ML19210C386

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Monthly Operating Rept for Oct 1979
ML19210C386
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 11/01/1979
From: Bair G
PORTLAND GENERAL ELECTRIC CO.
To:
Shared Package
ML19210C384 List:
References
NUDOCS 7911140167
Download: ML19210C386 (4)


Text

.

- OPERATING DATA REPORT DOCKET NO.

50-344 DATE 11-1-79 COMPLETED BY G. G.Bair TELEPHONE 501/ 556-3713 Ext. 234 OPERATING STATUS Notes

1. Unit Name:

Troian Nuclear Plant October 1979

. 2. Reporting Period:

. 3. Licensed Thermal Power (31Wt):

3411 1216

-4. Nameplate Rating (Gross 5tWe):

1130

' d. Design Electrical Rating (Net 31We):

6. Maximum Dependable Capscity (Gross SIWE): 1122

_3 1080

7. Mmmum Dependable Capacity (Net SIWE):

"8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) SinceT.ast Report. Give Reasons:

9. Power Level To which Restricted !f Any (Net MWe):
10. Reasons For Restrictions.If Any:

a This Month Yr.-te Dat:

Camuistive

11. Hours In Reporting Period 745 (time chance) 7296 28374
12. Number Of Hours R-setor Was Critical 275.1 5161.6 16284
13. Reactor Reserve Shutdown Hours 0

8.9 2171.8

14. Hours Generator On-Line 274.2 5083.8 15624.2
15. Unit Reserve Shutdown Hours 0

0.5 1508.7 660489 16948729 48887948

16. Gross Thermsi Energy Genersted (31WH)
17. Gross Electrical Energy Genersted (MWH) 279880 5533.225 15983995 264093 5278784
19. Unit Service Fsetor 3o.8 15045383
18. Net Electrical Energy Generated (5tWH) 60.7 55.1
20. Unit Availability Factor 36.8 69.-7 60.4
71. Unit Capscity Fsetor (Using alDC Net) 32.8 67.0 50.2

' 22. Unit Capacity Factor (Using DER Net) 31.4 64.0 46.9

23. Unit Forced Outsge Rare 1.2 2.02 30.7
24. Shutdowns Scheduled Over Next 6 Months (Type.Dste.snd Duration of Eacht:

Refueling, April 1980, 90 davs 7c0 p

i

.25. If Shut Down At End Of Report Period. Estimated Date of Stsrtup:

November 1970

26. Units In Test Status aPrior to Commereis! Operation):

Forecast Achieved INITIA L CRITICALITY M

'1A INITIAL E'.ECTRICITY NA NA COMMER'.'!AL OPERATION NA NA

-p 7911140[

/

f/77)

APPENDIX B AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-344 UNIT Troian DATE 11-1-79 COMPLETED BY G. G. Bair 9

TELEPHONE 556-3713 Ext. 234 MONTH October 1979 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 1061 17

-12 2

652 18

-10 3

451 gg

-9 928

-3 4

20 1064

-3

~

5 21 6

1069 22

-3 1066

-3 7

23 8

1069

-3 24 9

10r>6 3

-3 10 1066

-3 26 1070 11 27

-3 12 559 2a

-3 13

-13 29

-4 14

-4 30

-5

-10 15 33

-6 16

-11

~ 'O 179 INSTRUCTIONS On this form, list the average daily unit power level in MWe-Net for each day in the re;3orting month. Compute to the nearest whole megawatt.

These figures wdl be used to plot a graph for each reporting inonth. Note that when nuxnnum dependab: capacity is

~

tised for the net electneal ral.ng of il.e imit, there nuy be occauons when the daily average ; ower lesel exceeds the 10(r.1 hne (or the restrhted power level kne). In unh cases, the average daily umt power output sheet should be footnoted to expl.nu the app.nen t.monuly.

1.16-8

UNITSitUTDOWNS AND POWER IG.UUCTIONS DOCKET NO. 50-144 UNIT NAh1E Troi,n DATE 11-1-79 REI' ORT h10NTil Octo:er 1979 C05fPl.E1Ep ilY

('-

t' oir TELEPilONE ssA 1711 Ext. 234 "t_

,! E 3

Licensee Eg h.

Cause & C.nrective N. i.

Daic g

3g ij js5 Event uy e-1 Action to 3 =.

5 jdg

. Report a

@u gu I-Prevent Recurrence

. t$

79-12 791002 F

3.2 G

3 NA NA NA Steam Line A HSIV closed accidentally

~

when wortiman disturbed an air line to the control solenoid valve.

The reactor tripped on Lo-Lo level in A Sbeam Generator.

-~

79-13 791012 S

467.8 A, D 1

NA-NA.

NA Scheduled outtage ' occurred to, pern it NRC required inspection of hangers and restraints inside the containment and to plug small steam generator tube-leaks in the A and' D Steam Generators.

I 2

3 4-F: Finced Reason:

Elethod:

Exhible G. Instnicilons S: Scheduled A Equipment Failure (Explain) l-blanual for Preparation of Data 11-blaintenance or Test 2 blanual Scrarn.

Entry Sheets for Licensee i

C. Refueling

3. Automatic Scram.

Event Repori(LER) File (NUREG.

~

D Itci:ulasory Restricilon 4-Other (Explain) 0161)

O E-Operator Training & Ucense Examination F-Athninisitative 5

G Operational Error (Explain)

E.shibil 1 S.ne Source (9/77) 03 Il Other (Expla!n)

C

DATE:

11-1-79 COMPELTED BY:

G. G. Bair

' ' 5 TELEPHONE:

503/556-371 Ext. 234

SUMMARY

OF OPERATING EXPERIENCE OPERATION:

The plant began the month at full power, sustained one inadvertent trip on 10-2-79, and shutdown on 10-12-79 to plug small leaks in the 1. and D steam generators amounting to 125 gallons per day and to inspect seismic hangers and restraints inside the containments.

A positive displacement charging pump packing leak was discovered and repaired that had been responsible for periodic increases in Auxiliary Building airborne activity levels.

Temporary backup RCS cooling hoses were placed in the field pending resolution of the seismic integrity of hanger support under block walls.

MAJOR SAFETY-RELATED MAINTENANCE:

Work continued on improvement modifications to the Plant Security and Fire Protection Systems.

Work continues on the program of upgrading pipe hanger and restraints for seismic loading.

An inspection was conducted on the seismic hangers and restraints inside the containment.

Some repairs were made as defects were found.

Work was completed en repairing hanger SA-83 to correct its seismic interface with a cinder block wall in the RHR pump room area.

Work was completed on cteam generators A and D eddy current testing. Work began on steam generator tube plugging operation.

Work continued on a program to investigate stress corrosion cracking on stagnant water lines.

Completed the periodic overhaul of the electric tire pump.

Discovered and repaired a small surface crack found on the suction line pipe elbow of the south safety injection pump.

LICENSE CHANGES:

None.

MISCELLANEOUS:

During the steam generator eddy current testing, some contractor personnel were involved in radiological control incidents.

One person received a dose of 2.9R which is near the quarterly dose limit of 3R.

A few persons received some exposure without proper dosimetry.

These circumstances are now under reviet An investigation began on the seismic integrity of some cinder block walls to which seismic hangers are attached.

'"O 181