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| 05000267/LER-1976-001-01, LER 76/001:on 760105,mod Made to Certain Hydraulic Oil Sys Relief Valves W/O Proper Prior Approval.Caused by Misunderstanding by Personnel Performing Work.Review of Rules Held W/Working Foremen | LER 76/001:on 760105,mod Made to Certain Hydraulic Oil Sys Relief Valves W/O Proper Prior Approval.Caused by Misunderstanding by Personnel Performing Work.Review of Rules Held W/Working Foremen | |
| 05000267/LER-1976-001, LER 76/001:on 760113,during Shutdown,Inverter Supplying Noninterruptible Bus Failed.Backup Transformers Put Into Svc.Caused by Blown 150-amp Fuse.No Cause Could Be Found. Inverter Returned to Svc | LER 76/001:on 760113,during Shutdown,Inverter Supplying Noninterruptible Bus Failed.Backup Transformers Put Into Svc.Caused by Blown 150-amp Fuse.No Cause Could Be Found. Inverter Returned to Svc | |
| 05000267/LER-1976-002, LER 76/002:on 760201,during Cable Dressing,Battery Charger Input Breaker Tripped.Power Cable Insulation Cut by Conduit Shorting Cable to Ground.Temporary Junction Box & Terminal Installed | LER 76/002:on 760201,during Cable Dressing,Battery Charger Input Breaker Tripped.Power Cable Insulation Cut by Conduit Shorting Cable to Ground.Temporary Junction Box & Terminal Installed | |
| 05000267/LER-1976-003, LER 76/003:on 760206,during Weekly Surveillance Test on 1B Standby Generator Set,Output Breaker Would Not Close.Caused by Store Energy Arm Shaft Keeper & Arm Falling Off,Reducing Spring Force to Below Requirements | LER 76/003:on 760206,during Weekly Surveillance Test on 1B Standby Generator Set,Output Breaker Would Not Close.Caused by Store Energy Arm Shaft Keeper & Arm Falling Off,Reducing Spring Force to Below Requirements | |
| 05000267/LER-1976-003-01, :on 761220,during Weekly Surveillance Test, Clicking Sound at Engine & Intermittent Emergency Fire Water Pump 1B Run Alarm Detected.Caused by Failure of Drive Cable Due to Normal Wear.Cable Replaced |
- on 761220,during Weekly Surveillance Test, Clicking Sound at Engine & Intermittent Emergency Fire Water Pump 1B Run Alarm Detected.Caused by Failure of Drive Cable Due to Normal Wear.Cable Replaced
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| 05000267/LER-1976-004, LER 76/004:on760206,during Weekly Surveillance on 1A Standby generator,1B Engine Partially Declutched Under Load.Caused by Clutch Engaging Pressure Not within Acceptable Tolerance | LER 76/004:on760206,during Weekly Surveillance on 1A Standby generator,1B Engine Partially Declutched Under Load.Caused by Clutch Engaging Pressure Not within Acceptable Tolerance | |
| 05000267/LER-1976-004-01, During Investigation of Recurring Alarm,Primary Coolant Pressure Boundary Leak Into Helium Purification Cooler Well 1B Found.Caused by Leaking Piping Flange Internal | During Investigation of Recurring Alarm,Primary Coolant Pressure Boundary Leak Into Helium Purification Cooler Well 1B Found.Caused by Leaking Piping Flange Internal | |
| 05000267/LER-1976-005, LER 76/005:on 760207,during Cold Shutdown,Essential 480-volt Bus 2 Tripped,Causing Trip of Three Circulators.Caused by Electrician Carelessness.Electricians Reminded to Be More Careful | LER 76/005:on 760207,during Cold Shutdown,Essential 480-volt Bus 2 Tripped,Causing Trip of Three Circulators.Caused by Electrician Carelessness.Electricians Reminded to Be More Careful | |
| 05000267/LER-1976-006-02, :on 760227-0302,during Cold Shutdown,Seven Helium Circulator Trips Occurred.Caused by Water Accumulation in Instrument Sensing Lines & Operator Error.Sense Lines Cleared of Water.Operators Counseled |
