LER-1979-085, /03L-0 on 790715:following Power Reduction Caused by Secondary Plant Problems,Quadrant Power Tilt Alarm Was Observed.Possibly Caused by Dropped Rodlets.Tilts Under Review |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3381979085R03 - NRC Website |
|
text
.
... ~
(?-7h LICENSEE EVENT REPORT CONTROLetoCK: l l
l l
l l
l@
(PLEASE PRINT OR TYPE ALL REQUIRED INFOHMATION) 1 @] 0 l 0 -l 0 l 0 0
0 0 - 0l0l@l d 1l 11 1!
1 h l
l@
[oTil v Al sl P S
i a i uwa t com i4 u,
uu m a ra m H a
ua m m u be w u CON'T d L]
]{
Ll@l 0l 5 l 0 l 0 l 0 l 3 l 3 l 8 l@l Q 1 1l 1 % o'@] gl 2!0 l 7] ol@
EVENT DESCR PTION A DPROBA LEC JENCES [o p j l On 7/15/79 at about 0548 fol'owing a power reduct ion canSmLhy socondary Plant I
o 3
l problems, a quadrant power tilt alarm was observed.
Subsecuent t il t calculations l
o 4
l were perforced utilizing Excore detector currents which indicated that the tJ1t I
o s l reached a maximum of 1.056 at 0652 and decreased below the 1.02 linit of T.S.
3.2.4 l
[o Gj l at C920.
This event is reportable pursuant to T.S. 6.9.1.9.b.
The health and I
l safety of the general public were net affected.
I o
i o
s l I
80 1
P, 9
SYSTEM
CAusE
CAUsE C oY P.
VALVE CODE CODE SU3 ODE COYPONENT CODE EU0COCE SUBCODE i RI c @ I xl@ I x [@ l z zl zl zi zi zl@ g@ W @
o o
i 8
9 10 11 11 13 14 13 20 SEQUEN TI AL OCCU M P s '.C E REFORT R E VI5 ION
_f t E '. T Y E A R FiE POR T NO.
CODE TYPE NO b[Lf4;$.gT l 7l 9]
l ___ l l 0l 8l 5l l/]
[0 l3 l
%l l-l [0
40 1
'6 21 24
- )
JJ 31 31
_ 21
- ' l 23 24
/
AC T ION FUTUHF EFFECT SHUTC LN A TT AC H Y E N T
" PRO-4 PH1YE covP.
CO.YPON E N T TAKEN ACTION UN P L A'. T
~ ~i TH OD HOUHS SU'3VI TT E D F ORY dud.
SUPPLI E R M ANU r AC'r U H L H L >i@l >l@
l P1@
l l@
01 01 01 01 I Ylg l Nlg
[ Nl@
l Wl 1l 2l 0lQ
.U 11 35 36 3/
49 41 42 43 44 47 CAUSE DESCRIPTION AND CORREC TIVE ACTIONS h i
o l This event was preceded by two similar events reported in LER/R0 79-076/03L-0 and l
i i
l LER/R0 79-079/03L-0. This problem is currently being investigated bv both Venco I
- , ; q [ and Westinghouse.
Core flux napping surveillance has been increased, however suf ficient inforcation has not been obtained to deter-ine the exac t cause.
1 j,;]l i
a l
l 1
E u 80 F ACil 11Y YETHOD OF STATUS
. PO't.E H OTHER S T A TU3 DISCOVi HY DISCOVEHY DESCHIPTION l ElQ l Oj 5l 3lgl NA l Algl Operator Observation i
1 8 1 13 17 13 44 45 dii 80 AC i t V I T Y C:3N TENT HE LF AMD OF HE LE ASE AYOUNT OF AC TIVITY LOC A TION OT RELE ASE '
l NA l
j ' NA l
1 6
1 8 9 10 11 44 45 80 PE H50%E L f xPOSUHES N U?.ht E H TYPE DE SCHtP TION 31 1010lOj@lZl@l N.
l i
i 1
H 9 11 12 13 80 Pt HS9%E L INJURIES PH P? EH DTLCHP TION
/
8 9 11 12 80
{000h0f 7 g
Sc p 1
I ' l o l LzJ@l o
gg
(
80
/
U 9 i%.((81" $E CHmrmh 0 '-
NRc ust: ONLY L"
i Illilililllll!
