ML17347B644

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Insp Repts 50-250/90-04 & 50-251/90-04 on 900127-0223. Violations Noted.Major Areas Inspected:Monthly Surveillance & Maint Observations,Esf Walkdowns,Operational Safety & Plant Events
ML17347B644
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 03/14/1990
From: Butcher R, Crlenjak R, Mcethinney T, Schnebli G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17347B642 List:
References
50-250-90-04, 50-250-90-4, 50-251-90-04, 50-251-90-4, NUDOCS 9004020132
Download: ML17347B644 (17)


See also: IR 05000250/1990004

Text

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UNITEDSTATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-250/90-04

and 50-251/90-04

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami, FL

33102

Docket Nos.:

50-250

and 50-251

Facility Name:

Turkey Point

3 and

4

License Nos.:

DPR-31

and

DPR-41

Inspection

Conduc

Inspectors

.

C.

8

Janua

7

199

through February

23,

Wz.

e ior

R sident Inspector

1990

3- 9'- 9'o

Date Signe

4

si

nt

nspector

~rZ-

ne

Resi

e

Inspector

G. A.

S

Approved by:

R.

V.. r

nja

,

Sec

on Chief

Division of Reactor Projects

Date Signed

9- 'p- 9o

ate

igne

Z i'/ Pd

ate

igned

SUMMARY

Scope:

This routine resident

inspector inspection entailed direct inspection at 'the

site in the areas

of monthly surveillance observations,

monthly maintenance

observations,

engineered

safety features

walkdowns, operational

safety,

and

plant events.

Results:

One violation, two NCVs and

one IFI were identified.

One strength

and

one

concern

were also noted.

50-250,251/90-04-01,

NCV - Failure to accomplish

post maintenance

testing

on a

containment

phase

A isolation valve to verify operability.

50-250,251/90-04-02,

Violation - Failure to follow procedure

4-OP-013 resulting

in the loss of instrument air to Unit 4.

50-250,251/90-04-03,

NCV - Failure to follow procedure

TP-594 resulting in the

detensioning

of reactor

vessel

head

studs

out of sequence.

50-250,251/90-04-04,

IFI - Followup licensee's

investigation of Unit 3

SFP

pump

shaft failure.

9LIOlII,I Oi ..2 9QQ3 $ 4

F'LIR

AEICICI; 0=I.IC>02..'D

C~

PDC

A strength

in control

room operation

was noted.

The prompt, decisive actions

by the control

room operators,

during

a loss of control air event, stabilized

the plant and mitigated the transient.

A concern

was noted in that the

SFP heat exchanger

room drain was partially

blocked

and under different c'ircumstances (i.e., longer time interval before

discovery)

a spill or leakage

inside the

SFP heat exchanger

room could have

propagated

into adjacent plant areas.

REPORT

DETAILS

Persons

Contacted

ensee

Employees

V. Abbatiello, guality Assurance

Supervisor

W Anderson, guality Assurance

Supervisor

Arias, Sr. Technical Assistant to'Plant

Manager

C. Balaquero,

Assistant Technical

Department Supervisor

W. Bladow, guality Assurance

Superintendent

E. Cross,

Plant Manager-Nuclear

J. Earl, guality Control Supervisor

A. Finn, Assistant Operations

Superintendent

J. Gianfrencesco,

Assistant Maintenance

Superintendent

T. Hale, Engineering Project Supervisor

N. Harris, Vice President

Hayes,

Instrumentation

and Controls Supervisor

Heisterman,

Assistant Superintendent

of Electrical Maintenance

A. Kaminskas,

Technical

Department

Super visor

A. Labarraque,

Senior Technical Advisor

Marsh, Reactor

Eng'ineering Supervisor

G. Mende, Operations

Supervisor

W. Pearce,

Operations

Superintendent

Powell, Regulatory

and Compliance Supervisor

Remington,

System

Performance

Supervisor

M. Smith, Service Manager-Nuclear

N. Steinke,

Chemistry Supervisor

C. Strong,

Mechanical

Department Supervisor

R. Timmons, Site Security Superintendent

S. -Warriner, equality Control Supervisor

B. Wayland, Maintenance

Superintendent

D. Webb, Assistant Superintendent

Planning

8 Scheduling

T. Zielonka, Engineering Supervisor

. Lic

T.