- on 760227-0302,during Cold Shutdown,Seven Helium Circulator Trips Occurred.Caused by Water Accumulation in Instrument Sensing Lines & Operator Error.Sense Lines Cleared of Water.Operators Counseled
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| 05000267/LER-1976-006, :on 760804,hand Valve HV-2246 Appeared Not to Close Fully When Actuated.Cause Undetermined.Investigation Continuing |
- on 760804,hand Valve HV-2246 Appeared Not to Close Fully When Actuated.Cause Undetermined.Investigation Continuing
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| 05000267/LER-1976-006-01, :on 761219,during Rise to Full Power Testing, Primary Coolant Moisture Level Exceeded Limits of Tech Specs.Caused by Evolution of Water from Pcrv.Purification Sys Removed Excess Water |
- on 761219,during Rise to Full Power Testing, Primary Coolant Moisture Level Exceeded Limits of Tech Specs.Caused by Evolution of Water from Pcrv.Purification Sys Removed Excess Water
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| 05000267/LER-1976-007, A:On 760310,during Isolation of Helium Circulator 1D,static Seal Actuation Line Could Not Be Pressurized. Caused by Component Failure.Circulator Replaced W/Spare | A:On 760310,during Isolation of Helium Circulator 1D,static Seal Actuation Line Could Not Be Pressurized. Caused by Component Failure.Circulator Replaced W/Spare | |
| 05000267/LER-1976-008-01, :on 760322,during Shutdown,Helium Circulator 1A Tripped.Caused by Loss of Bearing Water Due to Instrument Bypass Valve Being Closed Too Quickly.Four Drain Level Indicating Switches Added |
- on 760322,during Shutdown,Helium Circulator 1A Tripped.Caused by Loss of Bearing Water Due to Instrument Bypass Valve Being Closed Too Quickly.Four Drain Level Indicating Switches Added
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| 05000267/LER-1976-008, :on 761101,analysis of Low Temp Absorbers Indicated Inadequate Heat Removal Capacity for Loss of Forced Cooling Accident.Caused by Design Error.Emergency Procedures Changeds |
- on 761101,analysis of Low Temp Absorbers Indicated Inadequate Heat Removal Capacity for Loss of Forced Cooling Accident.Caused by Design Error.Emergency Procedures Changeds
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| 05000267/LER-1976-009-01, During Reactor Shutdown, Bearing Water Pump Suction Valve Stroked W/Circulator Operating.Caused by Failure of Test Crew & Shift Supervisor to Check Work Prerequisite.Personnel Counseled | During Reactor Shutdown, Bearing Water Pump Suction Valve Stroked W/Circulator Operating.Caused by Failure of Test Crew & Shift Supervisor to Check Work Prerequisite.Personnel Counseled | |
| 05000267/LER-1976-009, :on 761116,inconsistency Discovered Between Accident Analysis Assumptions Used in Tech Specs & Fsar. Caused by Oversight in Original Analyses of Tech Spec Bases. Further Analyses Continuings |
- on 761116,inconsistency Discovered Between Accident Analysis Assumptions Used in Tech Specs & Fsar. Caused by Oversight in Original Analyses of Tech Spec Bases. Further Analyses Continuings
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| 05000267/LER-1976-010, Helium Circulators 1A & 1B Tripped.Caused by Bearing Water Pump Trip Due to Decrease in Bearing Water Surge Tank Loop 1 Water Level | Helium Circulators 1A & 1B Tripped.Caused by Bearing Water Pump Trip Due to Decrease in Bearing Water Surge Tank Loop 1 Water Level | |
