ML19207A145

From kanterella
Jump to navigation Jump to search
Forwards 790131-0223 Steam Generator Tube Insp Rept
ML19207A145
Person / Time
Site: Haddam Neck File:Connecticut Yankee Atomic Power Co icon.png
Issue date: 05/23/1979
From: Counsil W
CONNECTICUT YANKEE ATOMIC POWER CO.
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19207A146 List:
References
NUDOCS 7905300323
Download: ML19207A145 (1)


Text

RC F O RPA.'G5

~

~

f h" D l, l j b

}

Update to a previous rescet 77) in i

LICENSEE EVENT REPORT Ui a

lau t,.

subnitted August 2,1979 cotJTRol B LCCK: l l

l 1

l l lh (PLEA' 0 l'nlNT OR TYPE ALL REQUlH 80 INFOnuATinN' I

6

. J,c ! A I E I I I H I 2 l@! 010 l0101010101010 (010j@{411(1{llil@l l

Jg i

u t,.su Cm i4 is uC v.o.e..-

a a

u CLNst n,.e o

,,u,..,

"X "Cc l L }@l 0 i 510101013 l 6 l 6 '@l 016 I 2 1217 (9 l@l0 IS l1 1017 1 nn li bd c)

EVENT C Af ti 44 1h HtPOH T OAT E oJ 6;

t> I cc;nsT3.v93ga EVENT oESCRIPTioN AND PRC3ABLE CONSEQUENCES h 1 During startuo coerations at 25 fat, the hydrogen qas concentration, measured down-t a

2 This value is greater than the l

Lstream of the recombiners, increased to about 13%.

,3 3

1 Technical Specification Apoendix B Section 2.1.3.h limit of 4%. The hydrogen level j

,#4 There I was greater than 4% for aporoximately two hours before returning to normal.

a45 I has been two mcre events of this type, one occurring on 7-15-79 at 320 ;?At and one j

a o

The hydrogen level for the e"ent on 7-7-79 exceeded the 4%

o 17 ! I on 7-7-79 at 256 ;"4t.

linit for about 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> and the event of 7-15-79 exceeded the 4% limit for about 65

__C s

8 9 s.

C09P.

VA LV E SYSTE*A CAU3E CAUSE CCOE CODE SUSCOCE CC*/PONENT COCE SUSC7DE SUSOCOE TlT)

I nl Bl@ l Di@ l Z i@ IR IE Ic 10 IM IB !@ l Zl@ l Z j @

8 9

IJ II 12 IJ 16 19 2s CCCUE'JTI AL OCCU A R ENCE RE PO'1T REVI;lON LERJA EVE'H YE A R REFCRT NO.

CODE TYPC NQ h nuvm"O17 l 9J l-l l0 l7 !S I

]/]

]O l3 l lLl l___l l1 l me

,_ 21 22 23 24 M

27 23

.")

3J J1 0;

fC P 'l F U 'L':' E E8:EC?

S a tfTD" tlN ATT AC W.' E N T N P 7 0-4 PRIME t**"P.

CO"'OVCNT TA=EN A CTi; C,*4 e LN.T 9=4 r00 HOUR 3 SU WITT E D FOM'* dui OU P L i.- i "ANUrc.CrL'In

[,13,1Hj@

ij !@

[2_J@

l 0101010 l l1 [@ WQ lM !@

lC (1 !613 j@

.s a

u 2

4a m

n 43 u

a c.sust cesCmPTroN ANo cc=ntC,ve Acmow @

Tl i The ortbable cause for the event on.6-22-79 was the i-crocer coeretion of tna pre-

,i i

ii G l hster which resulted in insufficicnt temaerature of the gases and droplets of mo ct ;

The procable 3

, y l ure enterina the recerbiner, thus reducing its recctbining ability.

l cause fcr the other two event'; was excessive moisture entering the recnabiner during j

i,,-

transient conditions of o'. ant startuo operations.

An investigstion is undere.'ay to ii 64i l eo 6 3 UE TPCD CF STArJt

%FOWER OT14E9 STATUS Ot$0CVE Av DIOCO% FW O!SCFil8T10' F ACiliTV l5 iGl@ l0!OI1l@

NA l

l A l@l Operator Observation l

i 80 3 J

'J

1 11 44 45 46 ACTIVITY CONTENT LCC ATICN OF RELE ASE AFLF MiD OFHELELP A4tOUNT Cr ACT1vtTY II l l2 80 44 45 1

9 la ii PL A5CN*.[L E RPO sum f 3 E_! 1010 10 3 7 @OCSCrHPTION nA i

M '% E 1

!Y"E 7

8 9 11 1'

sJ PE EONNE L INJLnits ttvatn r E:;:upt iCN t-11c1010 @

nA 1

is 03 LCCS OF OR OW AM TO FACILITY @

7908200 2

P 7

3 3 in u.:,.i T, m.

a aG

-nA i i i

)

Ia lJ e

1-t ".

C4# 3 ;ON NA l

l t 1iiiI I I__!_ _!i. a i.>:; !JiX.'.

69 c3 i

L s

r s

J w

( 91'!) M7-7El W. H. reg r: Haal'h Physici' _

7 ggy n

.c : 4.

'm

~

Georgia Power Company Plant E. I. Hatch Baxley, Georgia Reportable Occurrence Report flumber 50-366-1979-078 Event Description and Probable Consequences continued hours. There were no effects upon the public health and safety due to

-these events.

/

Caure Description and Corrective Actions continued identify and correct deficiencies in the operation of this equipr.ent.

6 0

0 W

9

  • Ea