/ o I
a 9 to tM 69 80 5 NAME OF PRE PARER 17 Y
N e t,-ip t psoNE-tm] M / t i t t,
Virginia Electric and Power Company
Attachment:
Page 1 of 2 North Anna power Station, Unit #1 Docket No.: 50-338 Report No.: LER 79-035/03L-0 Description cf Event :
On 7/15/79 at approximately 0548 during a Power Escalation following mainte-nance on a secondary plant feedwater pump and main condenser, the alarn on core tilt deviation was observed.
Seven periodic tests which evaluate the tilt utilizing excore detector currents were perforced.
The tilt peaked in the upper half of the core with a tilt ratio of 1.0561 at 0652 and the ala.m cleared when the tilt ratio decreased to 1.0178 at 0920.
The action statements of T.S. 3.2.4 were followed until the tilt reduced belcw the 1.02 limit.
Probable Consequences of Occurrence The limit of T.S.
1.02 provides for DNB and linear heat generation rate pro-tection of X-Y plane power tilts. A period of two hours of operation between 1.02 and 1.09 is allowed by Technical Specifications to allow for problen analysis and correction.
A power reduction from 100% is necessary to reinstate the nargin of uncertainty for FQ.
Since the reactor was at reduced power during this event, the health and safety of the general public were not affected.
Cause of Concurrence An evaluation of potential causes of the tilt condition has been performed.
P~eliminary results from the evaluation ruled out control rod misalignment, L :rnable poison rod failure, 1-Salance of loop thermal power, fuel enrichment variations, and calculational errors as being the cause of the tilt condition.
The possibility of dropped RCCA rodlets has not been ruled out.
Therefore, a detailed safety evaluation to assess continued operation with a few dropped RCCA rodlets was performed.
The results of this safety evaluation conclude that there will be no adverse impact on safety fron continued operation with the current Technical Specifications limit.
Specifically, shutdown nargin is adequate, achievable power distribution during the remainder of NA1, Cycle 1 operation is bounded by the power distribution assumed in the FSAR, and the presence of dropped RCCA rodlets will not result in an inoperable control rod.
These results have been discussed with the NRC Division of Nuclear Reactor Regulation.
Inmediate Corrective Action Af ter the presence of the tilt was noted, the actions required by T.S.
3.2.4 were followed.
Since the power level was approximately 50% no further power reduction was required to restore the margin of safe ty for F.Q. and since the duration of the tilt condition was less than 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, no Power Rangu neutron flux-high trip setpoint reduction was required.
g n f)
- - oO b
[
i
Attachment:
Page 2 of 2 Scheduled Corrective Action To continue to perforn more frequent flux napping (i.e., bi-weekly whenever core conditions pernit) as well as acquire and analyze relevant data obtained during ona-,tions which result in an increased tilt.
To conduct a visual exaninatic -
the core to determine the condition of the control rods.
Actions Taken To Prevent Recurrence No specific actions have been outlined.
However, the tilts are being reviewed on a case-by-case basis in an attempt to prescribe an operating technique which would reduce the nagnitude and frequency of tilt occurrences.
As a result of more detailed evaluation and core inspection, additional actions may be taken.
