ML18033B669

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Insp Repts 50-259/91-07,50-260/91-07 & 50-296/91-07 on 910222-0313.Violations Noted.Major Areas Inspected: Reload Design,Shift Coverage Activities & Conditions Which Led to Load Chamber Spiking & Alarm Conditions
ML18033B669
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 03/26/1991
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18033B667 List:
References
50-259-91-07, 50-259-91-7, 50-260-91-07, 50-260-91-7, 50-296-91-07, 50-296-91-7, NUDOCS 9104230088
Download: ML18033B669 (17)


See also: IR 05000259/1991007

Text

UNITED STATES

NUCLEAR REGULATORY COIVIMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-259/91-07,

50-260/91-07,

and 50-296/91-07

Licensee:'Tennessee

Yalley Authority

6N 38A Lookout Place

1101 Market Street.

Chattanooga,

TN

37402-2801,

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection at Browns Ferry Site near

Decatur,

Alabama

Inspection

Conduc

d:

Fe r

r

22 - March 13,

1991

Inspector:

enior

es

ent

nspector

E. Christnot, Resident

Inspector

W. Bearden,

Resident

Inspector

K. Ivey-, Resident

Inspector

G. Humphrey, Resident

Inspector

P.

rnett,

Rea

r Inspec

r

Approved by:

Pau

el

In

e

rog

m,

TYA Projects Division

te

sgne

Date Signed

SUMMARY

Scope:

This

special

inspection

included

those

activities

associated

with the

February

21,

1991

through

March 6,

1991

Fuel

Loading.

Those activities

included

a review of reload design,

on shift coverage activities

and

a review

of the conditions that led to the beginning of fuel load

and loading of one

fuel

assembly

into the Unit 2 reactor core with a fuel load chamber spiking to

alarm conditions.

Results:

One refueling violation was identified for failure to follow the refueling

procedure,

paragraph

two.

Indications of

a fuel

load

chamber

causing

alarm

conditions

due to noise were available prior to commencing fuel load and during

movement of the 'first fuel assembly into the reactor vessel.

Fuel loading was

not stopped until after the first fuel assembly

wa's seated

into its designated

core position.

The

B Fuel

Load Chamber

was

then declared

inoperable

and fuel

loading

stopped

for approximately

50 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br />

during maintenance

and eventually

replacement of th~

R

I=

1 Load Chamber.

~lo"~3

soooas9

PDR

ADOCN, 050

Q

0

0

1

The, Plant Operations

Review Committee

review of this event contained

several

discrepancies.

The

sequence

of events

was different .from control

log entries

and resident

inspector observations.

After the initial problem with the

8 Fuel

Load Chamber the'emainder

of the

refueling

was

completed

in

a

professional

and

conservative

manner.

Fuel

loading was completed

on March 6,

1991 at 9:49 p.m.

A review of the Reload Licensing Report, reconstitution

program summaries,

and

the

Revised

Reload Technical Specification

by regionally based

inspectors

did

not result in any concerns

with operating Unit 2 with reconstituted

fuels.

o

10

REPORT

DETAILS

Persons

Contacted

Licensee

Employees:

  • 0. Zeringue, Site Director

L. Myers, Plant Manager

  • M. Herrell, Operations

Manager

J. Rupert, Project Engineer,

R. Johnson,

Modifications Manager

  • N. Bajestani,

Technical

Support Manager

R. Jones,

Operations

Superintendent

A. Sorrell, Maintenance

Manager

G. Turner, Site guality Assurance

Manager

  • P. Carier, Site Licensing Manager
  • P. Salas,

Compliance Supervisor

J.'orey,

Site Radiological

Control Manager

R. Tuttle, Site Security Manager

T. Beu,

BWR Fuel Engineering

Other

licensee

employees

or

- contractors

contacted

i'ncluded

licensed

reactor

operators,

auxiliary

operators,

craftsmen,

technicians,

and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel

  • C. Patterson,

Senior Resident

Inspector

  • E. Christnot,

Resident

Inspector

  • W. Bearden,

Resident

Inspector

  • Y.. Ivey, Resident

Inspector

G. Humphrey,

Resident

Inspector

P. Burnett, Reactor Inspector

M. McCoy,

NRR/SRXB

T. Ross,

NRR/PD2-4

  • Attended exit interview

Acronyms

and initialisms

used

throughout this report are listed in the

last paragraph.

