ML19210A806
| ML19210A806 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 03/01/1977 |
| From: | Lawyer L METROPOLITAN EDISON CO. |
| To: | |
| Shared Package | |
| ML19210A771 | List: |
| References | |
| NUDOCS 7910310693 | |
| Download: ML19210A806 (3) | |
Text
'
DOCKET NO.
50-289
~
E #1 UNIT
?' arch 1,1977 DATE COMPLETED BY L. L. Lav er 929-3601 Ext. 111 TEL. NO.
DAILY PLANT POWER OUTPUT MONTII Februar/
DAY AVERAGE DAILY MWe-net DAY AVERAGE DAILY MWe-net 1
790 21 804 2
792 801 22 3
793 798 23 h
790 2h 797 5
365 791 25 6
753 26 793 7
792 791 27 8
801 28 796 9
798 29 10 797 30 11 796 31 12 796 13 793 1h 796 796 15 16 799 7
1539 008 18 795 798 19 20 800 gerest o 613
SUFNAltY :
UNIT SHtffD(MNS ANI; POTER REIAICTIONS 50-289 DOCKET NO.
The tuilt operated at 10(% F power from 0001, 2/1/77 until 2300 2/4/77 when the unit wa: shutdown due to a nulfunction of the UNIT DAME N#I Turbine overspeed oil trip test tubing. The turbine was off-line for 7.2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> but the reactor remained erltical. The unit returned DATE March 1,1977 to 100% Power on 2/6/77 at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> amd reunined at essentially full I'* I'-
I'"WY " P power for the renninder of the mnth.
CU4PLETED BY TEL. NO O N REPORT MONTil Feb ruary METH G) 0F TYPE SHirl"f!NG DOWN F-FORCED OUHATI(N THE ItEACT(H Qt NO.
DATE S-SCHEltJIED (HOURS)
REASON (1)
REDUCING P(MER (2)
COMMEN'lil L
2/5/T(
S 72 A
1 Mal function of Turbine Overspeed Oil Trip Testing Tubing O
s W
(1) REASai:
(2) ME'niOD:
Cf3 A-EQUIINENT FAIIURE (EXPIAIN) 1-MANUAL g
B-MAINT. OR TEST 2-MANUAL SCRAM C-REFUELING 3-AlfrQ4ATIC SCRAM INItEGUIATOHY BMITHICTION h-orHER (EXPIAIN)
C E-OPERATOH THAINING AND C
LICENSE EXAMINATION W
F-ADf4INSTRATIVE G-OPEHATIUlAL EHROH (EXPLAIN) i H-urHErt (ExPIAIN) i i
i
CPERATI'iG DATA REPORT e
e-a-'Y DOCKE* 30.
-t e*
UNIT *iA"E DATE March 1, 197~
b*
- L'U ' #
C09LETED BY
- 0. 929-36C1 l.
REPCRT!'i", PEPICD: OCC1,77C201
- 3Ra;03 2kCO.*70223 GRCSS HCURS IN REPT*ING PERICD
672 2.
CUPEENTLY A: THCPl?.ID PCVER CVEL M'4t 2525 MAX. DEPENT. CAPACI"T(We-Net )
'?
Design Electrical Rating (We-net) cly 3.
PCWER LEVEL TC VHI~H RES*RIC"ED (!F ANY):
d.
FIASCNS FCR RES*PICTI TS ( IF A'iY):
d t
i 6
i i
i THIS CUMU!aT!'IE
}
MCU*H YR-TC A*I
- 0 CA'"E 1,
i 5.
NUMBER CF HCUPS RLC*CR WAS CR!*ICAL 6I2 lbl6 17267.3 6.
REACTCR RESERVE SHUTDC'a"N HCURS O
C c4e e 7.
HCURS GENERATCR Ci-LINE.......... 66k.S lkCS.S 16,917.2 l
3.
UNIT RESERVE SHUTDCVN HCUPS........ C 0
C i
i 9 GECSS "HEPXAL ENERGY GENERA *D (153).. 1,653,L92 ?,5?2,?70 al.2co,2a=
l.
10.
ORCSS E'20*PlCAL ENIRGY GENERA"'ED (L'H).. 555,557 1,l"a,'63 l?,3*?,155
.l.
NE* ELE ~!R! CAL EiERGY GENERA 0ED (53)... 52?,367 1,115.378 12.C'0 333 t
l 12.
REAC*CR SERVICE FAC*CR 100.0 100.0 70.0 13.
REAC"CR AVAILABILITY FACTOR.
100.0 100.0 21.6 la. UNIT SERVICE FAC"CR..........
95.G 99.5
? "*.*
- 15. UNIT AVAI'A3 LITY FAC*CR 08.0, 49.5
~?.a L6.
'.7IIT CAPACIIT FACTT (USING :CC) 98.3 90.5 Th.9 17-Unit Capacity Fact:r(Using Des ign We net) 95.1 9o.2 72.a 15.
FCR SD Ct." ACE Pa*E 0.0 0.0 6.0 19 SH'J*00WNS ST.:.0UIED TO BEGIN IN NEXT 6 MC*iTHS (STA'"E TYPE, LA*E AND DURA *!CN
^7 EACH): - Ref eling - March 19, 1977 - 6 weeks 20
"a 21 "N!"S IN "'E:'T STA!"3 (PRIT TC CCE'ERC!AL CPEP.A*ICN) : ;i2T APPLICABLE
)rol, P10 jo Ji