M S
/
/
k u
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000338/LER-1979-001-01, /01T-0 on 790115:non-conservatism Identified in Calculations Performed in Monitoring Axial Power Distribution Fj(Z).Caused by Omission of Sys & Procedures Used to Monitor Fj(Z) | /01T-0 on 790115:non-conservatism Identified in Calculations Performed in Monitoring Axial Power Distribution Fj(Z).Caused by Omission of Sys & Procedures Used to Monitor Fj(Z) | | | 05000338/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000338/LER-1979-002, Forwards LER 79-002/03L-0 & 79-003/03L-0 | Forwards LER 79-002/03L-0 & 79-003/03L-0 | | | 05000338/LER-1979-002-03, /03L-0 on 790101:during Normal Operation,Pump 1-RM-P-159A Tripped on Overload.Containment Particulate Sample Flow Was Lost,Rendering Inoperable 1 Reactor Coolant Leak Detection Sys,Due to Deficient Federal 1206LLT Bearing | /03L-0 on 790101:during Normal Operation,Pump 1-RM-P-159A Tripped on Overload.Containment Particulate Sample Flow Was Lost,Rendering Inoperable 1 Reactor Coolant Leak Detection Sys,Due to Deficient Federal 1206LLT Bearing | | | 05000338/LER-1979-003-03, /03L-0 on 790102:during Periodic Test,Noted That Containment Isolation Valve TV-SV-102-1 Would Not Shut Fully.Cause Undetermined | /03L-0 on 790102:during Periodic Test,Noted That Containment Isolation Valve TV-SV-102-1 Would Not Shut Fully.Cause Undetermined | | | 05000338/LER-1979-004-03, /03L-0 on 790108:during 1-PT-36-1(A) Found That Steam Generator 3 Hi Hi Level Test Panel Was Faulty, Preventing Test of This Channel.Caused by Faulty Universal Logic Card on Test Panel | /03L-0 on 790108:during 1-PT-36-1(A) Found That Steam Generator 3 Hi Hi Level Test Panel Was Faulty, Preventing Test of This Channel.Caused by Faulty Universal Logic Card on Test Panel | | | 05000338/LER-1979-005-01, /01T-0 on 790129:mufflers for Emergency Diesel Generators Not Seismically Supported Nor Missile Protected as Required by Fsar.Caused by Const Error | /01T-0 on 790129:mufflers for Emergency Diesel Generators Not Seismically Supported Nor Missile Protected as Required by Fsar.Caused by Const Error | | | 05000338/LER-1979-005, Forwards LER 79-005/01T-0 & 79-008/01T-0 | Forwards LER 79-005/01T-0 & 79-008/01T-0 | | | 05000338/LER-1979-006-03, /03L-0 on 790111:damaged Wiper Seal Found on Hydraulic Suppressor 1-FW-HSS-233.Caused by Poppet Valves Which Control Lock Up Rate Being Improperly Set.Suppressor Replaced W/Operable Spare Suppressor.No Danger to Public | /03L-0 on 790111:damaged Wiper Seal Found on Hydraulic Suppressor 1-FW-HSS-233.Caused by Poppet Valves Which Control Lock Up Rate Being Improperly Set.Suppressor Replaced W/Operable Spare Suppressor.No Danger to Public | | | 05000338/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000338/LER-1979-007-03, /03L-0 on 781116:during Normal Operation,Fire Door S54-5 Between Unit 1 Emergency Switchgear Room & Cable Vault Was Sprung & Would Not Make a Tight Seal,Evidently Due to Attempt to Free It While Stuck | /03L-0 on 781116:during Normal Operation,Fire Door S54-5 Between Unit 1 Emergency Switchgear Room & Cable Vault Was Sprung & Would Not Make a Tight Seal,Evidently Due to Attempt to Free It While Stuck | | | 05000338/LER-1979-008-01, /01T-0 on 790129:design Flow of 37 Gpm to Charging Pump Coolers Could Not Be Met.Caused by 2 Inch Carbon Steel Piping & Charging Pump Skid Piping Being Too Large to Allow Adequate Flow | /01T-0 on 790129:design Flow of 37 Gpm to Charging Pump Coolers Could Not Be Met.Caused by 2 Inch Carbon Steel Piping & Charging Pump Skid Piping Being Too Large to Allow Adequate Flow | | | 05000338/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000338/LER-1979-009-03, /03L-0 on 790212:during Normal Operation,Snubber