|
---|
Category:Deficiency Correspondence (per 10CFR50.55e and Part 21)
MONTHYEARML19158A1302019-05-31031 May 2019 Curtiss-Wright Nuclear Division - Notification Report for Potential Part 21 Update ML19078A0872019-03-0808 March 2019 Curtiss-Wright - Interim Notification Report for Potential Part 21 Update ML18332A1222018-11-15015 November 2018 Curtiss-Wright - Interim Notification Report for Potential Part 21 Update ML15259A5212015-09-10010 September 2015 Part 21 Report - Potential Failure of Electromatic Relief Valve Cutout Switches ML15161A2302015-06-0404 June 2015 Part 21 Report Regarding Potential Failure of a Time Relay at Quad Cities ML14210A0102014-07-23023 July 2014 Part 21 - Unseating of Valve Spring on Scram Solenoid Pilot Valve ML14204A7072014-07-23023 July 2014 Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Unseating of Valve Spring on SSPV ML14079A0272014-03-13013 March 2014 Part 21 - Unseating of Valve Spring on Scram Solenoid Pilot Valve ML13165A3422013-06-12012 June 2013 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML13094A1772013-03-18018 March 2013 Notice to the U.S. Nuclear Regulatory Commission of a Possible Deviation or Defect in Nuclear Qualified High Efficiency Particulate Air Filters Manufactured by Aaf ML13044A0752013-02-0808 February 2013 Part 21 - Completed Evaluation for Potential Error in Main Steam Line High Flow Calculational Methodology ML12347A3082012-12-12012 December 2012 Part 21 60-Day Interim Report Notification: Error in Main Steam Line High Flow Calculational Methodology ML12319A0122012-09-27027 September 2012 Error in Main Steam Line High Flow Calculational Methodology ML12258A3992012-09-10010 September 2012 Potential Part 21 Issue Related to Tyco Timing Relay ML12226A0022012-08-0202 August 2012 Revision to Notification Date 07/31/2012 Regarding Manufacturing Defect in a Timing Relay Which Prevents the Relay from Operating at a Specific Setting ML12219A3042012-08-0202 August 2012 Potential Part 21 Issue Related to Tyco Timing Replay ML12158A4472012-06-0606 June 2012 Part 21 60-Day Interim Report Notification - Closufailure of CRD Collet Retainer Tube/Outer Tube Weld ML12094A3712012-04-0202 April 2012 Part 21 Report - Rosemount Pressure Transmitters with Nonzero Based Calibrations ML1127000672011-09-26026 September 2011 GE-Hitachi Part 21 Reportable Condition Notification: Failure to Include Seismic Input in Channel-Control Blade Interference Customer Guidance ML1025202192010-09-0303 September 2010 Part 21 - Failure to Include Seismic Input in Reactor Control Blade Customer Guidance ML0907611882009-03-11011 March 2009 Part 21 Notification - Defective Hk and K-Line Circuit Breaker Tension Springs ML0623700952006-08-21021 August 2006 Update to Part 21 Interim Report Notification: Failure Analysis of Core Shroud Repair Tie Rod Upper Support Crack ML0232901622002-11-18018 November 2002 Final Report, Stability Option III: Possible Successive Confirmation Count Resets - Not Reportable 2019-05-31
[Table view] Category:Deficiency Report (per 10CFR50.55e and Part 21)
MONTHYEARML22087A0092022-03-0909 March 2022 Ultra Energy, Report Under 10CFR21 of Noncompliance for N7030 Transmitter ML19347A4262019-12-10010 December 2019 General Atomics - Reportable Occurrence Under 10CFR21: Reported Failure in Analog High Range Radiation Monitor (RP-2C) ML19168A0102019-05-31031 May 2019 Curtis-Wright Nuclear Division- Notification Report for Potential Part 21 Update ML19158A1302019-05-31031 May 2019 Curtiss-Wright Nuclear Division - Notification Report for Potential Part 21 Update ML19078A0872019-03-0808 March 2019 Curtiss-Wright - Interim Notification Report for Potential Part 21 Update ML19053A5002019-02-0101 February 2019 Sor, Inc. Part 21 Notification of Deviation Sor R-Series Housing with Terminal Block ML18289A4572018-10-0808 October 2018 Curtiss-Wright Nuclear Division - Interim Notification Report for Potential Part 21 with Exelon Powerlabs Failure Analysis ML17194A8252017-07-11011 July 2017 Part 21 Report Re Wedge Pin Failure in Anchor Darling Motor Operated Double Disc Gate Valves with Threaded Stem to Upper Wedge Connections ML16281A2712016-09-30030 September 2016 Part 21 - Safety Related Component Welding by an Unqualified Welder ML16243A4752016-08-26026 August 2016 Part 21 Safety Related Component Welding by an Unqualified Welder ML16188A3742016-06-30030 June 2016 Part 21 - Inadequate Swaging and Adherence of Silicone O-Ring and Silicone PAD Soft Seat Main Disc and Pilot Disc Assemblies ML15259A5212015-09-10010 September 2015 Part 21 Report - Potential Failure of Electromatic Relief Valve Cutout Switches ML15253A8592015-09-10010 September 2015 GE-Hitachi Nuclear Energy Americas, LLC - Closure of Part 21 60-Day Interim Report Notification: Potential Failure of Electromatic Relief Valve Cutout Switch ML15211A4962015-07-24024 July 2015 Part 21 - Actuator Shaft Did Not Meet Dimensional Requirements ML15169A0082015-06-18018 June 2015 Attachment 1 - Us Plants Potentially Affected ML15169A0092015-06-18018 June 2015 Attachment 2 - 60-Day Interim Report Notification Information Per 21.21(a)(2) ML15169A0102015-06-18018 June 2015 Enclosure 1 - Mfn 15-042 R0 - Description of Evaluation ML15169A0072015-06-17017 June 2015 Part 21 60-Day Interim Report Notification: