ML18219E006
| ML18219E006 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 08/06/1976 |
| From: | Hunter R American Electric Power Service Corp |
| To: | James Keppler NRC/RGN-III |
| References | |
| Download: ML18219E006 (5) | |
Text
DOCKET NUMBER 50-315 Fl E NUM L
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- American Elec.
Power Corp.
New York, N.Y.
R.S.Hunter DATE OF DOCUMENT 8-6-76 TO: J.G. Keppler DATE RECFIVED 8-11-76 C3NOTORIZED g UNC LASSIF IE D NUMBER OF COPIES RECEIVED INPUT FORM PROP Qf.ETTE R
@ORIGINAL Ocopv ENCLOSU RE DESCRIPTION Ltr. advising of recent developments. that bear on the safety analysis of the D.C.Cook Nuclear
'Plant in their judgement constitue unreviewed safety questions.......
'ACKNOWLEDGED
.(
1 CarbonsSigned Cy. Received)
(2 Pages) iyp@PT REMOVE NOTE:
IF PERSONNEL EXPOSURE IS INVOLVHLI SEND DIRECTLY TO KREGER/J.,COLLINS PLANT Na:
Cook I/
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File Cfn araki ROBERT S. HUiVTER Vice Prccidcnt-h'ttctcar Engineering lj 2 Broadtt:
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AUGJ J. tg16 Donald C. Cook Nuclear Plant Operating License DPR-58 Docket No. 50-315 August 6, 1976 Mr. J.
G. Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, Illinois 60137
Dear Mr,
Keppler:
This letter is to confirm our telephone report to your Mr.
."rC'Boyd at approximately 1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br /> on August 6, 1976, pursuant to the re'quirements of Appendix A Technical Specifications and the U.S.
- '=;.t'Nuclear Regulatory Commission Regulatory Guide 1.16, Revision 4, Section 2.a.
At that time we reported that on August 5, 1976, westinghouse informed us by telephone of recent developments that bear on the safety analysis of the Donald C. Cook Nuclear Plant which in their judgment constitute unreviewed safety questions.
The first issue -involved the temperature of the fluid in the reactor vessel upper hea'd' Past ECCS analyses assumed that the temperature in the upper head was equal to vessel inlet temperature.
Recent model tests, improved analytical techniques and one in-plant measurement suggest this to be in error and a more appropriate assump-tion is that the upper head temperature is 75K of the difference between vessel outlet and inlet temperature (added to inlet temperature).
The impact of this finding with reference to the Cook Nuclear Plant is a necessary reduction in Fn to prevent operation at an unaccept-able power level.
The current pla8t allowable Fq is 1.98.
Mestinghouse
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Mr, J, G. Keppler August 6, 1976 tells us that the current analysis suggests an increase in this value to 2.05, but because of this upper head temperature problem, this analysis will only permit operation with an Fz of 2.02, which is above our current technical specification limit of 7.98.
Our actual core peaking factor as determined by current in-core measurements is sub-stantially below the current technical specification limit.
Another consequence of this upper head fluid investigation concerns the effects on the steam line break analysis, but Westinghouse has reviewed the specific Cook case and informed us that this has no effect on Cook Nuclear Plant.
A separate problem involves rod bow.
Recent results indicate that the rod bow DNB penalty is higher than previously used as a
licensing basis.
The combination of this penalty with available margin will result in an estimated reduction of 8$ in DNBR.
To maintain safe operation of the plant this reduction has been incorporated by revising the FgH limit in our in-core flux mapping program.
To do this, we have lowered our Fg,H operating limit by 4I, from 1.51 to 1.45, a value which we are assured by Westinghouse will compensate for this 8Ã DNB penalty.
Our actual F~ as determined by current in-core measurements is less than the modified limit.
Westinghouse advised us that they will keep AEP informed on the results of meetings with the NRC on these matters and the acceptability of the recormended operating modification.
This letter constitutes the 24-hour written notification, and the written followup report which Section 2.a of Regulatory Guide 1.16, Revision 4, requires to be submitted within two weeks of the telephone notification.
If we receive additional information from Westinghouse on this subject which relates to our response, we will inform you.
Very truly yours, R. S. Hunter Vice President - Nuclear Engineering RSH kb cc:
John E. Dolan R. J. Vollen R. C. Callen K. R. Baker P.
W. Steketee R. Walsh Gerald Charnoff G. Olson J.
M. Hennigan R. S. Keith Plant Nuclear Safety Review Conmittee Director, IE (40 copies)
Director, MIPC 4