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Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. ML18106A2571998-01-19019 January 1998 Nuclear Business Unit Future Objectives. ML18106A2131997-12-15015 December 1997 Safety Evaluation Supporting Rev to TS to Adopt Option B of 10CFR50,App J,For Type B & C Testing & Modify Existing TS Wording for Previous Adoption of Option B on Type a Testing ML18102B3331997-02-28028 February 1997 Rev 0 to Cfcu Return Piping Inside CTMT,221F Temp Effect. ML20133D2201996-12-0606 December 1996 Root Cause Analysis of Struthers-Dunn Operate-Reset Relay Latch Failures for Salem Generating Station ML20133D2251996-10-30030 October 1996 Struthers-Dunn Model 255XCXP Relay Root Cause Evaluation for Salem Nuclear Generation Station ML18102A3231996-07-0101 July 1996 Reg Guide 1.121 Assessment of Indications at Salem Unit 2. ML18102A1591996-06-0404 June 1996 Fuel Handling Accident Analysis Radiological Evaluation. ML20101M6601996-03-24024 March 1996 Supplemental Submittal in Response to NRC GL 87-02/USI A-46, 'Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors.' ML18102A1321996-03-15015 March 1996 Change 2EC-3332 to Rev 0 to Design Analysis, 125 Vdc Battery Charger Replacement. ML18102B0201996-02-28028 February 1996 Rev 0 to Evaluation of Structures for Increased Temps Due to Updated Main Steam Line Break. ML20129K1031995-07-10010 July 1995 Exam of Fasteners from Salem Nuclear Generating Station ML18101A7481995-05-19019 May 1995 Safe Shutdown Equipment List Rept for Salem Generating Station Units 1 & 2 ML18101A7491995-04-25025 April 1995 Relay Evaluation Rept, Volumes 1 & 2, for Salem Generating Station Units 1 & 2 ML18101A7501995-04-20020 April 1995 Seismic Evaluation Rept, for Salem Generating Station ML20134K1031995-03-24024 March 1995 Organizational Effectiveness Assessment Rept for Sngs, ML18102B6541995-03-24024 March 1995 Organizational Effectiveness Assessment Rept for Plant, Redacted Version ML18101A4391994-12-21021 December 1994 Fire Protection Review of Salem Reactor Coolant Pump Oil Collection Sys, Dtd 941221 ML20134C5791994-10-23023 October 1994 Salem/Maint SC.MD-GP.SW-0001(Q) Svc Water Silt Survey, Rev 5 ML18106B0541994-01-31031 January 1994 Criticality Analysis of Salem Units 1 & 2 Fresh Fuels Racks. ML18100A7971993-12-23023 December 1993 Simulator Four-Year Certification Rept. ML20069M2221993-10-15015 October 1993 Flux Thimble Thermocouple Ultrasonic Profilometry & Eddy Current Encircling Coil Insp of Stored Thimble Tubes Jul-Aug 1993 ML18100A6281993-09-16016 September 1993 Updated Page A4-4 of Boric Acid Concentration Reduction Effort Technical Bases & Operational Analysis, Changing Figure Numbers A5-1 & A5-2 to A4-1 & A4-2 at End of First Paragraph ML18100A6801993-08-20020 August 1993 Engineering Evaluation of Sgs 1 & 2 Control Room Evacuation for Fire Induced MOV Hot Shorts as Discussed in NRC Info Notice 92-018. ML20045B8801993-05-21021 May 1993 Boric Acid Concentration Reduction Effort Technical Bases & Operational Analysis for Salem Nuclear Generating Station, Units 1 & 2. ML18100A3401993-04-28028 April 1993 Licensing Rept for Spent Fuel Storage Capacity Expansion Pse&G,Salem Generation Station,Units 1 & 2. ML18096B3561993-02-11011 February 1993 Cycle 8 Peaking Factor Limit Rept. ML20135A8141992-12-29029 December 1992 Control Room Overhead Annunciator Lock-Up of 921213 ML18096B1661992-11-13013 November 1992 Rev 1 to Fracture Toughness Analysis for Salem Units 1 & 2 Reactor Pressure Vessels to Protect Against Pressurized Thermal