ML18353A844

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Licensee Event Report UE-75-11 & UE-75-12 - LPSI Pump Seal Leakage & Seal Was Replaced with Similar Unit
ML18353A844
Person / Time
Site: Palisades Entergy icon.png
Issue date: 12/22/1975
From: Bixel D
Consumers Power Co
To: James Keppler
NRC/RGN-III
References
LER UE-1975-011-00, LER UE-1975-012-00
Download: ML18353A844 (2)


Text

.,;* *.

consumers Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201

  • Area Code 517 788-0550 December 22, 1975 Mr James G. Keppler Office of Inspection Enforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Gle~ Ellyn, IL 60137 DOCKET 50-255, L~CENSE DPR-20 PALISADES PLANT, REPORTABLE OCCURRENCES UE-75-11 & UE-75-12 Attached is a reportable occurrence report which relates to the Palisades Plant and has been classified as a condition leading to operation in a degraded mode.

Plant Technical Specifications permit operation to continue for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> with an additional 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> allowed to reach the hot shutdown condition.

The pump was out of service for 29 hours3.356481e-4 days <br />0.00806 hours <br />4.794974e-5 weeks <br />1.10345e-5 months <br /> and plant shutdown was not required.

c;9-~d~

David A. Bixel

/~

Assistant Nuclear Licensing Administrator CC:

File

CONTROL BLOCK: I 1

liiWENSEE EVENT REPORT

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I ~ I I I

[PLEASE PRINT AU REQUIRED INFORMATION]

LICENSEE NAME aiifil IM I I I p I Al LI ii

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9 14 CATEGORY REPORT TYPE 6

LICENSE NUMBER lolol-lol ol olo lol-lolol 15 25 REPORT SOURCE LICENSE TYPE I 4 I i 11 I i 11 I 26 30 EVENT DATE EVENT TYPE lo I 3 I 31 32 REPORT DATE

@illcoN'T r

  • I
  • I 7

8 57 58 l.J;J lbJ DOCKl;T NUMBER I o I 5 I o I ~ I o 12 I 5 I 5 I 1111121211151 1112121211151 59 60 61 68 69 74 75 80 EVENT DESCRIPTION lol2I I During normal operation, LPSI 7

8 9 pump seal leakage was observed while performing a I

80 10131 I periodic test.

The pump was removed from service and the redundant pump demonstrated I 7

8 9 lol41 I operable.

7 8 9 There are no records of previous problems.

The seal was replaced with a

~ I similar unit (UE-75-11 & -12).

7 8 9

[oj6I 7

8 9 SYSTEM CODE

@0 Is IF I CAUSE CODE COMPONENT CODE

~ I P lu IM IP I x I x I 7

8 9 10 11 12 17 CAUSE DESCRIPTION PRIME COMPONENT SUPPLIER l!J 43 COMPONENT MANUFACTURER II 1° 17 15 I 44 47 VIOLATION

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48

~ I Seal leakage appears to be caused by improper 0-ring clearance.

The pump is Type 7

B 9

~ I 8X21 Al, Ser A-67393 or 4.

7 8 9 The plant staff will investigate improved seal design I and methods for reducing repair.time.

B9 FACILITY STATUS

% POWER OTHER STATUS EEi W

I ol 1 I 9 I 7

B 9

10 12 13 FORM OF ACTIVITY RELEASED CONTENT NA I

44 rn w OF RELEASE AMOUNT OF ACTIVITY lli._J l.__ ____ ---"'-NA------~

7 B

9 10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION

~lo I ol ol w NA 7

B 9 11 12 13 PERffONNEL INJURIES NUMBER DESCRIPTION EE! I 0 I 0 I 0 I NA 7

B 9 11 12 PROBABLE CONSEQUENCES METHOD OF DISCOVERY DISCOVERY DESCRIPTION w I NA.

45 46 LOCATION OF RELEASE NA 45

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J No probable consequences.

Redundant :i?umP was demonstrated operable.

7 B 9 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION

~.W NA 7

B 9 10 PUBLICITY illZl NA 7

B 9

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ADDITIONAL FACTORS

~9 illfil 7

B 9 80 I

80 I

80 BO I

BO I

BO I

BO I

BO BO

. BO BQ BO BO BO BO BO