J.

J.

J.

  • L
  • J

R.

T.

R.

  • S
  • K.

E.

G.

  • V

J.

G.

R.

  • L
  • D

K.

G.

R.

J.

F.

  • G
  • M.

J.

A.

Other licensee

employees

contacted

included construction

craftsman,

engineers,

technicians,

operators,

mechanics,

and electricians.

  • Attended exit interview on February 23,

1990.

Note:

An Alphabetical Tabulation of acronyms

used in this report is

listed in paragraph

10.

Followup on Items of Noncompliance

(92702)

A review was conducted of the following noncompliance(s)

to assure

that

corrective actions

were adequately

implemented

and resulted

in conformance

with regulatory requirements.

Verification of corrective action was

achieved

through record reviews, observation

and discussions

with licensee

personnel.

Licensee

correspondence

was evaluated

to ensure

that the

responses

were timely and that corrective actions

were implemented within

the time periods specified in the reply.

0

e

(Closed) Violation 50-250,251/89-24-01.

Concerning

two examples

of failure

to follow procedures.

The licensee

responded

to this violation in letter

L-89-283, dated August 14,

1989.

The corrective actions required for this

violation were reviewed

by the inspectors

and found to be adequate.

This

item is closed.

3.

Onsite

Followup and In-Office Review of Written Reports of Non-routine

Events

and

10 CFR Part 21 Reviews

(90712/90713/92700)

The Licensee

Event Reports

and/or

10 CFR Part 21 Reports

discussed

below

were reviewed.

The inspectors verified that reporting requirements

had

been met, root cause

analysis

was performed, corrective actions

appeared

appropriate,

and generic applicability had

been considered.

Additionally,

the inspectors verified the licensee

had reviewed

each event, corrective

actions

were implemented, responsibility for corrective actions

not fully

completed

was clearly assigned,

safety questions

had

been evaluated

and

resolved,

and violations of regulations

or TS conditions

had

been

identified.

When applicable,

the criteria of 10 CFR 2, Appendix C, were

applied.

(Closed)

LER 50-251/88-01.

Technical Specification limits exceeded for

safety

system settings

due to non-conservative

acceptance

criteria in plant

procedures.

This issue

was discussed

in detail in IR 50-250,251/88-02

and

was identified as

an

NCV due to licensee initiative for self-identification

and prompt resolution.

This item is closed.

(Closed)

LER 50-250/88-13.

Functional test of Post Accident Hydrogen

Monitor did not test alarm function due to personnel

error.

The corrective

actions specified in this

LER were reviewed

and found to be adequate.

This

item. is closed.

(Closed)

LER 50-250/88-17.

Control

Room Ventilation System

Out of Service

in Excess of TS Time Limit due to Intermittent Circuit Failure.

This item

was also tracked via URI 50-250,251/88-18-02

which was discussed

and closed

out in IR 50-250,251/89-34.

This item is closed.

(Closed)

LER 50-250/88-23.

Plugged

Valves in Steam Generator

Blowdown

Sample

System Results

in No Sample

Flow to Process

Radiation Monitor R-19.

This item was also tracked via IFI 50-250,251/88-30-04,

which was discussed

and closed out in IR 50-250,251/89-40.

This item is closed.

(Closed)

P2188-07.

Morrison - Knudsen notification that

EMD Model 999,

excitation system for EMD emergency

diesel

generators,

have potential for

field breaker trip due to combined air temperature

and field amps.

The

licensee

has determined that Turkey Point diesel

generators utilize Model

2553 excitation system in lieu of the Model

999 systems

addressed

in the

10 CFR 21 report.

This information was confirmed by Morrison - Knudsen

Company, Inc., letter dated

November 23,

1988.

No further action is

required.

0

4.