Sequence

of Events for Fuel

Load

After an extended

shutdown of over six years

in duration,

Unit

2 fuel

loading

commenced at 6:39 a.m.

(CST)

on February 21,

1991.

The reactor .nuclear

instrumentation

included four

SRM channels

to provide

neutron monitoring during fuel loading.

Two of the

SRM channels,

A and

B,

were electrically wired, using temporary cabling, to FLCs.

The

FLCs were

placed

in the core in the

same

quadrants,

respectively,

as

SRM

C and

D.

The

two channels

wi~ed

to the

FLCs

were

considered

operable

by the

licensee.

SRMs

can

be declared

operable

when they indicate greater

than

3 cps.

The

SRM channels

attached

to FLCs were reading

100 cps

on channel

8

and

250

cps .on channel

A.

The following events

were

observed,

all

times are approximate

CST.

a.

4:00

p.m.

Wednesday,

February

20,

1991,

two inspectors

attended

a

PORC meeting

chaired

by the Plant Manager.

A')so present

were the

Site Director

and

the Vice President

Nuclear

Operations.

The

PORC

decided that adequate

systems

were operable

to support fuel loading.

The

RPS shorting links for the

SRMs would be in the non-coincident

logic pattern.

In this configuration

a single Hi-Hi Set Point Trip

from the

SRMs would cause

a full scram.

b.

2:00 a.m. Thursday,

February

21,

1991.

Hi-8i Set Point Trip from SRM

8 and erratic operation

was

observed

by

a RI.

This

was discussed

with the licensee.

An entry in the operator's

log at 2:50

a.m'.

indicated that

WR

CO 42091

was initiated to troubleshoot

and repair

SRM 8 as

necessary.

The

WR was closed out with no root causes

being

identi fied.

c.

6:30 a.m. Thursday,

February

21,

1991.

An entry in the operators

log

indicated

that 2-SOI-100-1,

Fuel

Load Prerequisites

Checklist,

was

completed;

the prerequisites

for 2-G01-100-3,

Refueling Operations,

were completed;

and that permission

had

been received

from the Plant

Manager to load fuel into the Unit 2 reactor vessel.

d.

6;39 a.m.

Thursday,

February

21,

1991.

Permission

was given to the

refueling bridge

personnel

to

commence

loading fuel

and the bridge

reported

the commencing of step

1 of the fuel loading procedure.

e.

g.

6:41

a.m.

Thursday,

February

21,

1991.

The refueling

bridge

personnel

reported that the fuel bundle

was clear of the spent fuel

pool.

The control

room operator

reported

to the

SOS that

SRM 8 was

spiking.

The control

room RI observed

that the

SRH

8 cps meter

was

ramping

up from a reading of approximately

100 cps to 500 cps.

6:43 a.m.

Thursday,

February

21,

1991.

Refueling bridge personnel

reported

that

the fuel

bundle

was

stopped

at the cattle

chute to

await the completion of a radiation control survey of the drywell.

The control

room

RI observed

that

the

SRM

8 cps

meter

was still

reading

approximately

500 cps

and the period meter

was erratic.

The

control

room

RI discussed

this with licensee

personnel

and

was

informed that this

was

not considered

a

problem

because

both

SRHs

were not receiving electronic noise.

The control

room RI noted that

the operator

had

informed the

SOS that the

SRM

A count rate

was

steady.

7:05 a.m.

Thursday

February

21,

1991.

Fuel

loading

resumed.

The

control

room

RI noted that the

SRH

8 cps meter

had returned

to

an

indication of approximately

100 cps prior to resuming fuel movement.

The operator reported,to

the

SOS,

and the control

room RI observed,

a

Hi-Hi Trip on the

SRM

B channel.

