ML18051A879

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Advises That Mod Will Be Made to Render Sump Pumps Inoperative Upon Receipt of Containment Isolation Signal, Per NUREG-0737,Item III.D.1.1, Integrity of Sys Outside Containment. Operating Procedures Will Be Revised
ML18051A879
Person / Time
Site: Palisades Entergy icon.png
Issue date: 04/30/1984
From: Johnson B
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To: Crutchfield D
Office of Nuclear Reactor Regulation
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-3.D.1.1, TASK-TM NUDOCS 8405030148
Download: ML18051A879 (2)


Text

consumers Power company General Offices: 1945 West Parnall Raad, Jackson, Ml 49201 * {517) 1aa~0550 April 30, 1984 Dennis M Crutchfield, Chief Operating Reactor Branch No 5 Nuclear Reactor Regulation US Nuclear Regulatory Commission Washington, DC 20555 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - NUREG-0737 ITEM III.D.1.1 -

INTEGRITY OF SYSTEMS OUTSIDE CONTAINMENT In response to NUREG-0737 Item III.D.1.1 "Integrity of Systems Outside Containment Likely to Contain Radioactive Material For PWRs and BWRs,"

Consumers Power Company implemented a program designed to reduce leakage from systems outside of containment to as-low-as practicai levels. Letters were submitted to the NRC dated December 27, 1979; March 4, 1980 and December 19, 1980 describing these programs.

A request for a change to the Palisades Plant Technical Specifications was submitted to the NRC on November 12, 1981.

The change request provided a preventative maintenance program to reduce leakage in systems outside containment.

Also, the current Palisades Technical Specifications (Section 6.15 "Systems Integrity) provide administrative control of the program.

Another phase of the leakage reduction program dealt with several modifications designed to prevent the unnecessary contamination of certain systems.

The Engineered Safeguards Room sump pump discharge lines were modified and operating procedures were developed to allow the safe return of the sump pump discharge back into containment.

After successful implementa-tion of the leakage reduction program, it is now considered undesirable to return sump pump effluents back into containment, which would require the re-opening of the containment isolation valves.

Therefore, a modification will be made to render the sump pumps inoperative upon receipt of a

! 8405030148 840430

PDR ADOCK 05000255 P

PDR OC0384-0010AA-NL02

DMCrutchfield, Chief Palisades Plant NUREG-0737 ITEM III.D.1.1 April 30, 1984 2

containment isolation signal.

Consequently, any system leakage will be retained in the Engineered Safeguards Room sump well and will not be introduced into the normal liquid radwaste processing systems.

Consumers Power Company will revise the appropriate operating procedures to reflect these changes.

Brian D Johnson Staff Licensing Engineer CC Administrator, Region III, USNRC NRC Resident Inspector - Palisades OC0384-0010AA-NL02