Monthly Surveillance Observations

(61726)

The inspectors

observed

TS required surveillance testing

and verified:

The test procedure

conformed to the requirements

of TS; testing

was

performed in accordance

with adequate

procedures;

test instrumentation

was

calibrated; limiting conditions for operation

were met; test results

met

acceptance

criteria requirements

and were reviewed

by personnel

other than

the individual directing the test; deficiencies

were identified,

as

appropriate;

and were properly reviewed

and resolved

by management

personnel;

and system restoration

was adequate.

For completed tests,

the

inspectors verified testing frequencies

were met and tests

were performed

by qualified individuals.

The inspectors

witnessed/reviewed

portions of the following test

activities:

s.

4-OSP-075.

1

AFW Train

1 Operability Verification

'-0SP-075.6

AFW Train

1 Backup Nitrogen Test

0-OSP-075. 11

AFW Inservice Test

No violations or deviations

were identified in the areas

inspected.

Monthly Maintenance

Observations

(62703)

Station maintenance activities of safety related

systems

and components

were observed

and reviewed to ascertain

they were conducted

in accordance

with approved

procedures,

regulatory guides,

industry codes

and standards,

and.in conformance with TS.

The following items were considered

during this review,

as appropriate:

LCOs were met while components

or systems

were

removed from service';

approvals

were obtained prior to initiating work; activities were

accomplished

using approved

procedures

and were inspected

as applicable;

procedures

used

were adequate

to control the activity; troubleshooting

activities were controlled

and repair records

accurately reflected the

maintenance

performed; functional testing and/or calibrations

were

performed prior to returning components

or systems

to service;

gC records

were maintained; activities were accomplished

by qualified personnel;

parts

and materials

used

were properly certified; radiological controls

were properly implemented;

gC hold points were established

and observed

where required; fire prevention controls were implemented;

outside

contractor force activities were controlled in accordance

with the

approved

gA program;

and housekeeping

was actively pursued.

The inspectors

witnessed/reviewed

portions of the following maintenance

activities in progress:

Repair of 81 Blackstart Diesel

Fuel Oil Tank Leak.

Repair

and Replacement

of k'5 Blackstart Diesel

Cracked Cylinder

Liner.

Diesel

Driven Fire

Pump

18 Month Inspection.

Replacement

of 3B Boric Acid Transfer

Pump Seal.

At 8:30 a.m.,

on January

19,

1990, with Unit 3 in Mode

1 at 100

percent

power, the Nuclear Watch Engineer discovered that

post-maintenance

testing

had not been

performed after adjusting

the valve stem -packing

on Phase

A containment isolation valve

CV-3-6275B (Steam Generator

B blowdown).

The adjustment of

valve stem packing is maintenance

that could affect valve

performance

parameters.

TS 3.3.3 requires

Phase

A containment

isolation valves'to

be operable

in Modes

1 through 4.

With a

Phase

A containment isolation valve inoperable,

compensatory

measures

must

be taken within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> to avoid

a unit shutdown

required

by TS 3.3.3.

Valve stem packing adjustments

were

made

to CV-3-62758 at approximately -9:00 a.m.

on January

18,

1990.

Failure to perform .concurrent

post-maintenance

testing

on

CV-3-6275B during valve stem packing adjustments

was

due to

error by non-licensed utility personnel.

Neither the Nuclear

Plant Operator or Control

Room personnel

were notified that

valve packing adjustments

were being

made

on valve CV-3-6275B.

A sign

on the valve required that Control

Room personnel

be

notified prior to performing maintenance

on the valve but this

did not occur.

At approximately 9:10

a.m.,

on January

19,

1990,

CV-3-6275B was satisfactorily tested

and demonstrated

to

be operable.

The licensee

took prompt corrective actions for

this event which included the following:

(1)

Mechanical

Maintenance

Personnel

involved in this

event were counseled

on their responsibilities for:

Strict adherence

to work instructions

contained in

PWO

packages;

ensuring satisfactory

completion of

post-maintenance

testing;

and complying with caution

signs

posted

on, or adjacent to, equipment

being

worked.

