ML19241B437
| ML19241B437 | |
| Person / Time | |
|---|---|
| Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
| Issue date: | 07/12/1979 |
| From: | Sjogren R VERMONT YANKEE NUCLEAR POWER CORP. |
| To: | |
| Shared Package | |
| ML19241B435 | List: |
| References | |
| MOR-790630, NUDOCS 7907170152 | |
| Download: ML19241B437 (7) | |
Text
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VERMONT YANKEE NUCLEAR POWER STATION M'!'THLY STATISTICAL REPORT 79-06 s
FUR THE MONTH CF JUNE, ~979 7907170 /.'s bj (3 'i
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)
-o
s OPERATING DATA REPORT DOCKET NO. 50-271 DATE N 7
CONIPLETED BY * " 94caren TELEPHONE /^171 '66-9011 X2281 OPERATING ST ATUS
- 1. Unic Name:
Ver ent Yankee Notes
- 2. Reporting Period:
J me 1979
- 3. Licensed Thenaal Power I5IWt):
1593 540
- 4. Nameplate Rating (Gross 51we):
514 (open cycle) 504 ( closed cycle)
- 5. Design Electrical Rating (Net 31We):
- 6. 312ximum Dependable Capacity (Gross SIWE):
535 504
- 7. Sf aximum Dependable Capacity (Net SIWE):
S. If Changes Occur in Capacity Ratings (items Number 3 Throu;h 7) Since Last Report.Gise Reasons:
- 9. Power Lesel To Which Restricted. If Any (Net 5!We):
- 10. Reasons For Restrictions. If Any:
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This 51onth Yr..t o.Da t e Cumulative 720 4,343 59,378.75
- 11. Hours in Reporting Period
- 12. Number Of Hours Reactor Was Critical 720 3,935.3 47,825.1
- 13. Reactor Resene Shutdown Hours 0
0 0
- 14. Hours Generator On Line 720 3,921.8 46.054.8
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (51WH) 1.075 471 6.034.372.7 64.421,150.2 17 Gross Electrical Energy Generated 151WH) 352.110 2,039,422 21,378,890 IS. Net E:ectrical Energy Generated (31WH) l'O.nno 1.o44.524 20.7.,64,047
- 19. Unit Senice Factor 100 00.3 77.6
- 20. Unit Availability Factor 1n0 90.3 77.6
- 21. Unit Capacity Factor (Using 5fDC Net) 00.0 89.8 67.7
- 22. Unit Capacity Factor (Using DER Net) 90.4 88.3 67.7
- 23. Unit Forced Outage Rate 0
0 6.7
- 24. Shutdowns Scheduled Oser Next 6 Slonths (Type. Date.and Duration of Eachi:
Refueline Sootenber 22 - 6 week's
- 25. If Shut Down Ac End Of Report Period. Estimated Date of Startup:
- 26. Umts in Test Status IPrior to Commercial Operation):
Foreca3r Achiesed INITIA L CRITICA LITY INITIAL ELECTRICITY V
C05131ERCIAL CPERATION
. s b]
-)., f rus (9/77 )
AVERAGE DAILY UNIT POWER..EVEL DOCKET NO. 50-271 UNIT Ve r~jPln t Yankee DATE 7007'2 COstPLETED JY R. M.
Sioeren TELEPHONE (617) 366-9011 X 2281 l'U" 1979
.\\tONTH DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL
(.\\1he Net) 151We-Net) 501 473 37 2
274 13 489 3
352 19 493 4
412 492 20 470 492 3
488 480 6
485 0
7 23 467 490 3
3 9
..' 9 25 492 to 469 26 448 11 483
- 7 481 493 485
- 3 13 405
,9 488 14 49' 30 486 13-490 3[
io 435 INSTRUCTIONS On this f armat. 'ut the aserage da:i un:t power tese! in \\tWe Net for e::ah d23 :n the repornn2 :m. nth. Compute to the nearest sneie mepwatt.
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- x 50-271 UNITSilUIDOWNS AND POWER REDUCTIONS DOCKET NO.
UNI T N AssE Vernent fankee DATE 790712 June 1979 COMPl.El ED ltY R.
Pf. Slovren
.((
RI: PORT M ONTil T ELI PilONE (617) 366-9011 X2281 c _.
en 3m E
sM L.icensee 5 g, Cause & Corrective
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No.
