ML19210A804

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Monthly Operating Rept for Dec 1976
ML19210A804
Person / Time
Site: Crane Constellation icon.png
Issue date: 01/03/1977
From: Lawyer L
METROPOLITAN EDISON CO.
To:
Shared Package
ML19210A775 List:
References
NUDOCS 7910310691
Download: ML19210A804 (3)


Text

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AVERAGE DAILY UNIT PCWER LDIEL DOCKET NO.

50-289 UNIT TIC #1 DATE Janua:7 3,1977 COMPIETED BY L. L. Lawyer TEL. NO. 215-929-3601, Ext. 111 MGTI'H Decenter DAY AVERAGE DAILY POWER LEVEL (We-Net)

DAY AVERAGE DAILY PCWER LEVEL (We-!Tet) 1

-16 21 80h 2

-20 22 807 3

-38 23 805 4

312 2h 807 _.

5 753 25 803 6

799 26 80h 7

797 27 803 8

806 28 803 9

805 29 801 10 805 30 799 11 802 31 797 12 805 13 802 1h 806 806 15 16 805 17 803 g< 18 803 806 19 W91031ob7[ Sch 20

CPERA*!NG OATA PEPCRT ECCKET No. 50-239 L'ET NAv2 "C el CATE .anuary 3, 1977 C0&!2"'ED EY L. L. lavfer '"I'. NO. 215 327-3601, Ext. .1_ o"', ' ' A, 2 ^ "' h C C ' 6 ~3 7 '- 1. FIF TTING PEPlCO: THRO 1GH GRCSS HCL?S IN RETTIN3 FEPlO: TLA 2. CURPINTLY AU"HCRI'E0 PCVER TiEL Wt 2535 MAX. EEPEND. CAPACI r(Mwe-Net) 792 3. PCWER LEVEL TO WHICH RES"IC'E2 (!F AIt): N:ne 4 REASCNS FCR 2ISTRICTI WS ( IF ANY): NA i i f "'HIS CUMUIA TIE MO. "H YR-TG-CATE "'O OA"'E 5. NUMEER CF HCURS REACOR WAS CRITICAI, 676.5 5839.2 15351.3 6. REACTCR RESERVE SHL*rDCWN HOUPS 67.5 6C3.5 6C3.5 7. HOUPS GENERATm 3-IlNE.......... 661.3 57k7.5 15506.'. 8. UNIT FISERVE SHLMN HCURS........ 0 0 0 9 GRCSS 1.'EPMAL ENERGY CINERA E (!Ed).. 16615LO 13926275 37757S75 10. GROSS EI2CPlCAL ENDGY GENERA"'ID (%d). 553G37 k6k2??? 12672737 11. NET ELEC"RICAL ENEROY GENERAGED (5 4).. 525055 L33c62c 1105a960 12. PIAC"0R SERVIG FA~!CR G0.95 66.c5 77.55 13. REAC"'CR AVAILA3!LITY FACTCR........ 100.0" ??.k5 30.55 Ik. UNIT SERVICE FACICR...... 39.05 65.kT 75.3% 15. UNIT AVAI* ABILITY FA C CR 30.05 65.k! 75.35 '3.25 16. U' LIT CAPACITY FAC"'T (USING M;C) 39.15 62.35, 17. FOECED CU~ AGE P.A*E 0.05 0.?T 6.55 IS. SH'J"O(NNS SCHECUII: TO BEGIN IN NEI* 6 MON 55 (STATE "YPE, OA~E AYD OL?A*!CN OF EACH): Re heling - Mare: 19,1977 - 6 weeks 19. IF 2H';"0C'a7! AT END CF PIPCRT PERICD, ESTIMATC CA2 5 CTAR"'lP: 3A -n r.~.w,.,,,. sN m -.a.,.J r t'o.a, N s w -rwe.e.r.,E.

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9 5 SUl44ARY : UNIT StilfPD(MNS AND PCMEH REDUCTIONS The unit, was shutdown at 2300 on 11/5/76 to repair Dil-V-1 and work on condenser, however, problems with the Nuclear Services Couting Hiver Water System kept, the DOCKET NO. 50-269 outage continuing into December. The reactor was taken crit.ical on 12/3/76 at 1930 houru and the generator went un line 12/h/(6 at 1130 hours. Power escalation UNIT NAME 3 #1 tovk place until 12/5/76 at 1950 hours when the plant reached 100% full power. The DATE gnun ry 'i, 19ff plant nutintained essentially 100". FP for the remainder of Decernber. CG4PIJ:TED BY L. L. Lawyer REPORT MONTH Dect '>e r. ] 976 TEL. NO. 2lS-929-4601, Ext. I11 METl!G) OF TYPE Sillfl"fING DOWN F-FOltCED DUHATIO4 Tile HEACTQt Qt NO. DATE S-GCIIEIO LED (HOURS) HEASON (1) BEIUCING P(.MER (2) COMMENTS 8 L1/5/76 G 82.2 B 1 ,Shutduwn to repair Dil-V-1 and work on condenser (continuation). O (1) REAS m: (2) ME'1110D: A-EQUIINENT FAIIJJHE (EXPIAIN) 1-MANUAL lU B-MAINT. Oft TEST 2-MANilAL SCHAM (j ) C-ItEFUELI NG 3-AUTG. TIC SCHAM g IAREGUIATOHY HESTRICTION 0-UI'llElt (EXPIAIN) E-OPEHATOR TRAINING AND LICENSE EXAMINATI(fl F-AI*flNSTitATIVE I-) G-OPEftATI(flAL FRitolt (EXPIAIN) O H-UI'IfEH (EXPIAIN) l I I 4}}