The

SOS

ordered

the refueling

bridge personnel

to stop moving fuel .

The .control

r oom RI observed

a discussion

among

control

room licensee

personnel

as

to whether

a full scram

should

have

been

received,

and whether

the shorting

links were in the coincidence

or non-coincidence

logic pattern.

The

SOS

asked

the refueling bridge

personnel

where the fuel bundle

was

located.

The refueling

bridge

personnel

replied that

the fuel

bundle

was approximately

2 feet from the top of the grid.

h.

7: 10 a.m.

Thursday February 21,

1991.

The

SOS informed the refueling

bridge personnel

and all control

room personnel

that he

was directing

the refueling bridge personnel

to install the bundle into the reactor

vessel

using the jogging mode.

7:21

a.m.

Thursday,

February

21,

1991.

The

refueling

bridge

personnel

reported that the. bundle

was in the vessel

and upgrappled.

During this eleven

minute time frame

the control

room

RI observed

that the

SRM

B cps meter

was indicating between

approximately

800 to

1000 cps,

SRM Channel

A was

steady,

and

SRM

B period

meter

was,

erratic.

j.

7:23 a.m. Thursday,

February 21,

1991.

The operator reported

and the

control

room RI observed

another

SRN

B Ki-Hi trip.

The 'control

room

RI observed that the

SRN

B cps meter

was indicating approximately

800

to

1000 cps,

the

SRM

A was

steady

and

the

SRN

B period meter

was

erratic.

k.

7:24

a.m.

Thursday,

February

21,

1991.

The

SOS

declared

SRM

B

inoperable

and stopped all fuel movement.

Both the

RO and

SRO logged

this

time

as

when the

B

FLC was declared

inoperable

and refueling

stopped.

The

inspector

concluded

that the refueling

procedure

was

not followed.

Technical Specification 6.8. 1. 1 requires

that written procedures

shall

be

established,

implemented,

and

maintained

covering

the

applicable

procedures

in Appendix

A of Regulatory

Guide 1.33, Revision 2,

February'978.

Appendix

A of Regulatory, Guide

1.33

includes

procedures

for

refueling.

Refueling Operations

Procedure,

2-GOI-100-3,

implements this requirement

for refueling.

Procedure

step

3. 1,

under

Precautions

and Limitations,.

require that refueling shall

be

immediately halted

upon occurrence

of

unexplained'r

abnormal

increase

in

SRMs or

FLCs readings

(procedure

step

3. 1. 1),

or loss

of neutron

monitoring with less

than

two

SRNs/FLCs

operable

and responding

wi,th one in the fuel handling quadrant

and

one in

an adjacent

quadrant

(procedure

step.3. 1.3).

The inspector

concluded that

a violation of TS

had occurred.

Refueling

was

not

stopped

after

questionable

and erratic

response

of the

B

FLC.

This

is identified

as

VIO 260/91-07-01,

Failure to

Follow Refueling

Procedure.

The '8'LC was

again declared

inoperable

due to spiking on February 27,

1991,and

remained

inoperable for the remainder of the fuel loading.

When

the spiking occurred this time, the bundle being moved

was returned to the

spent fuel pool.

The licensee

is conducting

an incident investigation of

these

problems

which will be reviewed

by 'the resident inspectors.

The

remainder

of fuel

loading

was carried

out in

a professional

and

conservative

manner.

Fuel

loading

was

completed

at

9:49

p.m.,

on

March 6,

1991.

3.

PORC Review Discrepancies

The

inspector

reviewed

an

event

description

of

B

FLC

problem

on

February 21,

1991.

The description

was

approved

by

PORC

on February.23,

1991,

and

a copy was given to the inspector.

This

PORC was chaired

by the

Plant Operations

Manager.

Numerous

discrepancies

and inaccuracies

were

noted

as follows:

The licensee's

events

and causal

factor ch'art stated

a high alarm was

received at 2:50 a.m.

The inspector

reviewed the

SRO 'log and the entry at 2:50 a.m.

was for

a high-high alarm and not

a high alarm.