Shock Events,10CFR50.61. ML18096B0081992-09-0202 September 1992 Analytical Data Rept, for Project 28173 ML18096A8061992-06-17017 June 1992 Rev 0 to Salem Unit 2 Response to Generic Ltr 92-01,Rev 1, 'Reactor Vessel Structural Integrity.' ML18096A8051992-06-17017 June 1992 Rev 0 to Salem Unit 1 Response to Generic Ltr 92-01,Rev 1, 'Reactor Vessel Structural Integrity.' ML18096A5831992-03-31031 March 1992 Rev 1 to Estimated Frequency of Loss of Off-Site Power Due to Extremely Severe Weather & Severe Weather for Salem & Hope Creek Generating Stations. ML18095A5151990-07-31031 July 1990 Vol 1 to Spring 1990 NDE of Selected Class 1 & Class 2 Components of Salem Generating Station,Unit 2. ML18095A3691990-07-26026 July 1990 Unit 1 Decommissioning Rept. ML18095A3681990-07-26026 July 1990 Unit 2 Decommissioning Rept. ML18095A3791990-07-20020 July 1990 Decommissioning Rept of Philadelphia Electric Co. ML18094B2241989-12-28028 December 1989 Simulator NRC Certification, Vols I-III ML18094A3551989-04-30030 April 1989 Assessment of Impacts of Salem & Hope Creek Generating Stations on Kemps Ridley (Lepidochelys Kempi) & Loggerhead (Carretta Caretta) Sea Turtles. ML20086U2571989-03-31031 March 1989 Estimated Frequency of Loss of Offsite Power Due to Extremely Severe Weather & Severe Weather for Salem & Hope Creek Generating Stations ML18093B2021988-09-30030 September 1988 Special Rept on Spare CRD Mechanism Weld Refurbishments. ML18093A7601988-02-18018 February 1988 Appendix R/Breaker Coordination as-Found Review (Pre-Audit 1987). ML18093A5471987-12-10010 December 1987 Breaker Coordination W/Respect to External & Internal Hazards. ML18093A4531987-10-14014 October 1987 Justification for Continued Operation of Salem Units 1 & 2 W/Outstanding Fire Protection Concerns. ML18093A4131987-10-0101 October 1987 Justification for Continued Operation of Salem Units 1 & 2 W/Outstanding Fire Protection Concerns. ML18093A3781987-09-16016 September 1987 Rev 7 to, Westinghouse Engineering Svcs Rept for Salem Nuclear Generating Station Units 1 & 2 Concerning RHR Sys Mid-Loop Operation Re NRC Generic Ltr 87-12. 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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- Page. 1 of 5 S-C-Rl20-CSE-287 Date 11/21/84 Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 TITLE: SAFETY EVALUATION FOR THE REPLACEMENT INTERVAL OF THE UVTA AND RELIABILITY CALCULATION OF THE DB-50 RE.ACTOR TRIP B.RE,AKER
~
1.0 PURPOSE To document and justify the replacement interval of the Undervoltage Trip Attachment and the reliability calculations for the Westinghouse DB-50 reactor trip breakers.
2.0 SCOPE This document applies to the Westinghouse DB-50 reactor trip breakers used at Salem Generating Station.
3.0 REFERENCES
3.1 Westinghouse summary of Test Results NS-EPR-2824, Letter from E. P. Rahe (Westinghouse) to H. Denton (USNRC),
October 1,, 1983.
3.2 IEEE Standard 352, 1975 Guide for General Principles of Reliability Analysis o.f Nuclear Power Generating Station.
Protection Systems *
. 3.3 Operational verification Program Reactor Trip Breakers, Letter from R~ A. Uderitz (PSE&G) to D. G. Eisenhut (USNRC), May 31, 1983.
3.4 Letter from s. Varga (USNRC) to R. A. Uderitz (PSE&G), July 26, 1983.
3.5 WCAP 10426, Reliability Estimates of the UVTA's in Reactor Protection System Trip Breakers. (January 1984) 3.6 Franklin Research Center Review Operational verification Program for Westinghouse DB-50 Reactor Trip Breakers, Letter from E. A. Liden (PSE&G) to s. A. Varga (NRC) dated September 16, 1983.