(2)

The checklist

used

by Maintenance

Department

PWO work

planners

was revised.

PWOs involving TS Limiting

Conditions for. Operation will contain

a step requiring

a Foreman or Field Supervisor to verify that the job

task is under

a clearance

order or that

an individual

from the Operations

Department is present.

This licensee identified violation is not being cited because

the criteria specified in Section

V.G. 1 of the

NRC Enforce-

ment Policy were met.

This item will be tracked

as

NCV 50-250,251/90-04-01.

6.

Operational

Safety Verification (71707)

The inspectors

observed control

room operations,

reviewed applicable logs,

conducted

discussions

with control

room 'operators,

observed shift

turnovers

and confirmed operability of instrumentation.

The inspectors

verified the operability of selected

emergency

systems,

verified

maintenance

work orders

had

been submitted

as required

and followup and

prioritization of work was accomplished.

The inspectors

reviewed tagout

records, verified compliance with TS

LCOs and verified the return to

service of affected

components.

By observation

and direct interviews, verification was

made that the

physical security plan was being implemented.

Plant housekeeping/cleanliness

conditions

and implementation of

radiological controls were observed.

Tours of the intake structure,

diesel, auxiliary, control

and turbine

buildings were conducted to observe plant equipment conditions including

potential fire hazards, fluid leaks,

and excessive

vibrations.

The inspectors

walked

down accessible

portions of the following safety

related

systems

to verify operability and proper valve/switch alignment:

A and

B

EDGs

Control

Room Vertical Panels

and Safeguards

Racks

ICW Structure

4160 Volt Buses

and 480 Volt Load and

HCCs

Unit 3 and

4 Feedwater

Platforms

Unit 3 and

4 Condensate

Storage

Tank Area

AFW Area

Unit 3 and

4 Hain Steam Platforms

Auxiliary Building

No violations or deviations

were ide'ntified in the areas

inspected.

7.

Plant Events

(93702)

The following plant events

were reviewed to determine facility status

and

the

need for further followup action.

Plant parameters

were evaluated

during transient

response.

The significance of the event

was evaluated

along with the performance of the appropriate

safety

systems

and the

actions

taken

by the licensee.

The inspectors verified that required

notifications wer e made to the

NRC.

Evaluations

were performed relative

to the

need for additional

NRC response

to the event.

Additionally, the

following issues

were examined,

as appropriate:

Details regarding

the

cause

of the event;

event chronology; safety

system performance;

licensee

compliance with approved

procedures;

radiological

consequences, if any;

and proposed corrective actions.

On January

28,

1990, at 3:25 p.m., the Control

Room received

a fire alarm

at an alarm point (Fire Zone 79A-North/South Auxiliary Building Breezeway).

In addition to the alarm, the deluge

system in the breezeway

actuated.

Operations

personnel

searched

the breezeway

and all adjacent

areas finding

no signs of fire.

The system

was then isolated.

The. licensee

performed

a

root cause

analysis

and determined that manual

push button actuation

was

considered

as the most likely root cause.

This was

based

on the results

found after testing the alarm circuit and detectors,

satisfactorily

verifying the pull station

was not actuated

and the deluge valve was reset

with no problems indicated.

Although the push button is designed with a

barrier to prevent actuation

by accidental

contact (i.e.

bumping into),

depressing

the button (i.e. fingers,

pen, screwdriver) maliciously is not

prevented.

Activity in the .area at the time of actuation

was low and

no

witnesses

could be located.

When operations

personnel

arrived

on the scene,

they found nothing unusual.

Based

on an additional licensee

review, the

likely root cause of the deluge

system actuation

was the actuation of

the manual

push button located in the front of the local alarm panel.

The

licensee will implement corrective actions to minimize or prevent the

problem.

These include installing

a nameplate

near the manual

pushbutton

on every alarm panel of this type to caution against the inadvertent

actuation of the deluge

system

and revising the general

employee training

to caution personnel

against inadvertently operating

any fire protection

related

equipment.