Date g
gg g
jg$
Event MY p
Attion in
$E
.5 ;j, c Report it 8a' u go Psevent itecnrience H
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O o
79-8 790602 S
0 11 4
RAA CONROD
!! - Control Rod Pattern Exchange (Power Redne-tion) 79-9 790608 S
0 11 4
RAA CONROD 11 - Cont rol Rod Pattern Adjust ment (Power Reduc-tion) 79-10 790626 F
0 A
4 CBR VALVEX A
"A" Recirc Discharge Valve (V2-53A (Power was electrenically backser.ted to Reduc-stop valve leakage.
tlon) 1 2
3 4
l'. linied Iteason:
M eilniil:
1:xhita G. Instruainns S St heiluted A l'qnipniens Failure (Explain) 1 Mannal for Picparaiion of Data 11 Maintenance oi Test
- 7. Manual Scrain.
I'ntiy Sheets inr L.icensee C Ref orfing 3.Antomatic Su.un.
Eveni Itepne s (1.1 lt I l'de INtiltl.G-D Regulatiny Resisiction 4 Other (Explain) 0161) 1 -Opciato: l aining & l.itense Exainination i
i. Aihnine.t e ative 3
G ()per.itional I i sor (l.x pl.nai)
[x]idsii l - Same Sones e l'8/17) 11 Oihe 11:apl.ein)
1)OCKET f;0.
50-271 UNIT Vermont Yankee 10 DAlli 790712 en N
CO:!PLETED hY R. ft. Sj og re r.
TELEPil0NE (617) 366-9011. X2281
.'~2 v
SAFirlY !!E!All:D f t\\lNil:NANCil NA~l uf tli 01' Llilt 011 Ul!!'Al;L i!All UNC l l ON 1:QllII'l!!~.N f f IAI N'l l:NANC E NU!!!!ER CAUSL 1:LSUL1 Cull!!!:C' LIVE ACI luN Fuel pool and reactor Corrective NA Failed power Units tripped Replaced power supplies building vent radiation FIR 79-332 supplies monitors Containment air dilution Corrective NA Failed t ransmit ter No output Replaced transmitter pressure transmitter MR79-452 PT-VG-4A llPCI booster pump outboard Corrective NA Leak,ge Low oil level Added oil bearing MR79-454 IIPCI booster pump seal Corrective NA 1.oose fitting 1.eakage Tight ened f it t ing water MR/9-464 RCIC flow ludicator Corrective NA Partially drained False flow indi-Filled reference leg MR79-467 reference leg cations
DOCKET NO.
50-271 UNIT v
mnt n., t e e e
DATE 700712 CCMPLETED BY R. M. sineron TELEPHONE (A17T 367 o011 X2281 REPORT MONTH June 1979 SL" MARY OF OPEPMI.' G EXPERIENCES Highlichts Ve rnent Yankee operated at 93.87. of rated thermal power for the month of June, 1979. Gross electrical generation for the month was 332,110 MWHe, or 90.6% of design electrical capacity.
Operations Summary The following is a chronological description of plant operations including other pertinent items of interest for the month:
6-1 At the beginning of the report period, the plant was operating at 997. of rated thermal power.
6-2 At 0210 hours0.00243 days <br />0.0583 hours <br />3.472222e-4 weeks <br />7.9905e-5 months <br /> power was reduced to 317. to effect a control rod pattern exchange. Power increase to 97%
co =enced at 1113 hours0.0129 days <br />0.309 hours <br />0.00184 weeks <br />4.234965e-4 months <br />.
6-8 At 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> power was reduced to 68% to ef f ect a control rod pattern adjustment. Power increase to 98% commenced at 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br /> on 6-9.
6-26 At 0837 hours0.00969 days <br />0.233 hours <br />0.00138 weeks <br />3.184785e-4 months <br /> power was reduced to 67% to fa
.e a primary containment entry by plant personnel to
.it i f y and correct a source of primary coolant leakage.
Power increase to 98% co==enced at 1133 hours0.0131 days <br />0.315 hours <br />0.00187 weeks <br />4.311065e-4 months <br />.
6-30 At the conclusion of this report period, the plant was operating at 98% of rated thermal power.
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