4.0 BACKGROUND
- PSE&G committed to a test program to determine the life cycle and replacement interval for the UVTA's and to verify the adequacy of the maintenance and surveillance programs used on the DB-50 reactor trip breakers. Reference 3.3 identified the Westinghouse Breaker Test Program as the test program to fulfill the PSE&G commitment. The NRC requested that PSE&G respond to RTB/l_J_ _ ---*------ ---- ----,
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2 of 5 S-C-Rl20-CSE-287 Date: 11/21/84 issues raised by Franklin Research Center - NRC consultant in Reference 3.4. In addition this letter requested that PSE&G address the confidence interval, sources of bias, and factors that influence service life.
The Westinghouse test program comprised two separate phases.
Phase I of the testing utilized five UVTA 1 s. Four devices were actually tested. The fifth device was maintained as a control sample for comparison purposes at the completion of the test.
In Phase I A, two UVTA 1 s were cycled a total of 2500 times with periodic lubrication and inspection every 200 cycles. In addition, the Phase I A test included 600 operations utilizing the shunt trip attachment. The other two devices were subjected to 2500 UVTA cycles without periodic lubrication, during Phase I B.
In Phase I A, one UVTA test sample performed without failure to trip the total test run of 2500 UVTA and 600 shunt trip cycles.
The other UVTA, after the 200 cycle lubrication and inspection, exhibited several intermittent misoperations. Physical and visual examination indicated that the lubricant had not properly carried into the intended points on the UVTA. Both UVTA's were removed from the test breakers thoroughly lubricated and the test was continued utilizing a similar lubrication procedure throughout the rest of the test. Both devices performed for the remainder of the test without failure.
The two test samples from Phase I A and the control sample were then disassembled and subjected to a metallurgical examination to establish the significance of the service wear on the performance of the UVTA during service life. The wear at three different locations on the attachments was determined to be the most significant. These locations were: (1) the push rod to pin joint, (2) the bottom surface of the latch where it makes contact with the flat leaf spring and (3) the leading edge of the guide notch of the latch where it makes impact sliding contact with the latch pin. An additional wear scar was identified during this examination and was part of the basis for instituting Phase II testing.
In Phase I B one test sample performed its trip function for 571 cycles before it failed to latch and the second test sample performed its trip function for 1700 cycles before it malfunctioned.
Phase II of the testing was conducted to evaluate a design modification that would capture the joint pin and to evaluate a new lubricant application technique. The design modification prevents the lateral pin motion which was identified during the metallurgical examination in Phase I A.
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3 of 5 S-C-Rl20-CSE-287 Date: 11/21/84 Phase II testing was similar to Phase I testing which included inspection and lubrication every 200 cycles for two UVTA's, (Phase II A) and only initial lubrication and inspection on two UVTA's (Phase II B). During Phase II A, both UVTA test devices performed 2500 UVTA and 600 shunt trips without malfunction.
During Phase II B, one device performed 2500 UVTA cycles without trip malfunction while the other device performed appproximately 2390 cycles before it malfunctioned. The metallurgical examination of these devices indicated similar wear patterns as those found during Phase I with the exception of the casing wear which was removed by the captive pin modification. As a result of the Phase II testing, it was determined that the captive pin modification did not adversely affect UVTA performance and that proper device lubrication could be conducted with the UVTA installed on the breaker.
In addition to the testing, Westinghouse performed a statistical evaluation of actual plant operating history covering the use of the UVTA in DB-50 reactor trip switchgear applications for the Westinghouse Owners Group. This study included 26 operating plants, some of which performed maintenance on the breakers and some which have not performed maintenance. The total UVTA population cycles were 9984 operations and of these operations 19 failures were reported. Based upon this data we estimate the reliability to be .9981.
