ML19253B912
| ML19253B912 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 08/08/1975 |
| From: | Lawyer L METROPOLITAN EDISON CO. |
| To: | |
| Shared Package | |
| ML19253B910 | List: |
| References | |
| NUDOCS 7910310642 | |
| Download: ML19253B912 (3) | |
Text
UNI 1 mww.e vila Islaad Unit 1 DATE A-eust 8. 1079 COMPLE M BY L. L. Lavfer TEL. NO. 215-929-3601 Ext. 567 DAILY PLANT POWER OUTPUT MONTH July 1075 DAY AVERAGE DAILY MWe-net DAY AVERAGE DAILY MW-net 1
795 21 777 2
788 22 781 3
785 23 777 h
790 2h 77k 5
788 25 777 6
788 26 790 7
786 27 718 8
785 28 608 9
783 29 609 10 78h 30 629 11 788 31 781 12 785
" 13 78h 14 785 15 78h 16 781 17 777 1505 297 18 772 19 777 20 776 7910810 (h $/
f
CL72* Alit : Reactor was run at ag proxinatlly lod full power from July 1,19T5 UNIT NAllE Three ffile Island l' nit I to July M,1975 On July 27, 19T5 power was relucad to 78% to perform repairs on the B f tain Feadwater Pump. Power was returned CATE Aurist 8.19T5 to 100% on July 31, 1975 COfTLETED BY L.
I,.
Lawyer TEL. NO. 21%929-36' 1 Ex1 56T REPORT MONTH July 1975 PLANT SL0TD0WNS TYI'E METHOD OF F-FOPCFD DUPATION SHUITING D0kii NO.
DATE S-CCHEDULED (HOURS)
REASON (1)
THE REACTOR (2)
C0f2 TENTS 13 T-2T-T5 F
0.0 A
NA Transmission gears in B main feedwater pump were worn and needed repair. (Monnuclear)
I (1) REASON:
(2) METHOD:
A-EQUIntENT FAILURE (EXFIAIN)
A-MANUAL B-MAINT. OR TEST B-MANUAL SCRAM C-RFFUELING C-4" LMATIC SCRAM D-REGULATORY RESTRICTION E-OPERA'IOR TRAINING AND LICENCE EXAMINATION F-ADMINISTRATIVE G-OPERATIONAL ERROR
( EXPIAIN)
W CD W
W 00
UNIT NA.G T'r-- 91' 9 ! a_ 4 "-ft OATE f_..,._.-.
,q-e COMPLETED SY i. ' ' a n-TEL. NC. Sie o?q Va' 567 ev.
0PERATING STATUS 1.
REPORTING PERIOD:
^ C C '-
'c
' 0!
THRCUGH c 'e n
-e GROSS HOURS IN REPCRTING PERIOD:
'LL 2.
CURPI*iTLY AUTHORIZED PCWER LE7EL Wt ?coc We-NET v
D'AX!MLN DEPENDAELE CAPACITY - MDC) 3 POWER LEVEL 'It WHICH RESTRICTED (IF ANY):
'ic ' -
k.
REASCNS ftR RESTRICT!CNS (IF ANY): Not Applicable i
THIS CLHULATIVE MCh""M YR *0-DATE M PATE 1
5 HOURS REAC'tB WAS CRITICAL.
7LL,1
-hL-6 a
'acc o r
6.
REAC'ICR RESERVE SHUTDOWN HOURS O
c a
7 HOURS GENERATCR CN-LINE 7LL L2c?.c FAe'_e 8.
UNIT RESERVE SHUTDCVN HCf?RS..
0 0
a 9 GRCSS THEPyAL PCVER GENERATED (WM) 1.827.63L 10.L70.c?2 16.66?."L 10.
GROSS ELECTRICAL PCWER GENERATED (WH).
6CL,168 3,532.611 C.6L2. 2 C' 11.
NET ELECTRICAL PCWER GE'FRATED (WH) 568,830 3,307,703 5.289.c19 12.
REAC70R AVAILABILITY FACTOR (1) 10CT
$8.C5 M. 35 13 UNIT AVAIIABILITY FAC"CR (2) 1CCT Sk.5%
85.8%
- 14. L71IT CAPACITY FACTOR (3) 96.5%
82.15 a3.55 15 FORCED OU:' AGE RATE (L)
C 10.7%
8.IT 16.
SHU"DC'.7i3 SC:!EDULED TO 3EGIN IN. VEX"' 6 MON'HS (STA~E "'YFE, DATE, A'O CUPATION OF EACH): Refueling 1/76 10 weeks 17 IF ShV"DCW'i AT END OF REPCRT PERICD, ESTIMA*ED CATE OF CTAR"'UF:
- iA
- 18. UNITS IN TEST STA?JC (PRICR *0 COMMIPCIAL CPERATICN). NCT AFPLICA3LE (1) REACTR AVAILABILITY FAC' CR= """' '"' '"'" dA3 E AL
- 100 ELC3 fiCUP2 :N REPORTING FE3!;D (2) UNIT AVAILABILITY FACTCR= f'r r;r :rt
+r qY.; I y7. m R..'.7r,.
..s.,
m A,.f.. CUR.2 4 - r-r
+100 J
"L a n x,,,,,
- -~a er r~o vA-"" ~ ' ' " " " pngrg. g ' 'pA="ra
- ^
(3) UNIT CAPACITY ' ACOR-
~
MCC t We - net )
JROJ.3 HOURS I., REFCETING FERI;;
r gera r.r' ' "
- "v
,, r g (4) FCRCED CU'" ACE RATE hCURS GE'iERA70R CN-LINE + FCRCEO CU"' AGE EiCUFJ
' ~