Support for C Steam Generator Atmosphere Discharge Line Found Damaged.Caused by Use of Support as Anchor for Chain Fall.Support Replaced | /03L-0 on 790212:during Normal Operation,Snubber Support for C Steam Generator Atmosphere Discharge Line Found Damaged.Caused by Use of Support as Anchor for Chain Fall.Support Replaced | | | 05000338/LER-1979-010-03, /03L-0 on 790127: During Calibr of Containment Particulate Monitor RMS159 in Mode 1, Instrument Read Low for Known Radiation Level. Caused by Detector High Voltage Setting Being Set Too Low | /03L-0 on 790127: During Calibr of Containment Particulate Monitor RMS159 in Mode 1, Instrument Read Low for Known Radiation Level. Caused by Detector High Voltage Setting Being Set Too Low | | | 05000338/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000338/LER-1979-011-03, /03L-0 on 790126:fire Door SS54-9 Was Nonfunctional.Caused by Removal of Latch from Door by Person or Persons Unknown | /03L-0 on 790126:fire Door SS54-9 Was Nonfunctional.Caused by Removal of Latch from Door by Person or Persons Unknown | | | 05000338/LER-1979-012-03, /03L-0 on 790127: Unidentified Primary Coolant Leakage Greater than 5 Gpm Noted. Caused by Blown Packing on Residual Heat Removal Isolation Valve MOV-1700 & Packing Leak on Pressurizer Spray Valve PCV-1455A | /03L-0 on 790127: Unidentified Primary Coolant Leakage Greater than 5 Gpm Noted. Caused by Blown Packing on Residual Heat Removal Isolation Valve MOV-1700 & Packing Leak on Pressurizer Spray Valve PCV-1455A | | | 05000338/LER-1979-013-03, /03L-0 on 790214:during Normal Operation,Fire Door S71-7 Between Auxiliary Bldg & Health Physics Found non- Functional.Caused by Bent Phaser on Left Door.Phaser Taped Out of Way & New Phaser Installed | /03L-0 on 790214:during Normal Operation,Fire Door S71-7 Between Auxiliary Bldg & Health Physics Found non- Functional.Caused by Bent Phaser on Left Door.Phaser Taped Out of Way & New Phaser Installed | | | 05000338/LER-1979-014-03, /03L-0 on 790202:pressurizer Level Indicator Indicated High Over Allowable Range.Caused by Voltage Drift in Associated Level Transmitter.Appropriate Channel Placed in Trip Condition & Transmitter Recalibr | /03L-0 on 790202:pressurizer Level Indicator Indicated High Over Allowable Range.Caused by Voltage Drift in Associated Level Transmitter.Appropriate Channel Placed in Trip Condition & Transmitter Recalibr | | | 05000338/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000338/LER-1979-015-03, /03L-0 on 790204:rod F08 Indicators in Disagreement.Caused by Voltage Drift in Signal Conditioning Card.Card Recalibrated & Functional Checks Performed Satisfactorily | /03L-0 on 790204:rod F08 Indicators in Disagreement.Caused by Voltage Drift in Signal Conditioning Card.Card Recalibrated & Functional Checks Performed Satisfactorily | | | 05000338/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000338/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000338/LER-1979-016-03, /03L-0 on 790213:main Steam trip,TV-MS-111A,valve Opened to Only 75% Capacity.Caused by Improperly Positioned Needle Valve Which Supplied Air to Valve Actuator.Valve Repositioned & Operation Restored | /03L-0 on 790213:main Steam trip,TV-MS-111A,valve Opened to Only 75% Capacity.Caused by Improperly Positioned Needle Valve Which Supplied Air to Valve Actuator.Valve Repositioned & Operation Restored | | | 05000338/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000338/LER-1979-017-01, /01T-0 on 790212:during Axial Power Distribution Monitoring Sys Failure on 790206,FQ Survey Computer Program Could Not Monitor Axial Power Distribution.Caused by Incorrect Power Inputs from Process Computer | /01T-0 on 790212:during Axial Power Distribution Monitoring