Potential Failure of Electromatic Relief Valve Cutout Switch ML15161A2302015-06-0404 June 2015 Part 21 Report Regarding Potential Failure of a Time Relay at Quad Cities ML15022A6502015-01-20020 January 2015 Letter from Steven R. Eisenberg USNRC 10CFR Part 21 Notification ML14275A1622014-09-25025 September 2014 Notification of Potential Part 21 Report - Electromatic Relief Valve Excessive Wear ML14210A0102014-07-23023 July 2014 Part 21 - Unseating of Valve Spring on Scram Solenoid Pilot Valve ML14204A7082014-07-23023 July 2014 Enclosure 2, Description of Closure Evaluation, Non-Proprietary Information - Class I (Public) ML14204A7072014-07-23023 July 2014 Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Unseating of Valve Spring on SSPV ML14197A3802014-07-14014 July 2014 Part-21 Notification-Assembly Errors During Breaker Refurbishment ML14072A3282014-03-13013 March 2014 Part 21 60-Day Interim Report Notification Re Unseating of Valve Spring on SSPV ML14072A3262014-03-13013 March 2014 Enclosure 2: Description of Evaluation ML13165A3422013-06-12012 June 2013 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML13064A0122013-02-25025 February 2013 Notification of Potential Part 21 Report Re Wedge Pin Failure of an Anchor/Darling Double-Disc Gate Valve ML13042A0962013-02-0808 February 2013 Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Error in Main Steam Line High Flow Calculational Methodology ML13044A0752013-02-0808 February 2013 Part 21 - Completed Evaluation for Potential Error in Main Steam Line High Flow Calculational Methodology ML12352A1232012-12-13013 December 2012 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML12348A1362012-12-13013 December 2012 Part 21 60-Day Interim Report Notification: Adequacy of Design Change in Am Magne-Blast Circuit Breakers ML12347A3082012-12-12012 December 2012 Part 21 60-Day Interim Report Notification: Error in Main Steam Line High Flow Calculational Methodology ML12319A0122012-09-27027 September 2012 Error in Main Steam Line High Flow Calculational Methodology ML12258A3992012-09-10010 September 2012 Potential Part 21 Issue Related to Tyco Timing Relay ML12219A3042012-08-0202 August 2012 Potential Part 21 Issue Related to Tyco Timing Replay ML12177A0562012-06-21021 June 2012 Part 21 - Reliability Degradation of Resistors in Trip Units and Readout Assemblies ML12158A4472012-06-0606 June 2012 Part 21 60-Day Interim Report Notification - Closufailure of CRD Collet Retainer Tube/Outer Tube Weld ML12163A1302012-06-0606 June 2012 Part 21 Report - Failure of CRD Collet Retainer Tube/Outer Tube Weld ML12094A3712012-04-0202 April 2012 Part 21 Report - Rosemount Pressure Transmitters with Nonzero Based Calibrations ML12058A1412012-02-23023 February 2012 Part 21 Report - Rosemount Nuclear Instruments, Inc., Pressure Transmitter with Nonzero Based Calibrations ML12040A2832012-02-0707 February 2012 Notification of Potential Part 21 - Failure to Include Seismic Input in Reactor Control Blade Customer Guidance ML12038A0282012-02-0202 February 2012 Failure of CRD Collet Retainer Tube/Outer Tube Weld ML12032A2402012-02-0101 February 2012 Notification of Potential Part 21 - 60-Day Interim Report Notification: Failure of CRD Collet Retainer Tube/Outer Tube Weld ML11228A0842011-08-12012 August 2011 Notification of Part 21 - Failure to Include Seismic Input in Reactor Control Blade Customer Guidance ML1122401422011-08-11011 August 2011 Part 21 60-Day Interim Report Notification: Failure to Include Seismic Input in Channel-Control Blade Interference Customer Guidance ML1106701742011-02-28028 February 2011 Notification of Potential Part 21 Re Limited E7000 Relay Recall (CII-021) ML1106107042011-02-28028 February 2011 Notification of Potential Part 21 Report - Specified Relays with Degraded Coils ML1104800542011-02-15015 February 2011 Notification of Potential Part 21 Reportable Condition: Crack Indications in Marathon Control Rod Blades 2022-03-09
[Table view] |
Text
Nuclear Division 4600 East Tech Dr.
- Cincinnati, OH 45245 Phone: 513.528.7800
- Fax: 513.528.9292 www.CWNuctear.com March 8, 2019 U.S. Nuclear Regulatory Commission Attn: Document Control Desk 5"'/J- Z-5'/ /ZIPS Washington, D.C. 20555-0001
Subject:
Interim Notification Report for Potential Part 21 update.
Dear Sir or Madam:
In reference to the Curtiss-Wright Interim Notification Report dated 10/8/2018 (Event No.
ML18289A457/Log No. 2018-24-00) for an EA700-90964 limit switch failure, the following updates are provided.
Curtiss-Wright's investigation is ongoing, with the current focus being the evaluation of in-service switch operating temperatures and results from a recent disassembly/inspection of similar switches (same model but different date codes). Additional inspection of other switches currently in-service at the plant is needed to finish the investigation. Evaluation of these switches is expected to be completed by mid May. Once this data is made available, a final conclusion as to the root cause of the failme can be detennined.
We therefore request additional time to complete our evaluation and should have our final report issued by May 31, 2019.
Sin~~
Tim Franchuk Director, Quality Assurance Curtiss-Wright Nuclear Division, Cincinnati Operations 513-201-2176 TFranchuk@CurtissWright.com