05000338/LER-1979-134-03, /03L-0:on 790928,six Valves Failed to Close on First Signal of Containment Depressurization Test But Did So on Second Signal.Cause Undetermined.Valves Will Be Rechecked & Repaired as Necessary

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/03L-0:on 790928,six Valves Failed to Close on First Signal of Containment Depressurization Test But Did So on Second Signal.Cause Undetermined.Valves Will Be Rechecked & Repaired as Necessary
ML19254E286
Person / Time
Site: North Anna Dominion icon.png
Issue date: 10/26/1979
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19254E281 List:
References
LER-79-134-03L, LER-79-134-3L, NUDOCS 7910310417
Download: ML19254E286 (2)


LER-1979-134, /03L-0:on 790928,six Valves Failed to Close on First Signal of Containment Depressurization Test But Did So on Second Signal.Cause Undetermined.Valves Will Be Rechecked & Repaired as Necessary
Event date:
Report date:
3381979134R03 - NRC Website

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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION

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LICENSEE EVENT REPORT CONTROL BLOCK: l l

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8 60 61 DOCKET NUMBEH 68 69 EVENT DATE 14 73 REPORT D ATE 80 EVENT DESCRIPTION AND PROBA0LE CONSEQUENCES h 1 n September 28, 1979, during the performance of the 18 month Containment Depressuri-l 0

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zation Actuation test, valves TV-SW101A and B, MOV-SW110A and B, and MOV-SW114A and B l o 3 l failed to close on the first CDA test signal but did close when the second CDA signal l o

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Since all these valves are administrative 1y kept closed and opened l

lo is i l only when testing is required, the health and safety of the general public were not I

l o l 7 l l af fected by their failure to close.

Reportable pursuant to T.S. 6.9.1.9.b.

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o lThe cause for the valves not closina has not as yet been determined.

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During the Dresent refuelino outaae. tha valves wl11 ha 1

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W. R. Cartwricht p,4oy e NAME OF PREPARER

Virginia Electric and Power Comptay North Anna Power Station, Unit #1 Atta :hment : Page 1 of 1 Docket No. 50-338 Report No. LER 79-134[.L-0

Description of Event

On September 28, 19 79, with e"

at cold shutdown, service water val TV-SW101A and B, MOV-SW110A a, B, and MOV-SW114A and B failed to close e th e first CDA test signal but did close when the second CDA si,w

  • was initiated during the performance of the 18 month Containment Depressu-

'on Actuation Functional Test.

Probable Consequences of Occurrence The consequences c' this event were minimal because all six valves, which are located on the su. y and return lines for the containment recirculation air r

cooling coils, are administrative 1y kept closed to prevent treated water in the service water system from entering the chilled water system and are opened only when testing on the valves is required.

(Normally, chilled water flows through the containment recirculation air cooling coils.) As a result, the health and safety of the general public were not affected by this event.

No generic implications exist for this occurrence.

Cause

The cause for th. valves not closing on the first CDA signal has not been determined at this time.

Further testing and/or maintenance during the outage will be performed to determine the cause.

Immediate Corrective Action

A maintenance report has been submitted.

Scheduled Corrective Action The six valves will be checked and repaired as necessary during the present refueling outage.

Actions Taken to Prevent Recurrence No further actions are required.

4 209