Sys Failure on 790206,FQ Survey Computer Program Could Not Monitor Axial Power Distribution.Caused by Incorrect Power Inputs from Process Computer | | | 05000338/LER-1979-018-03, /03L-0 on 790214:during Mode 1 Operation at 98% Power,Main Steam Trip Valve 1-TV-MS-111B Leaked Excessively & Was Isolated for Repair.Caused by Deteriorated Internal Gasket.Valve Isolated & Gasket Replaced | /03L-0 on 790214:during Mode 1 Operation at 98% Power,Main Steam Trip Valve 1-TV-MS-111B Leaked Excessively & Was Isolated for Repair.Caused by Deteriorated Internal Gasket.Valve Isolated & Gasket Replaced | | | 05000338/LER-1979-019-03, /03L-0 on 790216:during Surveillance,Emergency Diesel Generator 1H Did Not Reach 900 Revolutions Per Minute in Required 10-s.Probable Cause Was Low Ambient Air Temp. Conditions of First Start Were Not Reproducible | /03L-0 on 790216:during Surveillance,Emergency Diesel Generator 1H Did Not Reach 900 Revolutions Per Minute in Required 10-s.Probable Cause Was Low Ambient Air Temp. Conditions of First Start Were Not Reproducible | | | 05000338/LER-1979-020-03, /03L-0 on 790131:fire Door S54-9 Was Found to Be non-functional.Caused by Recently Installed Electric Door Strike Slipping Out of Adjustment | /03L-0 on 790131:fire Door S54-9 Was Found to Be non-functional.Caused by Recently Installed Electric Door Strike Slipping Out of Adjustment | | | 05000338/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000338/LER-1979-021-99, /99T-0 on 790212:meterological Air Temp Change in Temp Indication Was Observed to Be off-scale Low.Caused by Faulty Resistance Temp Detector.Temp Element Replaced | /99T-0 on 790212:meterological Air Temp Change in Temp Indication Was Observed to Be off-scale Low.Caused by Faulty Resistance Temp Detector.Temp Element Replaced | | | 05000338/LER-1979-021, Forwards LER 79-021/99T-0 | Forwards LER 79-021/99T-0 | | | 05000338/LER-1979-022-03, /03L-0 on 790227:power Supply to Post DBA H Recombiner Deenergized Rendering Recombiner Inoperable for 4-h.Caused by Deenergizing of Motor Control Center to Perform Voltage Measurements | /03L-0 on 790227:power Supply to Post DBA H Recombiner Deenergized Rendering Recombiner Inoperable for 4-h.Caused by Deenergizing of Motor Control Center to Perform Voltage Measurements | | | 05000338/LER-1979-023, Forwards LER 79-023/03L-0,79-025/03L-0 & 79-031/03L-0 | Forwards LER 79-023/03L-0,79-025/03L-0 & 79-031/03L-0 | | | 05000338/LER-1979-023-03, /03L-0 on 790303:disagreement Noted Between Group & Individual Indication for Rod D-10.Caused by Voltage Drift in Conditioning Card.Calibr & Functional Checks Were Performed | /03L-0 on 790303:disagreement Noted Between Group & Individual Indication for Rod D-10.Caused by Voltage Drift in Conditioning Card.Calibr & Functional Checks Were Performed | | | 05000338/LER-1979-024, Forwards LER 79-024/43X-1 | Forwards LER 79-024/43X-1 | | | 05000338/LER-1979-024-43, /43X-1:on 790228,radwaste Release Occurred Unexpectedly During Pumping of Unit 2 Containment Sump Via Temporary Pump to Storm Drain Sys.Caused by Pressure Relief Valve Leaks in Units 1 & 2 Purge Headers | /43X-1:on 790228,radwaste Release Occurred Unexpectedly During Pumping of Unit 2 Containment Sump Via Temporary Pump to Storm Drain Sys.Caused by Pressure Relief Valve Leaks in Units 1 & 2 Purge Headers | | | 05000338/LER-1979-025-03, /03L-0 on 790228:power Range Channel N42 Placed in Tripped Condition.Caused to Allow Replacement of Erratic Delta Flux Indicator.Indicator Replaced & Power Range Detector Returned to Svc | /03L-0 on 790228:power Range Channel N42 Placed in Tripped Condition.Caused to Allow Replacement of Erratic Delta Flux Indicator.Indicator Replaced & Power Range Detector Returned to Svc | | | 