ML18045A396
| ML18045A396 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 07/16/1980 |
| From: | Fobes R CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | |
| Shared Package | |
| ML18045A395 | List: |
| References | |
| PAL-80-07-NC38, PAL-80-7-NC38, NUDOCS 8007290616 | |
| Download: ML18045A396 (3) | |
Text
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F~~No PIO. 2.1
-1.
. I~cnt No:
PAL~80~07-NC38
- NPDES NONCmlPI.T ANCE. NOTIFICATION Possible Noncompliance With Daily Avcrag~/Maximum Li~icati6ri Jury 16,. 1980 Plant:
Palisades Outfall
Description:
Turbine Sump Oil Separator Waste (OOG)
Parameter:. :Oil and Grease
- 1.
Date of Incident:
7/3/80 Through 7/7/80 Permit No:
MI-0001457~
Outfa.11 No:
800218 Parameter No:
00556
- 2.
Identification of specific* effluent limitation exceeded:
.Oil arid grease daily maximum limitation of 20 mg/l and monthly average limitation of 15 mg/l.
3;. Description of Incident:.
See
- a.ttached.
- 4.. Apparerit.c.-1use:
\\'
See attached.
/
'5. If not. immediately corrected, the anticipated time.the conditio'n is expected to continue:
NA.*.
- 6.
Corrective Action. - The following corrective act.ion was taken or will be taken to. r*educe, eliminate and prevent recurrence:*
see attached.
- . 7.
Additional Comments:
NA.
- *. 8.
Signed:. R L Fobes
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- 3.
pcs.crJption rlf NnncompU.L111c.e.:ind On July 2, 1980 nt 1700 hour0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />.s, a welded scam on the Gcnerntor Seal Oil Strainer. bun:;t result fog in n major loss of oil to the turbine buil_ding *floor.
Due to the. Hydrogen concentrati~n in the generator
. at that titile, the oil system could not be shutdown until the unit was.shutdown and thoroughly purged with carbon dioxide~
The Hydrogen con~e:ntration was less than 3% at 2200 hou_rs on 7 /2/80 and _the oil
- system ~as shutdown*nt that time.
During this five hour period,*
approximately 10,000 gallons of lubricating oii was spilt onto.the floor*.
. The. 'immediate :action taken by members of the plant staff, Operations, Mai~tenance, a~d Chemistry was to:
- 1) build dams(t1sing clay based oil* absorba~t) to prevent. oil from getting. into floor dra1ns '* 2) using
.. 50 cubic foot waste liner. tanks and availab_le pumps,. the majority of the o~i was collected and is being stored on site awaiting shipment for re-processing, and 3) expedite getting Hydrogen *off.themachin~ and re..;
J>laccd ~ith carbon ~ioxide.~. These actions were extremely ef fect~.ve in minimizing the ahi.oui1t of oil which reached the floor drains **.
- The maximum amount of oil whi~h reached* the Turb.ine Sump Separator* Tank
- (T 41) was about 80-gallon~.
Follow-up actions taken after the incident were as follows:
- 1)
On Thursday, July 3, 1980, Stoddard & Sons of Hayland.was called in to remove the accumulated oi.l in tl:le T.urbinc Sump_ Separator Tank (T41) *
- 2) *** The.T 41 discharge sampling.proera:m was increased to a daily sam!Jle.
to.accurately monitor.~hc*discharge.
- 3)
A passive* oil* remov~*l filter was placed in the s'torm dniln into which
- T 111 dr.riins.pr:ior to release into* the~ disch::irgc.* mixinr, basi.n.. This filt~r did remove.<)bot'1t l!;. -
2 liters of oil from the bnsin during.
a 3. dny pcr:i.oCi.
- 11_
- 6.
.. li)
Clc:nn up of the oil and the abtrnrb.'.int used to contain the oil-
. throur.hout. the area of the turbine building affected by the spJll.
- 5)
The strainer. wns repaired by rc~1clding the seam *..
- 6). closer attention is being paid to the oil interceptor and oily
- . waste emulsion breaker to continue. to clean up any.residual oil not already clcariccl up.
The results of the sampling program for the.first.5 days following the incidents are listed in Table l.
Date*
'7/3/80 7/4/80 7/5/80 7/6/80 7 /7 /80 mg/1 Oil
.320.*
. 46.4
. 81.5 15.3*
83.9..
Table 1 Volume of Waste Water 41,300
. 31,500.
23,700 9,200
_9,200.
- Calculated Oil
- Discha:rged (Gal. )
i3.2 1.47.
1.93
- O. l,4
. 0~77.
As can be seen,. less than *two tenths of one percent of th~, oil lost from
. the sy~temwas actually rcileasecl.to *the lake~ During.the entire period, there* was* no. perceptible.. oil. in the mixing basin or in any part. of Lake.
Michigan discharge.
The samples analyzcd*thus far*ind::lcate that we are in-violation of our 20 rng/l.daily lindt for four of the days following :the incident and the magnitude of these values is such that we will be in violal:io1i of our
. 15 mg/1 monthly aver:age also.. The act.ions taken by the pli_l.nt during this iridcjcnt should result in the oil discharge being less th.:in the.maximum allowable for. the majorit)'.of the month rem<iining *.
Corrective Actio~
The.:icti.ons t.:iken hy pl~tn~ pcrs()mw.l as st*1tci;i ahovc were adequate to
- .* 111inin;i~;l' th('. i~1p*1ct. or this spill'. No* lOll!', term corrective.-ictions..:ir~
. Jllim111*cl. dur~ to the, low prob:1ld li.ty of rC'occur-rcnce* of this type of event.