The control

room RI stated

that at approximately this time he observed

the operators

resetting

a

Hi Hi Trip on the

SRM

B channel

because

a clear, distinct

Red Light

was

on.

When the

RI discussed

this observation with the licensee

he

was

informed that

a

SI

on the

FLC

was

in progress

and this

was

expected.

A later review by the control

room RI indicated that the

SI was

being performed

on an

FLC for the

A SRM and not the

B

SRM at

this time.

b.

C.

The licensee's

events

and causal

factor chart

and event description

narrative

stated

that

the

B

FLC was

determined

to be inoperable at

7: 18 a.m.

and before

a second

high-high alarm

was received

when the

bundle

was placed into the core.

The inspector

reviewed

both the

RO and

SRO log and the

B FLC was not

declared

inoperable until 7:24

a.m. after the bundle

was

placed in

the core

and after several

high-high alarms.

The inspector

in the

control

room also

heard

-the

announcement

that

the 'B'LC was

inoperable after the bundle

was released.

The assessment

of personnel

performance

concluded that the decision

to lower the

bundle into the core

was

made

in accordance

with Step

3.2 of 2-GOI-100-3

which requires

that if core alterations

are

suspended

for any

reason

other

than

a fire alarm

or

medical

emergency,

a fuel -bundle being

moved wi 11

be lowered

and placed in a

safe condition immediately.

,

The inspector

noted that lowering

a fuel bundle into,,the core meets

the, definition of a core alteration

and Step 3.2 is not applicable.

d.

The actions

to

be taken to preclude future occurrences

stated

that

changes

were

being

made to 2-GOI-100-3

and 2-TI-147A to include

a

precaution

that if erratic

or unexplained

SRM/FLC

response

is

obsess ved, fuel, loading shall

be immediately stopped.

The

inspector

reviewed

2-GOI-100-3

procedure

Step

3. 1.1

and

the

precaution already existed in the procedure.

In general,

the inspector

concluded that the

PORC

assessment

contained

several

discrepancies.

The

assessment

did not critically assess

operations,

actions,

or troubleshooting of the

MR written.

The assessment

did

not

adequately

assess

the significance

of proceeding

with fuel

handling after

a high-high alarm was received

and

an expected

scram signal

was not received.

Although later it was

learned

from GE that spiking can

result in an alarm without

a scram signal,

the

PORC did not specifically

conclude that this event

was the

phenomenon

described

by GE.

4.

Related Matters

a.

Shift Turnover During Movement of First Fuel Assembly

Refueling

began

during shift turnover of operations

personnel.

The

Plant Operations

Manager

was present

in the control

room during this

time, of the

movement 'of the first bundle into the vessel.

The

oncoming shift relieved the watch during movement of the first fuel

assembly.

The inspector

concluded that during

a major evolution was

not the best time to conduct shift relief.

In .addition, the oncoming

crew

may not have

been fully aware of the spiking problem

on the

B

FLC.

b.

Noise Problem

Known Related to Bridge Movement Prior to Fuel

Load

Planners

who process

WRs were aware of the

FLC spiking problem

and

the relationship to bridge movement prior to beginning fuel movement.

An entry into the

planners

log at 5:00

a.m.

stated

"FLC

B spikes

appear

to be related to bridge work (Ops says they will buy it off)".

Evidently, this

information

was

not fully communicated

to all

management.

co

System

Engineer

Not Notified

During this

event,

the

system

engineer

was

not notified of the

spiking problem.

In the past,

the involvement of the system engineer

in problem resolution

has

been effective.

5.

Fuel Handling Problems at Other Sites

An inspector

reviewed

events

involving failures of the fuel

handling

bridge at other nuclear

plants

to determine if they could

be potential

problems for BFN.

The inspector discussed

these

events with the cognizant

system engineer

and the

SRO responsible for refuel floor activities.

The

events

and the

BFN actions

are addressed

below:

a,

At another facility in early

January,

1991,

a fuel

bundle

was

released

from the main hoist grapple while it was being lowered into

the core

when the refuel bridge electrical

power was lost.

