ML19257D015

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LER 79-156/03L-0:on 791230,during Visual Insp,Local Lexan Reservoir Tube for Snubber 1-RC-HSS-873 Found Damaged & Empty.Apparently Caused by C Steam Generator Blanket Heat. Snubber Replaced & Equipped W/Stainless Steel Reservoir
ML19257D015
Person / Time
Site: North Anna Dominion icon.png
Issue date: 01/29/1980
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19257D008 List:
References
LER-79-156-03L, LER-79-156-3L, NUDOCS 8001310214
Download: ML19257D015 (2)


Text

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  • i nn I o 3 l the local lexan reservoir tube for snubber 1-RC-HSS-873 was found damaged and co-nletolly o 4 l enpty of fluid. The health and safety of the veneral public were not affected by thic I o s l event. Paportable pursuant to T.S. 6. 9 .1. 9 . b . I O 6 l l 0 7 l l 0 H l 80 7 8 9 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SU6CCDE COYPONEN T CODE SUSCODE SUWCODE 7

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43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o l Hea t from "C" steam generator blanket apparently caused the lexan reservoir tube to l

[,)i; distort which resulted in the release of the snubber oil. The damaned snubber war I

, ,  ; replaced with a spare snubber calibrated to the proper environmental zone and oculpped I

,i ;3; l with a remote stainless steel reservoir. l li 141 I l 7 8 9 80 ST S ,SCAER OTHER STATUS DISCOV RY DISCOVERY DESCRIPTION Visual Inspection 7

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l1 l7l 7 8 9 l0 l 0 0l@lZl@l 11 12 13 80 PERSONNE L INJUHtES NUVRE R DESCRIPTION i R l0[0l0lgl 7 8 9 11 12 80 LOSS OF OR OAVAGE TO F ACILITY TYPE D E scrlP rlO N l i l oH l9 I ZI@l10 7

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Virginia Electric and Power Company North Anna Powt. Station, Unit #1

Attachment:

Page 1 of 1 Doc ke t No. 50-338 Report No. LER 79-156/03L-0 Description of Event During a visual inspection of hydraulic snubbers not accessible during reactor operation, snubber 1-RC-HSS-873 failed to meet the applicable acceptance criteria due to a lack of oil in the local reservoir and damage to the lexan reservoir tube.

Probable Consquences of Occurrence The af fected snubbe r is located on Loop "C" RTD bypass line 1"-RC-1502-Q1.

Without fluid in the reservoir, it was possible that the snubber could have lost its ability to become a rigid strut when subjected to an excessive rate of movement due to seismic ef fects. The health and safety of the general public were not af fected by this event. No generic implications exist for this occurrence.

Cause of Event The distortion of the lexan reservoir tube and subsequent loss of snubber oil apparently resulted from the neat emitted by the "C" steam generator blanket.

Immediate Corrective Action A spare snubber, calibrated to the proper environmental zone, was installed in place of the damaged snubber and the fluid reservoir for the new snubber was changed from a local lexan reservoir to a remote stainless steel reservoir.

Scheduled Corrective Action No scheduled corrective action is required.

Actions Taken to Prevent Recurrence No further actions are required.

1845 146