| 05000267/LER-1976-011, A:On 760520,helium Circulator 1C Tripped Due to Negative buffer-midbuffer Differential Pressure.Caused by Flow Blockage of Buffer Gas Reburn Sys.Plugged Filter Cleaned | A:On 760520,helium Circulator 1C Tripped Due to Negative buffer-midbuffer Differential Pressure.Caused by Flow Blockage of Buffer Gas Reburn Sys.Plugged Filter Cleaned | |
| 05000267/LER-1976-012, Circulator 1B Tripped. Caused by Buffer Seal Malfunction.Sys Operating Procedure for Reset Following Trip Will Be Revised | Circulator 1B Tripped. Caused by Buffer Seal Malfunction.Sys Operating Procedure for Reset Following Trip Will Be Revised | |
| 05000267/LER-1976-013-01, Circulators Tripped Due to Trouble Shooting.Caused by Pulled Module Interlock Circulator Isolation Relays.Modules Inserted | Circulators Tripped Due to Trouble Shooting.Caused by Pulled Module Interlock Circulator Isolation Relays.Modules Inserted | |
| 05000267/LER-1976-013, A:On 760607,circulators Tripped During Trouble Shooting.Caused by Pulled Interlock Circulator Auxiliary Isolation Modules.Procedure Rewritten to Limit Module Removal | A:On 760607,circulators Tripped During Trouble Shooting.Caused by Pulled Interlock Circulator Auxiliary Isolation Modules.Procedure Rewritten to Limit Module Removal | |
| 05000000/LER-1976-014-03, /3L:on 760907,high Vibration at Tube Tension Assembly Detected on 13 of 16 Svc Water Pumps.Caused by Loose Bolts & Galvanic Corrosion at Column Pipe Flanges. Pumps Replaced | /3L:on 760907,high Vibration at Tube Tension Assembly Detected on 13 of 16 Svc Water Pumps.Caused by Loose Bolts & Galvanic Corrosion at Column Pipe Flanges. Pumps Replaced | |
| 05000000/LER-1976-014, Circulator 1B Tripped on Loss of Bearing Water Due to Apparent Decrease of Bearing Water Cavity Differential Pressure.Cause Unidentified | Circulator 1B Tripped on Loss of Bearing Water Due to Apparent Decrease of Bearing Water Cavity Differential Pressure.Cause Unidentified | |
| 05000267/LER-1976-015, Circulator Trip Modules T1BR2 & C21AR2 Failed Pulse Tests & Dew Point Moisture Monitors MM-1119 & MM-1116 Malfunctioned.Cause Not Stated | Circulator Trip Modules T1BR2 & C21AR2 Failed Pulse Tests & Dew Point Moisture Monitors MM-1119 & MM-1116 Malfunctioned.Cause Not Stated | |
| 05000267/LER-1976-016, Handwrritten LER 76-016:on 760617,diesel Engine 1D Exhaust Temp Indicator Switch Failed.Cause Not Stated | Handwrritten LER 76-016:on 760617,diesel Engine 1D Exhaust Temp Indicator Switch Failed.Cause Not Stated | |
| 05000267/LER-1976-017, Module Logic a Would Not Generate Required Trip Signal During Surveillance Testing. Caused by Two Defective Logic Chips.Chips Replaced | Module Logic a Would Not Generate Required Trip Signal During Surveillance Testing. Caused by Two Defective Logic Chips.Chips Replaced | |
| 05000267/LER-1976-018, Circulator 1B Tripped on Negative Buffer Differential Pressure.Caused by Rapid Change in Backup Bearing Water Pressure.Procedure Changed to Manual Isolation Valve Closure | Circulator 1B Tripped on Negative Buffer Differential Pressure.Caused by Rapid Change in Backup Bearing Water Pressure.Procedure Changed to Manual Isolation Valve Closure | |
| 05000267/LER-1976-019, One Steam Water Pump Valve in Each Loop Found Open.Cause Not Stated.Investigation Underway | One Steam Water Pump Valve in Each Loop Found Open.Cause Not Stated.Investigation Underway | |
| 05000267/LER-1976-020, Automatic Water Turbine Start on Helium Circulator 1A Initiated W/Circulator on Steam Tubine Drive.Caused by Three Failed Integrated Circuit Logic Chips.Trip Module Replaced | Automatic Water Turbine Start on Helium Circulator 1A Initiated W/Circulator on Steam Tubine Drive.Caused by Three Failed Integrated Circuit Logic Chips.Trip Module Replaced | |
