ML19221A561

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List of Plant Operation Staff Functions According to Priority
ML19221A561
Person / Time
Site: Crane 
Issue date: 04/23/1979
From:
NRC COMMISSION (OCM)
To:
References
OLP-790423, NUDOCS 7905230195
Download: ML19221A561 (5)


Text

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/v PLANT OPERATION STAFF

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  • g, g '4,u,.e Task Description Priority Status /Due Date Task Coord Obtain RCS pressurized Schedule next Thorpe /Hetrick sa=ples. Review sample 1

sample--CS00 Shift Surarvisior frequency (Broughton) 4-25.

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Pressurizer Heise and Recalibrating Wilson /Broughton D ff. press [ ~t dead-1 LT-2 failed.

Ignt tester.

,X Reductfon k RCS temp.

Logan to 175 -- Limit speed of turbine to 500 rpa.

,A[

Boron concentration in 0700 4]Q; sample.

3rcughton RCS calculation Sample was 2937 Shift Super.

35cc/kg gas.

f Obtain SEC approval and (Tie in approval only.)

Need ECM'S h Porter / Faulkner 36, 37R1, 52, 56, Seelinger M, 9 2, M, M$,

109, 127,,13T, 132, b

[

SSRW pump repairs 1

A.

In service Miller /Shovlin B. Asser.ble 4/24 //,,co C. Disassc=bling the C. punp.

K Set up 350 CE! air Cc=p-3achoffer/ Thorp f

ressor for use by W in 2,

decontamination of D. C.

building.

L'se Eberline to monitor Bru==er trend. Plot every 10 mins.

[

Make calculation of RAD.

Ccbeap/Gunn levels that will occur in cond. Demins - if we circulate and clean 3 OTSC.

/

J0.

Layout STE office for use Porter.

as Aux. Inst. location for Incore temps. etc. -

Provide Milestone Schedule.

164 262 Make sketch of WGDT Miller /Floyd and Mcnitor tank level vs time.

7005230 64 C

-.r Task bescriotion Priority

' Status /Due Date Task Coord.

[

Prepare instructions for Herbein/Morck/Kunder loss of gland stea:2 to turbine.

1 Determine Hotwell radla-Hetrick tion levels twice a day.

[

Look at using generic 4/23/79 Thorp / Miller R'JPs to cover heavy traf fic or department.

f L5.

Se prepared to run Toole Existing 3 Decay Heat Pump on recire - Wednesday 4-25 Have Schedule 6 pc today (Include megger of mo tor).

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Hydro FW heater to determine pM,h i

T le if it leaks - we need surge tank for "B" OTSG long ters b #,y ccoling system.

f M

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A. Sample "B: OTSG for total y Hopkins B. Sample Cond Pump discharge.

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p l* M,A-activity.-

AN Match every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to VAC I

.p b

C. B Main Steam stop on B side. @ g gp pump exhaust.

4 /

y pgo I@

Seeinger Operations check Turbine Su=p, gpk Cond Pol Sunp & Waste 'ent

. /A MM yy#

tank sump to see if the y go to Ras waste.

, (,9 & 'U Verify heaters cperational on Vac)* jO Shoviin/Teole gha %DWi Pump exhaust.

f Take gas sample on HPR - 221 A53.

Miller p

Do we have extra sample pumps.

,d u/4t) /0 g h 4Lf for HP-R-222 5228?

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164 263

PLANT MODIFICATIONS Task.

_pescrintion Priority Status /Date Due Task Coord.

.WF

.Decon water in AB using 1

Relay inst. process, Cobean Epicorion exchange pro-ventilation, fire svc, cess. Targer operation, Demin water, serv. air 5-11.

power-Need ECM 36&96.

/

TS-Develop complete package 1

Equip. avail. 4/21 Wilson /

for logn-term cooling of Instal. comp. 5/7 Cobean OTSG "B". Use Unit #2 7

g Demins, for long ters

,/

system.

/

TS 4 Develop comp 1ne package 1

Heise gauges instal.

DeVine/

for measuring water level 4/12. Do not open Cobean/

inside reactor building.