On February 4,

1990, with Unit 4 at

100% power, the instrument air supply

pressure

decreased

causing

the feedwater regulating valves to begin

to close.

To stabilize

steam generator

levels,

the

PSN directed

the

RCO

to runback the turbine to match

steam flow with feed flow.

The load was

reduced

approximately

200

MWE before the instrument air pressure

was

returned to normal.

Investigation of the event revealed

the instrument

air supply to Unit 4 was isolated

by a

SNPO.

The Unit 4 air receiver

was

isolat'ed

by clearance

4-90-02-008, therefore,

Unit 3 instrument air was

cross-tied

to Unit 4 by opening the cross-tie isolation valves 3-40-IAS-012

and 4-40-IAS-012.

The

SNPO was instructed to return the Unit 4 instrument

air dryer to service using 4-0P-013,

Instrument Air System,

dated

December

15,

1989, Section 7.5,

and also to lift clearance

4-90-02-008.

Section

7.5, Step

14, directed the

SNPO to close 4-40-IAS-012.

Because

the

clearance

was not released,

the Unit 4 instrument air supply was still

isolated.

Therefore,

when the

SNPO performed step

1'4, the Unit 3

instrument air supply to Unit 4 was isolated.

The

SNPO noticed the air

pressure

decrease

and re-opened

the valve, 4-40-IAS-012, to restore

pressure.

The licensee attributed this event to

a combination of the

following factors:

(1) improper releasing

order of the clearance;

(2)

no job briefing; (3) operator

assumed

that 4-OP-013 would properly line up

system

and the prerequisites

were satisfied.

The

PSN discussed

the event

with the personnel

involved and the licensee initiated corrective actions

including ensuring job briefings are held for complex evolutions

and also

e

ensuring

SRO reviews releasing

order

on clearances.

The failure to verify

the prerequisites

contained

in 4-OP-013 constitutes

a violation of TS 6.8. 1.

This item will be tracked

as Violation 50-250,251/90-04-02.

The

inspectors

noted

a strength in control

room. operations

by personnel

on

shift.

The prompt, decisive actions, stabilized the plant and mitigated

the transient.

On February

12,

1990, while performing step 6.3. 17. 12 of TP-594, three

reactor vessel

head studs,'0,

39 and 58, were detensioned

instead of just

stud

58 as specified

by the procedure.

The licensee

recently obtained

a

new stud tensioning

system from Kleiber

& Schulz,

Inc.

The tensioning

system is manufactured

by Klockner - Becorit of West Germany.

Because

this outage

was the first time the licensee

was to use the

new detension-

ing system,

Kleiber

& Schulz technicians

were

on site to facilitate head

stud detensioning.

Although the tensioning

equipment

had

been tested

on

a

test block and

had

been found to be functioning properly,

when the

tensioning

system

was installed

on the first three studs,

minor adjust-

ments

were necessary.

The technician

was called in to trouble shoot

and

make necessary

adjustments.

TP-594,

step 6.3. 17. 12, states,

in the first.

sequence

for detensioning,

only nut 58 has to be turned

as

shown

on

attachment

6.

Step 6.3. 17. 12 states,

after tensioning,

using the nut

turning device, turn nuts to angle

shown

on attachment.6.

Attachment 6,

sequence

1, requires turning the nut rotating device only for stud 58.

It

also stated that studs

20 and

39 are loosened

in sequence

20.

While

making the final 'checkout of the stud detensioning

system,

the Kleiber

&

Schulz,

Inc. technician correctly tensioned

studs

20,

39 and

58 and then

rotated

the nuts- for all three studs

45 degrees

counter clockwise.

Licensee

and Westinghouse

representatives

were present,

at tHe top of the

refueling cavity, but were unaware that the technician

was actually

detensioni ng the studs.

When the technician stated that his checkout

was

completed,

and the stud detensioning

system functioned 'correctly, it was

determined that the procedure

was not followed.

The licensee

stopped

the

job and wrote

NCR 90-0054, describing

the non-conformance.