The loss

of power to the bridge

removed

the air from the grapple

and

the

grapple

opened.

The grapple is designed

to remain closed

upon

a loss

of air, but the

licensee

discovered

that the grapple air lines

had

been reversed

during previous work.

At BFN the refuel grapple is designed to.fail in the closed position.

Procedure

EPI-0-079-CRAOOl,

Refueling

Platform

and

Jib, Crane

Inspection,

includes

a main grapple failsafe check.

This procedure

is conducted

within 30 days of fuel

movement.

The check includes

opening

the= grapple

and

removing

power to verify that the grapple

fails closed,

and using test weights to determine if the grapple will

open while in a loaded condition.

The licensee

stated

there

had been

no recent maintenance

on the grapple airlines or switch.

No problems

were identified during the performance

of the EPI prior to beginning

Unit 2 fuel load.

b.

At another facility the refuel bridge main hoist emergency

and motor

brakes failed while lowering

a bundle into the core.

This resulted

in the bundle being put into the core in an uncontrolled. manner.

At BFN the Unit 2 refuel bridge main grapple hoist

has

a double set

of brakes

which are the disc type.

An inspection'as

pe~formed

on

the brakes

and extensive

wear

was noted.

The brake

was

reassembled

using

a

new coil

and operating

assembly

and the original pressure

plate

and fiber brake disk.

In addition,

MMI-34, Refueling Platform

and

Grapple

Assembly

Inspection,

includes

inspection

of the

main

hoist grapple

and

EPI-0-079-CRA001

includes

checking the electrical

and mechanical

integrity of the brakes

using test weights.

Both of

these

procedures

are

performed within 30 days of fuel movement.

No

problems

were identified during the performance of these

inspections

prior to beginning Unit 2 fuel load.

The inspector

concluded that the licensee

had adequately

addressed

both of

these

events

prior to beginning

Unit

2 fuel

load.

No violations or

deviations

were identified in this area.

6.

Browns Ferry Unit 2, Cycle 6,

Fuel Selection

and Core Load (60710,

61702)

a.

References

(I)

TVA-BCD-906,

SUMMARY REPORT

FOR

THE

BROWNS

FERRY

NUCLEAR PLANT,

UNIT 2,

CYCLE 6,

INSPECTION

AND RECONSTITUTION

PROGRAM, August

1988 (Revision 0).

{2)

TVA-RLR-002,

BROWNS

FERRY

NUCLEAR

PLANT,

RELOAD

LICENSING

REPORT,

UNIT 2,

CYCLE 6.

(3)

USNRC,

REVISED

RELOAD TECHNICAL SPECIFICATIONS

(TS254)

BROWNS

FERRY NUCLEAR PLANT, UNIT 2, September

13,

1989.

b.

Introduction

Reconstitution of

BWR fuel

by replacing

damaged

or failed fuel pins

with pins of like initial enrichment;

similar exposure,

and similar

residual

enrichment

from a donor fuel'assembly

is not new.

Prior to

reconstituting

fuel

at

Browns

Ferry,

successful

reconstitution

programs

had

been

conducted

at least

three

other

BWR facilities.

However,

the

program

conducted

at

Browns Ferry

was

much larger in

the

number

of fuel

assemblies

and

fuel

pins

affected

than

the

earlier

programs.

Consequently,

when the

program

was

proposed,

NRR

initiated

a dialogue

and

exchange

of technical

documents

with TVA.

That exchange

culminated

in issuance

of new Technical Specifications

(Reference

a.(3)) with conservatively

reduced

'MAPLHGR limits for the

reconstituted

fuel.

TVA submitted

both Reference

a.(1)

and Reference a.(2) in support of

TS

amendment

172,

but

the

NRR review of the neutronic

analyses

presented

by TVA was limited to confirmation that approved

computer

codes

were used in the an'alyses.

The

analyses

described

in Reference

a.(1)

were

reviewed

in the

Region II office

and

discussed

by

Region II personnel

with the

responsible

TVA analyst.

The

Region II staff concluded that the

strategy

of using

the

codes

to confirm that replacement

pins

had

neutronic characteristics

similar to the replaced

pins

was

sound.