DH-V6B, until approved.

Herbein TJritf' Install 2/2500 kw diesel 1

Equip. avail. 4/10 Cobean/

/

generators - check ship-Instal. comp. 4/20 Gunn/

ping damage - vendor. Run Toole diesel, fill fuel system.

Jfd Develop electrical distri-1 Equip. avail. 4/10 Cobean bution system. Install Instal. ccep. 4/20 cabling and switchgear from DG's to current BOP loads requiring loss of off-site power protection.

[WG-Install storage vessels in 1

MEC relocate their Cobean/

Fuel Pool " A" equipment.

Gunn Tc RC loop passive pressure 1

ECM cceplete Gunn control sys te:2.

Instal. comp. 5/2.

Irstall AB/FHB Filter 2

Relay power fire sve.

Gunn/ Thorp system. MEC install high process inst. Do base 3achoffer noise level signs.

line noise survey 4/23.

Tc Install and coepicte turn-2 ECM-S-069 Cunn over package of electrical heaters in supply side of Aux. Building. Existing Filter.

f Shield for decay heat pu p.

1 Installation to be

'iilson scheduled by 4-30 y

Resolve procedures that require Gunn/ Thorp evacuating FB prior to sampling 3g

!s inghouse CH removal system by Westinghouse.

IU p 16 Provide cap for lux. Building Gunn stack.

.c PLAST MODIFICATIONS task

' Description Priority Status /Date Due Task Coord.

Open two h' oles for R3 B&R/Cobean purge to be used for AB air cleaning.

Relocate #1 access to FH Cunn/ Rice building on Unit #2.

B&R put together set of Have by 4/24 Toole/B&R small flow prints.

WASTE EU AGEMENT CROUP G-5 Set-up to change AB/FH 1

Cut in A Aux.

Shovlin/

building vent. filters.

Bldg. Filter Bachoffer Changing out FHB filter-on 4-23 "A" & Aux. Building. filter "B'.' Map ou t change sequence.

L-33 Develop plan for tying tank farm to Epicor "2".

1 In progress Snyder Develop Health Physics Seelinger Plan to cover waste agmt.

Begin Maste Gas Program to Seelinger determine location of leak.

Develop plea for canage=ent Seelinger of decont<aination of radioactivity in Aux. &

Cont. Bldgs. - 4/23 Cet Bldg Sample thru Air Lock Miller Check possibility of det-Levy /

ermining containment semp Industrial level by measuring radiation Ads iso ry at centainment wall.

Group TECHNICAL SUPPORT LS-2 Tech. Spec. Daletions, 1

Issue 5-01-79 Harding f

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Changes, and additions of Long-Term Cooling.

TM 32 Review with B&R work'on 7

DHR system codification 1

Issue 4-18-79 Capodanno

~M53'5 Establish long-term plc.at 1

Is sue 4-18-79 Chisholm

,/

Instrumentastor, game plan.

tobe revised Develop Cuidance en Natural need date.

Circulation procedure to be out 4/21 Broughton/ Tech Tech Group-Wilsen

TASK _

SCHED/

CCNST.

CCC.

TEST NO.

TITT.E COOPS.

_E';G_R.

_E_:._:G_R.

CO NT?A_CT_C R CCM". EST

'iG 1 A3 Filter tirif M. Schuber: McMullin UESS He'aold s -

TS 3 SG 3 Rose J. Paparelli ?oje Long ter Freulx T. Jordon Catalytic coeling f

'JG 6 Storage

?nusi J. Tochy McMullin CI55 tank "3" D. Payne pools

'?ater recen V. Fricke Gatto Ca:alytic

'iG 2 systen Uilkira D. Lilly (CAPGO)

Fre drik TS 6 Fressure Shippert Fapaiya Poje Centrol Ray D. Lilly TS 10 Diesels Canale Gen:cle:

Kakarla Catalytic

& 11 McCabe Meniyar TS 13 Heater in Ccnale M. Schuber:

McMullin Catalytic A-3 filter McCabe Shield for'Iright de c ay-h e a t pump pi:s :Te ll=ol d

T/A Catalytic 164 266 g

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