05000338/LER-1979-026-03, /03L-0 on 790306:RHR Discharge Valve Opened Accidentally Causing Loop C Accumulator Level to Drop Below Min Volume Required.Caused by Accidental Operation of MOV-1720B.Valve Closed & Loop Accumulator Level Restored | /03L-0 on 790306:RHR Discharge Valve Opened Accidentally Causing Loop C Accumulator Level to Drop Below Min Volume Required.Caused by Accidental Operation of MOV-1720B.Valve Closed & Loop Accumulator Level Restored | | | 05000338/LER-1979-027-03, /03L-0 on 790225:axial Flux Difference Deviated Greater than 5% from Target.Caused by Xenon Transient Occurring During Startup Operation.Corrected by Boration by Reactor Operator | /03L-0 on 790225:axial Flux Difference Deviated Greater than 5% from Target.Caused by Xenon Transient Occurring During Startup Operation.Corrected by Boration by Reactor Operator | | | 05000338/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000338/LER-1979-028-03, /03L-0 on 790225:greater than 12-step Disagreement Noted Among Rod Position Indication,Computer Position Indication & Demand Signal Indication for Rod 9.Caused by Voltage Drift in Signal Conditioning Card | /03L-0 on 790225:greater than 12-step Disagreement Noted Among Rod Position Indication,Computer Position Indication & Demand Signal Indication for Rod 9.Caused by Voltage Drift in Signal Conditioning Card | | | 05000338/LER-1979-030-03, /03X-1 on 790308:nonconservative Gain Setting on delta-flux Signal Feeding Overpower Delta T Protection Circuitry Observed.Caused by Improper Setting of delta-flux Gain.Signal Recalibr | /03X-1 on 790308:nonconservative Gain Setting on delta-flux Signal Feeding Overpower Delta T Protection Circuitry Observed.Caused by Improper Setting of delta-flux Gain.Signal Recalibr | | | 05000245/LER-1979-030-03, /03L-0 on 790308:calibr Procedure Revealed Nonconservative Gain Setting on delta-flux Signal Feeding Overpower Delta T Protection Circuitry.Caused by Improper Setting of delta-flux Gain.Signal Recalibrated | /03L-0 on 790308:calibr Procedure Revealed Nonconservative Gain Setting on delta-flux Signal Feeding Overpower Delta T Protection Circuitry.Caused by Improper Setting of delta-flux Gain.Signal Recalibrated | | | 05000338/LER-1979-031-03, /03L-0 on 790302:surveillances of Engineered Safety Feature Pumps Not Performed within Interval.Caused by Personnel Error Due to Long Period from Preoperational Tests to Operation.Surveillances Will Be Performed | /03L-0 on 790302:surveillances of Engineered Safety Feature Pumps Not Performed within Interval.Caused by Personnel Error Due to Long Period from Preoperational Tests to Operation.Surveillances Will Be Performed | | | 05000338/LER-1979-032-03, /03L-0 on 790312:containment Vacuum Pump Suction Valve TV-CV150A Would Not Remain Closed When Operated from Control Room.Caused by Relay Sticking in Energized Position.Relay Repaired & Tested Satisfactorily | /03L-0 on 790312:containment Vacuum Pump Suction Valve TV-CV150A Would Not Remain Closed When Operated from Control Room.Caused by Relay Sticking in Energized Position.Relay Repaired & Tested Satisfactorily | | | 05000338/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | | | 05000338/LER-1979-033, Forwards LER 79-033/03L-0,79-036/03L-0,79-037/03L-0 & 79-038/03L-0 | Forwards LER 79-033/03L-0,79-036/03L-0,79-037/03L-0 & 79-038/03L-0 | | | 05000338/LER-1979-033-03, /03L-0 on 790321: C Steam Generator Narrow Range Level Indicator LI-1496 Gave Readings w/20% Disagreement W/Two Other Channels.Caused by Steam Leak in One Sensing Line Isolation Valve | /03L-0 on 790321: C Steam Generator Narrow Range Level Indicator LI-1496 Gave Readings w/20% Disagreement W/Two Other Channels.Caused by Steam Leak in One Sensing Line Isolation Valve | |
|