A

similar conclusion

was that the strategy for analyzing

the current

neutronic

characteristics

of

the

reconstituted

bundles

and

predicting, their future behavior

was also sound.

No concerns

or caveats

about operating

Browns Ferry Unit 2 with the

reconstituted

fuels

described

in Reference a.(I)

were identified.

It was also

noted that the

use of reconstituted

fuel

has

placed

no

special

or additional

surveillance

requirements

on

the facility

staff.

c.

Core, Design Predictions-

Calculations

for Cycle

6

show that

the

lead fuel

assembly will

produce

from 1.35 to 1.45 times the core

average

power at any point

in the cycle.

The relative

power

production for R2/R3 fuel will

. range

from 1.2 to 1.05 at any time in the cycle.

During parts of

the cycle,

the leading

R2/R3 bundle will be

a reconstituted

bundle,

but many of the reconstituted

bundles will operate at less

than core

average

power throughout the cycle.

The effects of the long shutdown

on fission product

and transuranic

isotope

concentrations

were

calculated

fo'r the

unreconstituted

core.

Bundle

power distributions

were essentially

unchanged.

At

BOC,

SDM increased

by approximately

0.5% dk/k, but that effect burned

out by mid-cycle.

These results

are consistent

with those

reported

for Sequoyah.

The

ana lyses did not identify a need for any special

core monitoring

as

a result of the fuel reconstitution.

Two conservatisms

were

intr'oduced

into

the

plant

computer

to

provide

conservative

monitoring of the reconstituted

fuel.

MAPLHGR curves

were lowered

3.2".

The R-factors

to be

used

in

CPR determination

were increased

by 0.02.

d.

Corrective Actions

Changes

in feedwater .chemistry

have

been instituted to prevent the

recurrence

of the

CILC observed

in

U2C5.

The

condensers

were

retubed

with stainless

steel

to eliminate

the copper

in the brass

tubes.

The system

has

undergone

considerable

flushing to eliminate

residual

copper.

'The method of precoating

the demineralizers

may be

changed

to

improve

copper

removal

by

the

demineralizers.

Previously,

the demineralizers

were ineffective in removing copper.

There will be

online monitoring of the

copper

content

in the

feedwater.

Plant activities to reduce 'CILC will be inspected

during

the

power ascension

phase of plant activities.

7.

Exit Interview

The inspection

scope

and findings were summarized

on March

15', 1991, with

other

persons

indicated in paragraph

1 above.

The inspectors

described

the areas

inspected

and discussed

in detail the inspection findings listed

below.

The licensee

did not identify as proprietary

any of the material

provided

to or

reviewed

by

the

inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

Item Number

Descri tion and Reference

259, 260; 296/91-07-01

VIO, Fai lu're to Follow Refueling

Procedures,

paragraph

2.

8.

Acronyms

and Initialisms

BOC

BFN

BWR

CFR-

CILC

CPR,

CPS

CST

EPI

FLC

FSAR

GOI

GE

MAPLHGP

NRC

PORC

RI

RO

RPS

SI

SOI

SOS

SDM

SRM

SRO

SRXB

TI

TS

TVA

VIO

WR

Beginning of Cycle

Browns Ferry Nuclear

Boiling Water Reactor

Code of Federal

Regulations

Crud Inducted Localized Corrosion

Critical Power Ratio

Counts

Per Second

Central

Standard

Time

Electrical Preventive Instruction

Fuel

Load Chamber

Final Safety Analysis Report

General

Operating Instruction

General

Electric

Maximum Average Planar

Heat Generation

Rate

Nuclear Regulatory

Commission

Plant Operations

Review Committee

Resident

Inspector

Reactor Operator

Reactor Protection

System

Surveillance

Instruction

Special

Operating Instruction

Shift Operations

Supervisor

Shutdown Margin

Source

Range Monitor

Senior Reactor Operator

Reactor

Systems

Branch,

NRR

Technical

Instruction

Technical Specification

Tennessee

Valley Authority,

Violation

Work Request

0'