ML18005A033

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Responds to NRC Re Violations Noted in Insp Rept 50-315/94-02 & 50-316/94-02.Corrective Action:Testing Was Performed to Verify Proper Operation,Required Stroke Length, & Required Pressure Valve
ML18005A033
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 05/06/1994
From: Fitzpatrick E
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: Martin J
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1212, NUDOCS 9405160073
Download: ML18005A033 (9)


Text

ACCELERATED DISTRIBUTION DEMONSTPA.TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

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SSION NBR:9405160073 DOC.DATE 94/05/06 NOTARIZED: YES DOCKET

'IL:50-315 Donald C.

Cook Nuclear Power Plant, Unit 1, Indiana M

05000315 50-316 Donald C.

Cook Nuclear Power Plant, Unit 2, Indiana M

05000316 AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.

Indiana Michigan Power Co.

(formerly Indiana

& Michigan Ele RECIP.NAME RECIPIENT AFFILIATION MARTIN,J.B.

Document Control Branch (Document Control Desk)

SUBJECT:

Responds to NRC 940406 ltr re violations noted in insp rept 50-315/94-02

& 50-316/94-02.Corrective action:testing was performed to verify proper operation, required stroke length,

& required pressure valve.

DISTRIBUTION CODE: IEOID COPIES RECEIVED:LTR J ENCL L SIZE:

TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES:

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RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/DEIB AEOD/DSP/TPAB DEDRO NRR/DRCH/HHFB NRR/DRSS/PEPB NRR/PMAS/ILPB2 D

REG FILE 02 ILE Ol EXTERNAL EG&G/BRYCEiJ

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NSIC COPIES LTTR ENCL 1

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RECIPIENT ID CODE/NAME HICKMAN,J AEOD/DSP/ROAB AEOD/TTC NRR/DORS/OEAB NRR/DRIL/RPEB NRR/PMAS/ILPB1 NUDOCS-ABSTRACT OGC/HDS2 RES/HFB NRC PDR COPIES LTTR ENCL 1

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D NOTE TO ALL"RIDS" RECIPIENTS:

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PLEASE HELP US TO REDUCE WASTETH CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAMEFROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 22 ENCL 22

Indiana Mmhigan Power Company P.O. Box 16631 Columbus, OH 43216 INSMbfA NICRIGAM POlhfM AEP: NRC: 1212 10 CFR 2.201 Donald C.

Cook Nuclear Plant Units 1 and 2

Docket Nos.

50-315 and 50-316 License Nos.

DPR-58 and DPR-74 NRC INSPECTION REPORTS NO. 50-315/94002 (DRP)

AND 50-316/94002 (DRP)

REPLY TO NOTICE OF VIOLATION U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.

C. 20555 Attn:

Mr. J.

B. Martin May 6, 1994

Dear Mr. Martin:

This letter is in response to a USNRC letter dated April 6, 1994, that forwarded a notice of violation to Indiana Michigan Power Company.

The notice of violation contained one violation identified during a routine safety inspection conducted by Messrs.

J. A. Isom, D. J. Hartland, C. N. Orsini, and G. D. Replogle from January 19 through March 11, 1994.

The violation is associated with procedural noncompliance and inappropriate procedure designation with regard to the maintenance of Unit 2 main steam stop valve dump valve 2-MRV-241 on February 21, 1994.

Our reply to the notice of violation is provided in the attachment to this letter.

An observation was also made in the notice of violation with regard to the I&C maintenance involvement in recent reactor trips, including the subject Unit 2 trip.

To address this comment, an evaluation of I&C involvement in trip events and trip event precursors since 1990 was conducted.

This study concluded that 1&C's overall performance has shown improvement and their involvement in trip events and trip event precursors has decreased over the past four years.

Nonetheless, we will continue to strive to improve I&C's performance.

In addition, overall plant performance on reactor trips has improved each year this decade, with only two trips occurring in 1993.

The reactor trip rate for 1993 meets the 1995 industry goal.

9405160073 940506 PDR ADaCK 05000315 9

PDR

Mr. J.

B. Martin 2

AEP:NRC:1212 This letter is submitted pursuant to 10 CFR 50.54(f) and, as such, an oath statement is attached.

Sincerely, ZF E. E. Fit p trick Vice President dr Attachments CC:

A. A. Blind G. Charnoff W. T. Russell, NRC - Washington, D.C.

NRC Resident Inspector NFEM Section Chief J. R. Padgett

STATE OF OHIO)

COUNTY OF FRANKLIN)

E.

E. Fitzpatrick, begin duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power

Company, that he has read the forgoing response to NRC INSPECTION REPORTS NO. 50-315/94002 (DRP)

AND 50-316/94002 (DRP),

REPLY TO NOTICE OF VIOLATION and knows the contents thereof; and that said contents are true to the best of his knowledge and belief.

