05000313/LER-1979-024-03, /03L-0:on 791206,during Test of Turbine Driven Emergency Feedwater Pump,Pump Was Declared Inoperable.Caused by Loose Speed Governor Lock Nut on Turbine Pump Drive.Pump Speed Increased & Lock Nut Tightened

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/03L-0:on 791206,during Test of Turbine Driven Emergency Feedwater Pump,Pump Was Declared Inoperable.Caused by Loose Speed Governor Lock Nut on Turbine Pump Drive.Pump Speed Increased & Lock Nut Tightened
ML19257B918
Person / Time
Site: Arkansas Nuclear 
Issue date: 01/10/1980
From: Bramlett L
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19257B916 List:
References
LER-79-024-03L-01, LER-79-24-3L-1, NUDOCS 8001210230
Download: ML19257B918 (1)


LER-1979-024, /03L-0:on 791206,during Test of Turbine Driven Emergency Feedwater Pump,Pump Was Declared Inoperable.Caused by Loose Speed Governor Lock Nut on Turbine Pump Drive.Pump Speed Increased & Lock Nut Tightened
Event date:
Report date:
3131979024R03 - NRC Website

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