ML18136A317

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Forwards Responses to Infractions Reported in IE Insp Repts 50-280/79-61 & 50-281/79-80
ML18136A317
Person / Time
Site: Surry  
Issue date: 12/20/1979
From: Stallings C
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
990-112779, NUDOCS 7912270441
Download: ML18136A317 (4)


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RESPONSE TO IE INSPECTION REPORT NOS. 50-280/79-61 AND 50-281/79-80 NRC COMMENT:

(Appendix A)

As required by Section 3.21.G of the Technical Specifications 9 all penetration fire barriers protecting safety-related areas shall be functional at all times.

In the event a penetration fire barrier becomes non-functional 9 a continuous fire watch must be established on at least one side of the affected penetration within one hour.

Contrary to the above~ the fire door that controls the opening between the Unit 1 and Unit 2 Switchgear rooms at the 9 '-6" elevation was found inopera-

  • tive due to a 4160 volt transformer being stored in door opening which would not permit the door to close in the event of a fire and a continuous fire watch had not been established.

This is an infraction.

RESPONSE

The violation is correct as stated *

1.

Corrective steps which have been taken.

a.

Transformer has been removed.

z.

Corrective steps taken to avoid further infraction.

a~

Memorandum from Station Manager sent to all plant superintendents and contractors. to be aware not to block fire doors.

b.

Area to be checked more frequently to ensure there are no obstructions.

3.

Date when full compliance will be achieved.

a.

Fnll compliance has been achieved.

NRC COMMENT:

(Appendix B)

A.

Section IV.E.5 of the Fire Protection System Review for Surry Power Station of July 1, 1977 states that the carbon dioxide fire protec-tion systems at the plant meet the provisions of National Fire Protec-tion Association (NFPA) Standar'd 12, "Carbon Dioxide Systems".

Sections l.803.4 and 1-9.1.3 of NFPA-12 require a manual control station for

.actuation of the system to be located within the protected area.

The manual control station must be capable of activa'ting the bank of carbon dioxide cylinders that are in service.

Contrary to the above, the manual activation control device for the combination automatic and manual actuated carbon dioxide system protecting the diesel fuel tank room at the service water intake structure is arranged to only activate the ma.in bank of cylinders.

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Attachment page 2 NRC COMMENT (Appendix B) (continued)

RESPONSE

With the main bank of cylinders removed for recharge or repair, it is not possible to activate the reserve supply from the manual station within the fuel tank room.

This is a Deviation.

The violation is correct as stated.

1.

Corrective steps which have been taken.

a.

Main bank of cylinders has been replaced negating need for reserve supply.

2.

Corrective steps taken to avoid* further deviation.

a.

Main bank COz bottles will remain in service until a design change can be made.

A design change bas been submitted to insure activation capability of the reserve supply in the event the main bank is rendered inoperative.

3.

Date when full compliance will be achieved.

a.

Full compliance has been achieved.

NRC COMMENT:

(Appendix B)

B.

Section 9.10.1 of the Final Safety Analysis Report (FSAR) states that the fire protection systems and features for the plant, including

RESPONSE

fire barrlers, will be designed to meet the standards of the National Fire Prcrr_ection Association (NFPA). The standard for the fire doors is NFPA-80~ Fire Doors and Windows.

Section 516.b of NFPA-80-1968 Edition (Section 2-8.2 of the 1977 edition) requires all swinging type fire doors to be provided with approved positive latching devices.

Contrary to the above, the swinging type doors separating the three diesel generator rooms from the turbine building and the Unit 1 and 2 Switchgear rooms from the turbine building are not provided with positive acting latches to maintain these doors in the closed position in the event of fire.

This discrepancy may also exist on other fire doors located throughout the plant.

This is a deviation.

The violation is correct as stated.

1.

Corrective steps which have been taken.

a.

Positive acting latches have been installed on the doors to the diesel generator room.

Other fire doors have been in-spected and a latching mechanism installed as needed.


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RESPONSE: (continued)

2.

Corrective steps to avoid further deviation.

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Attachment page 3

a.

Administrative controls will be provided to assure the effective-ness of other fire doors.

3.

Data when full compliance will be achieved.

a.

Full compliance has been achieved *