| 05000267/LER-1976-021, Electrical Sys Upset Tripped Circulator 1B.Caused by Operator Mistakenly Closing Output Breaker During Weekly Surveillance Test.Output Breaker Switches Enclosed W/Bird Cage | Electrical Sys Upset Tripped Circulator 1B.Caused by Operator Mistakenly Closing Output Breaker During Weekly Surveillance Test.Output Breaker Switches Enclosed W/Bird Cage | |
| 05000267/LER-1976-023, Circulator Tripped on Loss of Beaking Water.Caused by Normal Beaking Water Supply Valve Shutting Due to Contact Closure During Calibr of Normal Beaking Water Flow Switch | Circulator Tripped on Loss of Beaking Water.Caused by Normal Beaking Water Supply Valve Shutting Due to Contact Closure During Calibr of Normal Beaking Water Flow Switch | |
| 05000267/LER-1976-025, :on 760803,primary Closure Leak Rate for Circular 1C Penetration Exceeded Limits.Cause Unknown.Investigation Underway |
- on 760803,primary Closure Leak Rate for Circular 1C Penetration Exceeded Limits.Cause Unknown.Investigation Underway
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| 05000267/LER-1976-027, :on 760827,circulator 1B Tripped on Apparent Loss of Bearing Water.Caused by Dry Water Surge Tank Low Level Trip Switch Actuation.Const Workmen May Have Inadvertently Actuated Switch |
- on 760827,circulator 1B Tripped on Apparent Loss of Bearing Water.Caused by Dry Water Surge Tank Low Level Trip Switch Actuation.Const Workmen May Have Inadvertently Actuated Switch
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| 05000267/LER-1976-028, A:On 760920,reactor Bldg Sump Pump Started Automatically During rise-to-power Test.Caused by Operator/ Procedure Error.Step of Dual Purpose Surveillance Test Incorrectly Performed.Procedure Revised | A:On 760920,reactor Bldg Sump Pump Started Automatically During rise-to-power Test.Caused by Operator/ Procedure Error.Step of Dual Purpose Surveillance Test Incorrectly Performed.Procedure Revised | |
| 05000267/LER-1976-029, :on 761004,fire Pump Engine Showed Signs of Overheating During Surveillance Test.Caused by Shorted Solenoid Valve Coil.Valve Removed as Unnecessary |
- on 761004,fire Pump Engine Showed Signs of Overheating During Surveillance Test.Caused by Shorted Solenoid Valve Coil.Valve Removed as Unnecessary
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| 05000267/LER-1976-030, :on 761010,standby Generator 1B Engines Tripped Due to High Temps.Caused by Fouled HX Jackets.Hxs Cleaned |
- on 761010,standby Generator 1B Engines Tripped Due to High Temps.Caused by Fouled HX Jackets.Hxs Cleaned
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| 05000267/LER-1976-031, :on 761028,valve Failed to Close Automatically. Caused by Burned Coils on Valve Solenoids.Solenoids Replaced & Subsequently Burned Out.Investigation Underway |
- on 761028,valve Failed to Close Automatically. Caused by Burned Coils on Valve Solenoids.Solenoids Replaced & Subsequently Burned Out.Investigation Underway
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| 05000267/LER-1976-032, :on 761030,steam Outlet Block Valve Fuse Would Not Shut After Circulation Transferred to Water Drive.Caused by Stuck Solenoid Valves on Hydraulic Sys.Solenoids Changed on Eight Valves |
- on 761030,steam Outlet Block Valve Fuse Would Not Shut After Circulation Transferred to Water Drive.Caused by Stuck Solenoid Valves on Hydraulic Sys.Solenoids Changed on Eight Valves
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| 05000267/LER-1976-036, Forwards LER 76-036/03L-0 | Forwards LER 76-036/03L-0 | |