Westinghouse

performed

an Engineering evaluation

and

recommended

retorquing studs

20

and 39.

A final Westinghouse

evaluation

regarding

the effects of the

above actions

on the integrity of the vessel

flange will be evaluated

by

the licensee prior to entering

Mode 4 following the refueling outage.

Also, Westinghouse

representatives

are to be present

when technical

representatives

are trouble shooting equipment.

Failure to follow

procedure

TP-594, is

a violation of TS 6.8. 1.

However, this licensee

identified violation is not being cited because

the criteria specified in

Section

V.G. 1, of the

NRC Enforcement Policy were satisfied.

This item

will be tracked

as

NCV 50-250,251/90-04-03.

.On February

14,

1990, with Unit 3 in Mode 6, the NIS count rate increased

causing

the Migh Flux at Shutdown annunciator

to alarm and the containment

evacuation

alarm to actuate.

The

RCO followed ONOP-046. 1 and initiated

emergency

boration.

The Unit 3 containment

was evacuated

and the cause of

the increased

count rate

was investigated..

The licensee

found that

SRNI (N-31) spiked high and operated erratically as indicated

on the

ERDADS trend.

The licensee

switched to the spare detector

and declared

0

e.

9.

N-31 back ih service.

Personnel

were allowed to re-enter

containment

after the increased

count rate proved to be invalid.

The licensee

plans

to further troubleshoot

the suspect

detector to identify a failure mode.

On February 20,

1990, with Unit 3 in Mode 6, while removing fuel from the

reactor to the

SFP,

a leak from the operating

SFP cooling water

pump (3B)

was noted at 11:20 a.m.

Approximately

3 inches of water had accumulated

.

in the

SFP heat exchanger

room and cask

wash area.

The

NO entered

the

SFP

heat exchanger

room to isolate the failed pump.

Another

NO entered

the

room within twenty minutes to align the

3A SFP cooling water

pump.

Both

workers were slightly contaminated. 'hey returned to work, later that

day, after standard

decontamination

procedures.

The licensee

determined

approximately

2000 gallons of borated water leaked

from the

pump shaft

mechanical

seal.

The

pump shaft was subsequently

found to be sheared.

All of the water was contained within the

SFP heat exchanger

room and the

cask

wash area with no rele'ase

to the environment.

However, the floor

drain system did not work properly.

The resident inspectors

expressed

conc'em to licensee

management

that although tested

and found satisfactory

on January

25,

1990, the

SFP heat exchanger

room drains

were partially

blocked and,

under different circumstances,

this condition could have

resulted in a spill outside the

SFP heat exchanger

room.

The licensee

formed

ERT 90-04 to investigate this event.

The inspectors will followup

on the licensee's

root cause

evaluation

and corrective actions.

This item

will be tracked

as IFI 50-250,251/90-04-04.

Licensee guality Assurance

Program

Implementation

(35502)

An internal office evaluation

was conducted

on February

13,

1990, of the

licensee's

quality assurance

program implementation

by reviewing recent

inspection reports,

SALP reports,

open items, licensee corrective actions

for NRC inspection findings,

and licensee

event reports.

Particular

emphasis

was placed

on all

new items or findings since the last

SALP report

period (July 31, 1989).

During this evaluation, it was'ecognized

that

team inspections

in the area of Design Validation, Appendix R,

RG 1.97,

and

EOPs

were conducted.

Based

on the licensee's

current performance

and the

results of this evaluation,

no recommendations

were

made to increase

the

inspection effort at Turkey Point.

Exit Interview (30703)

The inspection

scope

and findings were

summarized

during management

interviews held throughout the reporting period with the Plant Manager-

Nuclear

and selected

members of his staff.

An exit meeting

was conducted

on February

23,

1990.

The areas

requiring management

attention

were

reviewed.

No proprietary information was provided to the inspectors

during the reporting period.

The inspectors

had the following findings:

50-250,251/90-04-01,

NCV - Failure to accomplish

post maintenance

testing

on

a containment

phase

A isolation valve to verify

operability.

(paragraph

5)

v

1

~

'