Subscribed and sworn to before me this

~~~'ay of 19~/

NOT Y PUBLIC BIT.". D. HILL tIOTARY PUDI.IC. STATE OF OHIO

ATTACHMENT TO AEP:NRC: 1212 REPLY TO NOTICE OF VIOLATION

ATTACHMENT TO AEP 'NRC: 1212 Page 1

C

Background

A routine safety inspection was conducted by J.

A. Isom, D. J. Hartland, C. N. Orsini, and G.

D. Replogle from January 19 through March 11, 1994.

During this inspection, one item was found to be in violation.

The violation was identified as procedural noncompliance and inappropriate procedure designation with regard to the maintenance performed on Unit 2 on February 21,

1994, on main steam stop valve dump valve 2-MRV-241.

This violation was set forth in a letter containing the notice of violation, dated April 6,

1994, from Mr.

E.

G.

Greenman, Director, Division of Reactor Projects.

The letter was received April 11, 1994.

Our response to the notice of violation is contained within this document.

NRC Violation I "Criterion V of 10 CFR 50, Appendix B requires that activities affecting quality be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

Procedure No.

12 IHP 6030.IMP.030, Revision 5,

"Inspection Adjustment of Pneumatic/Spring Valve Actuators Associated Positioner

& Limit Switches,"

documents the requirements for reassembling pneumatic valve actuators, including valve 2-MRV-241

'lant Manager Instruction PMI-2010, Revision 23, "Instructions, Procedures and Associated Indexes Policy," Step 4.17.2, states that technical documents that are intended to be used by qualified individuals during the performance of an activity shall be designated in-hand as signified by double asterisks preceding the procedure number.

Procedure No. 12 IHP 6030.IHP.030 is a technical document intended to be used by qualified individuals during the performance of an activity.

Contrary to the above:

On February 21,

1994, maintenance work on main steam stop valve dump valve, 2-MRV-241, was not performed in accordance with procedure 12 IHP 6030.IMP.030, Revision 5, "Inspection &

Adjustment of Pneumatic/Spring Valve Actuators

& Associated Positioner

& Limit Switches", in that the proper stroke length was not achieved.

ATTACHMENT TO AEP:NRC:1212 Page 2

2.

Procedure 12 IHP 6030.IMP.030, Re~ision 5, was not developed in accordance with PMI-2010 in that the procedure was not designated In-Hand as signified by double asterisks preceding the procedure number.

This is a Severity Level IV violation (Supplement I)."

Response

to Violation l.

Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

2.

Reasons for the Violatio On February 21, 1994, corrective maintenance to repair leakby was performed on the Unit 2 main steam stop valve dump valve, 2-MRV-241.

As part of this maintenance activity, valve 2-MRV-241 was to be set up and stroked.

The set up and stroke set was performed without an in-hand procedure.

Plant Manager's Instruction, PMI-5020, "Corrective Maintenance" identifies the need to preplan work on safety-related equipment and to perform the work in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

Upon review of the above maintenance activity, it has been concluded that the work involved in setting the correct stroke for this valve is too complex to be performed without an in-hand procedure.

We failed to identify that inadequate instruction existed at the work site to perform the task in question.

3.

Corrective Actions Taken and Results Achieved Prior to unit startup, work activities were performed to correct the pre-load values of the valve.

The bench set, with the actuator uncoupled from the valve, was verified to be correct for the required stroke length.

The actuator was then properly coupled to the valve to achieve the required stroke length and pressure values.

Testing was performed to verify proper operation, required stroke

length, and required pressure values.

Procedure 12IHP6030.IMP.030 was enhanced and designated as an in-hand procedure.

ATTACHMENT TO AEP:NRC:1212 Page 3

4.

Corrective Actions Taken to Avoid Further Violations Maintenance will review the standards applicable to quality work, and re-evaluate their procedures currently designated as non-in-hand against these standards.

There are 30 of these procedures.

These 30 procedures will be

revised, enhanced to contain appropriate levels of detail, and redesignated as in-hand procedures or
canceled, as appropriate.

The maintenance screening process checklist, MA3.3-05, Attachment 5, was revised to clarify requirements for procedures at the work site.

Lessons learned from this event were shared with all other departments which perform maintenance work.

5.

Date Whe 11 Com liance Vil Be Achieved Maintenance administrative.

process MA3.3-05, Attachment 5

was revised April 27, 1994.

The "Lessons Learned" memo was issued May 6, 1994.

Procedure revisions and redesignation will be completed by July 1, 1994.

Full compliance was achieved on April 6,

1994, when procedure 12IHP6030.IMP.030 was revised and re-issued as an in-hand procedure.