05000338/LER-1979-143-01, /01T-0:on 791109,fuel Vendor Identified Potential Problem Affecting Temp of Large Break LOCA-ECCS Evaluation Model.Caused by Erroneous Fuel Burst Calculations.Study in Progress for Peak Clad Temp

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/01T-0:on 791109,fuel Vendor Identified Potential Problem Affecting Temp of Large Break LOCA-ECCS Evaluation Model.Caused by Erroneous Fuel Burst Calculations.Study in Progress for Peak Clad Temp
ML19210D687
Person / Time
Site: North Anna Dominion icon.png
Issue date: 11/21/1979
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210D670 List:
References
LER-79-143-01T, LER-79-143-1T, NUDOCS 7911270451
Download: ML19210D687 (2)


LER-1979-143, /01T-0:on 791109,fuel Vendor Identified Potential Problem Affecting Temp of Large Break LOCA-ECCS Evaluation Model.Caused by Erroneous Fuel Burst Calculations.Study in Progress for Peak Clad Temp
Event date:
Report date:
3381979143R01 - NRC Website

text

NRC FORM 366 (7 77)

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8 60 63 DOCKET NUMBER 68 63 EVENT D ATE 74 75 REPORT DATE tIO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l VePeo was notified by the fuel vendor th.-t a potenti31 noncnnsoruntion fn 2 t., rg g o

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JJ 34 35 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l The problem is related to fuel burst calculations and the use of notentin11y nnnennenrJ i

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Virginia Electric and Power Company North Anna Power Station, Unit 1 Attachment: Page 1 of 1 Docket No. 50-338 Report No. LER/R0 79-143/01T-0 Description of the Event The fuel vendor notified Vepco on November 9,1979 that a potential nonconser-vative feature of its large break LOCA-ECCS evaluation model existed. This event is reportable pursuant to T.S. 6.9.1.8.h.

Probable Conseque~nces of the ' Event This problem could affect the peak clad temperature calculated for the large break LOCA transient. The F(Q) limit may be affected.

The health and safety of the general public were not affected by this event.

Cause

This new discovery resulted from work performed subsequent to meetings held with the NRC on November 1 and 2,1979 concerning studies made by Oak Ridge National Laboratory.

The fuel vendor determined that a nonconservative fea-ture could exist in the large break LOCA-ECCS analysis with respect to the portion of the calculation related to fuel rod burst.

The existing fuel rod burst model used clad heatup rates of 25 F per second or greater.

Actually, clad heatup rates could be less than the existing model.

A shift in clad burst time can affect the peak clad temperature calculated for the LOCA transi-ent.

Immediate Corrective Action

Discussions were held with the fuel vendor with respect to reanalysis of the LOCA transient to formulate scheduled corrective actions.

Scheduled Corrective Action It is anticipated that the required analysis will be completed in December 1979 and the F (Q) limit modified, if required.

Actions Taken to Prevent Recscrence Not applicable to this event.

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