5.0 DISCUSSION PSE&G is confident that the testing performed provides valid data with respect to the installed reactor trip breakers at the Salem Generating Stations. The Phase II A testing described above tested approximately 12.5% of a typical UVTA production batch (16 UVTAs) utilizing identical lubrication procedures and intervals actually used by PSE&G. The samples tested were selected from a manufacturing program which requires 100%
dimensional inspection of ten critical parts and a post assembly acceptance test of twenty-five successful operations at the manufacturing facility. This manufacturing program is in accordance with the PSE&G purchasing specification for the UVTAs. In addition the main breakers at both Salem Units will be or have been replaced with new breakers similar to those tested.
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S-C-Rl20-CSE-287 Date: 11/21/84 ea 4 of 5 In Reference 3.6, one of the Franklin Research Center's comments was that each time the breaker is operated from any source (UVTA, shunt trip, or manual trip) the UVTA is either partially or fully cycled and should be counted as a UVTA cycle. During Phase II A testing, each breaker was subjected to 2500 UVTA operations and 600 shunt trip operations without failure for a total of 3100 breaker operations. From IEEE Standard 352-1975 (Reference 3.2), a binomial distribution is the distribution of the number of successes in 11 n 11 independent Bernoulli trials in which the probability of success at each trial is P. The estimate of the parameter P is;
/\o p = number of successes total number of trials Since there were zero (0) failures during Phase II testing one (1) failure will be assumed in order to calculate a meaningful value of the parameter P, and therefore
/"-
p = 6199 6200, assuming (1) failure
/\.
p = .9998387 Also from Reference 3.2 an approximate confidence interval for P is given by
~+ c~ (1~1~ ~ (1~;1 2 2 Z d/2 P < -; + Z1- <>'f2 Where z cl.( 2 = -1. 96 Zl- o{/2 ~ +l. 96 n = 6200 trials From the above, the estimated confidence interval on P is
.9995226 < P < 1.0; at a 95% confidence interval It should be noted here that the calculated reliability from Phase II A test data also supports the plant evaluation study performed by the Westinghouse Owners Group.
The present replacement interval used by PSE&G for the UVTA is each refueling outage. This interval corresponds to a conservative 400 breaker cycles for an 18 mon~h refueling RTB/l 4 EDD-7 FORM 1 REV 0 10SEPT81
5 of 5 S-C-Rl20-CSE-287 Date: 11/21/84 cycle. The Westinghouse test program tested the UVTA to twice the Westinghouse service life of 1250 cycles. PSE&G chooses to continue the present replacement interval of each refueling outage. With this information, the reliability or the probability of zero (0) failures in "N" trials is given in Reference 3.2 as Rn = pn Rn = (.9998387)400 Rn = .9375125 Also, since the reactor trip breakers are redundant components the reliability or the probability of zero (O) failures to drop the control rods utilizing the 400 cycle replacement interval is
.9960953.
6.0 CONCLUSION
When lubricated and maintained every 200 breaker operations in a similar manner to that used in the Westinghouse Phase II A testing program, the DB-50 reactor trip breaker will exhibit an approximate reliability of .9998387. The 95% confidence interval for this reliability value indicates that the actual reliability is somewhere between .9995226 and 1.0. PSE&G chooses to replace the UVTAs at each refueling outage which will equate to approximately a 400 cycle service life, which is much more conservative than the manufacturer's recommended replacement interval of 1250. The resultant reliability of zero (0) failures during any 400 cycle life is .9375125. Since the reactor trip breakers are redundant, the reliability of the reactor trip breakers to drop the control rods into the reactor with zero (0) failures during the UVTA service life at Salem will be .9960953.
PSE&G has also modified the reactor trip circuit by installing an auto shunt trip feature. The auto shunt trip feature operates the shunt trip attachment on the main reactor trip breakers whenever a solid state protection system trip signal is generated or the console manual reactor trip switches are operated. With this design feature both the UVT and shunt tripping devices are actuated simultaneously whenever a reactor trip is demanded. The above testing described actuated only one of the two tripping devices with each trial, therefore the above reliability values are minimum reliability values since breaker operation is no longer dependent upon the successful operation of just one of the tripping devices.
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