ML18283B485

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Abnormal Occurrence Report BFRO-50-296/762W Control Rod Drive Pump Removed from Service to Permit Installation of Strain Gauge Instrumentation on Selected Fuel Channels
ML18283B485
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 08/06/1976
From: Fox H
Tennessee Valley Authority
To: Moseley N
NRC/IE, NRC/RGN-II
References
BFRO-50-296/762W
Download: ML18283B485 (6)


Text

TO:

N.C. Moseley FROM: Tennesee Valley Authority Chattanooga, TN..

H.S. Fox gLETTER K)ORIGINAL QCOPY 0 NOTO8 I2 E D PUNCLASSIFIED PROP INPUT FORM

'NRC FoRM 195 U.S. NUCLEAR REGULATORY COMMI N

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I NRC DISTRIBUTION FoR pA'RT 50 DOCKET MATERIAL DOC KEQ4 UQBQ R FILE NUMBER XNCXDENT REPORT DATE OF DOCUMENT 8-6-76 DATE RECClVEO NUMBER OF COPIES RECEIVED DESCRIPTION Ltr.

trans the following......

PLANT NAIKi; Browns Ferry 8

3 ENCLOSURE Licensee Event Report (R.O.

/> 762) on 7-23-76 Concerning the control rod drive pump being removed to permit the installation of strain gauge instrumentation.......

(1 Signed Cy. Received)

ACKNOWLEDGED DO NQ1 -H,g]g0VE NOTE; IF PERSONNEL EXPOSURE XS INVOLVED SEND DIRECTLY TO KREGER/J,COLLINS RANCH CKEEF W

CYS FOR ACTION XC..ASST.:

W CYS CRS 16CYS Lee FOR ACTION/INFORMATION SAB 8-10-7 C PDR SEE 2

PC CHROEDER IPPOLITO iOUSTON OVAK CHECK RIMES

,ASE INTERNALD ISTRl BUTION ESCO MACCARY ISENHUT

'R OLLMER EJNCH GER J.COLLINS enise PDR:

Athens Ala.

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EXTERNAL DISTRIBUTION CONTROL NUMBER 8087 NRC FORM 195 I2.76)

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TENNESSEE VALLEYAUTHORITY CKATTANOOCeA. T 37401 DOCKOSD Auyurb 6s 1976 9

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P(01I Seetfcte Ih. XToxman C, Mosey@~

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n Office of Xnspection and.

Znfo'econ XX 230 Peachtrce Street, Rf,>. 8th Floor Atlantat, Ceorp&

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Dear Ih'e,

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TQIGMH VAXZZ[AUTIIRXZ SROLKS ABBYXCXMFJMT KGZ 3-SOCKET Hoi $0 2g6 MCXLEX OPEHATXL7{r'ECTUE DPR 68 ~ REPORTABXIE OCcuxuZCZ REPORT amo-gO-'ag6/76m>

The cnclosecL rexlort is to provico Retails concondng the control rod drive pump which >ms remcnred. fran servico to Xtermit the installntion of strain gauge instnmentation on aelecteC fuel channels anl is subnd.tte6 in accordance td.th ApyemHx E to Regulatory GuMe 1.16> Revision 4s August 1975.

This event

'occurTecl on ~lfAB PQzzg KQclCar Plant uni'te 3o

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5KGZSSEH VATifZKAUTHOBZK I, S, Peat.'rector of Power Production Znclosure (3)

CC (Enclosure):

&rector (3)

Office of~~t Xnformation and, Pl~an Contro1'.S, Bud,ear ReyQntory'mznission VashinIMn, D.C.

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Director 40 office of Xnsyection anl Znforcemnxk U.S. Qxclear RemQatoiy Cmmission Uashington, D.C.

20m An Equal Opportunity Employer

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CONTROL BLOCK UCENSEE NAME A

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6 LICENSE NUMBER 0

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15 REPORT (PL c PRINT ALLREQUIRED INFORMATION)

UCENSE EVENT TYPE TYPE 0

0 4 1 1

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~01 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE REPORT OATE

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8 57 58 59 60 61 68 69 74 75 EVENT DESCRIPTION Qpg On 7/23/76, the control rod..drive pump was removed fram service to permit the 80 7

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installation of strain gauge instrumentation on selected. fuel channels.

Cn 7

89 80 lDOER]

7/27/76, Surveillance Instruction 4.3.A.2-d determined the control rod 7

8 9 80 t00j5

. accumulators to be inoperable due to low pressure without the requirements of

/06 LC033A2b being met (BFRO-50<<296/762 )

COMPONENT MANUFACTURER 7

8 9 work was a roved..

7 8 9 7

8 9 PAME SYSTEM CAUSE COMPONENT CODE CODE COMPONENT CODE SUPPUEA VOLATION R

D R

V E

N 0 0 8

0 7

8 9 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION

[0D8]

The requirement of LC033A2b was overlooked by plant personnel when the 80 80 '

80 OTHER STATUS 7

89 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION Q6 R

HA 7

89 10 PUBLICITY NL 7

89 7

89 FACILITY STATUS POWER

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NR 7

8 9

10 12 13 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY Q~g

~Z I Z HA 7

8 9

10 11 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION, I113I ~00 0

2 NA 7

89 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION t1I1j ~00 0

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89 11 12 OFFSITE CONSEQUENCES 15 NA METHOD OF OISCOVERY B

44 45 46 NA 44 45 OISCOVEAY DESCRIPTION LOCATION OF RELEASE 80 80 80 80 80 80

, 80 80 ADDITIONAL FACTORS

~18 Although the control rods were not disarmed, with the CRD pumps off, the rod.

7 89 could not be moved.

7 89 80 00 NAME:

PHONE CPO est-607

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