the two (2) diesel generators; and housekeeping

on the lower two levels of the reactor building.

b.

Fluctuations

Fluctuations were observed on November 4,1978, during Test RT-500.

The purpose of the test was to determine the influence of core

flow resistance on the threshold power for fluctuations and to

obtain FM data with revised instrumentation.

Data was also to

be obtained with the reg-rod held in a fixed position.

The fluctuations were observed during a rise in power from 43%

to 49% while the core pressure drop was set at 2.85 psig.

Initially the fluctuations were noted as swings of abc it 1.5%

on the channel VII nuclear detector and + 20 F of the :nuin steam

temperature. After approximataly 30 to 35 minutes into the

fluctuation the exit temperature for steam generator module

B-1-1 dropped approximately 120 F.

Some temperature drops were

also noted on other steam generator modules. With the

observation of the main steam temperature swings the reactor

power was reduced 35% to terminate the fluctuations.

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Also noted during this time were a drop in refueling region 13

exit temperature of about 2000F and an increase in refueling

region 12 temperature approaching this same magnitude. At

present, the reactor is being operated at a low pressure drop

across the core in a mode to preclude fluctuations while the

data gathered during the test is evaluated and until tests are

permitted to resume.

No items of nonconformance or deviations were identified.

4.

Reserve Shutdown System

The inspector reviewed surveillance procedures, operating procedures,

records of tests and procedures performed, and inspected the reserve

shutdown system to determine that the licensee conformed to technical

specification, the FSAR and approved procedures.

Review of the last quarterly surveillance procedure 5.1.2 ad-Q,

" Reserve Shutdown Hopper Pressure Test," performed September 11,

1978, indicated in Step 5.3.2 that all locking devices which were

removed from manually operated valves were replaced.

However, during

observation of these valves by the inspector on the morning of

November 14, 1978, valves V11684, V11333, V11672 and V11674 were

found to have broken seals (locking devices). Additionally, valves

V11652 and V11641 had no seals in place on the valves. At this

same time the cover plate was also observed to be off of PS 1106-33.

A check of the current startup records and those for startup 78-09

dated September 26, 1978, contained a system 12 sign-off sheet

indicating the system status was acceptable based on the statement

" System operable based on the fact that it has remained in normal

operating configurations or that all portions cleared out, shutdown

or altered for maintenance have been returned to service." In

addition, no locked valve check-off list was completed for system 12

(Reserve Shutdown System).

A check of startup 78-08 records for

August 20, 1978, were similar to those for 78-09. A check of startup

78-07 records for August 4, 1978, were similar to those for 78-08

and 78-09 except that the sealed valve list indicated a "not

applicable" for the system 12 valves.

Since the time when the seals were removed or broken appears to be

indeterminate, this matter is considered unresolved pending develop-

ment of a satisfactory method by the licensue for assuring that

locked valves (open or closed) are appropriately checked prior to

and during operation where necessary.

No items of nonconfomance or deviations were identified.

b

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5.

Training

The inspector reviewed various elements of the overall training

program by direct .,uestioning of personnel and review of training

records.

fio items of noncompliance were identified.

It was noted, however,

that no portion of the overall training curriculum is devoted to

plant systems familiarization for craf tsmen.

A licensee representative

as well as well as craftsmen interviewed indicated that such an

addition to the training program would be most beneficial.

6.

Requalification Training

The inspector reviewed the requalification program including the

following records and documents:

Lecture Schedule

Attendance Records

Control Manipulative Records

Annual Examination for 1977

Composite Personnel Training Records

Personnel Requalification Files

Within the scope of this inspection effort, one (1) item of noncompli-

ance was identified.

Four (4) reactor operators scored less than 80% on the safcty and

emergency systems (category E) portion of the 1977 annual examination.

Contrary to 10 CFR 55, Appendix A, Section 2, the requalification

training program administered subsequent to this examination did not

address safety and emergency systems.

This is a deficiency.

10 CFR 55, Appendix A, Section 4c. requires " systematic observation

and evaluation of the performance and competency of licensed operators

and senior operators by supervisors and/or training staff members

including evaluation of actions taken or to be taken during abnormal

and emergency conditions."

Implicit in this requirement is that

evaluations be done in a timely manner (i.e., within one (1) or two

(2) working days) and that evaluations include discussions with watch

personnel as well as review of operator logs, recorder charts, etc.

The inspector noted that plant management reviews generally did not

include a qualitative statement addressing the operator's actions

or give indication of the depth of the evaluation.

This is

particularly significant where evaluation of shift supervisors are

concerned.

Futher, it should be pointed out that evaluations may

be done by training staff members.

The absence of a date on the

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two (2) evaluation sections (15 and 18) of the Fort St. Vrain form 0-6,

reactivity manipulation form, leaves some question as to the

timeliness of the evaluation. This is an open item pending revision

of the 0-6 form.

No other items of noncompliance or deviations were identified in

this area.

7.

Unresolved Items

Unresolved items are matters about which more information is required

in order to ascertain whether they are acceptable items, items of

noncompliance, or deviations.

The following item was identified

during the inspection:

7819-1 Determination of status of locked valves - paragraph 4.

8.

Exit Interview

An exit interview was conducted with representatives of the licensee

on November 16, 1978, at the conclusion of the inspection.

At the

interview, the inspectors discussed the findings indicated in the

previous paragraphs.

The licensee acknowledged their findings.