ML17347A567
| ML17347A567 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 06/15/1987 |
| From: | Reyes L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17347A565 | List: |
| References | |
| 50-250-87-22, 50-251-87-22, NUDOCS 8706250245 | |
| Download: ML17347A567 (3) | |
Text
ENCLOSURE 1
NOTICE OF VIOLATION Florida Power and Light Company Turkey Point Units 3 and 4
Docket Nos.
50-250 and 50-251 License Nos.
DPR-31 and DPR-41 During the Nuclear Regulatory Commission (NRC) inspection conducted on April 27 - May 18,
- 1987, a violation of NRC requirements was identified.
The violation involved the failure to properly implement administrative procedures.
In accordance with "General Statement of Policy and Procedure for NRC Enforce-ment Action," 10 CFR Part 2, Appendix C (1986), the violation is listed below:
Technical Specification 6.8.1 requires that written procedures and administrative policies shall be established, implemented and maintained that meet or exceed the requirements of sections 5.1 and 5.3 of ANSI N18.7-1972 and Appendix A of USNRC Regulatory Guide 1.33.
ANSI N18.7-1972, section 5.1.5, specifies that procedures shall be provided for control of equipment, as necessary, to maintain reactor and personnel safety and to avoid unauthorized operation of equipment.
Section 5.1.2 of ANSI N18.7-1972 specifies that procedures shall be followed.
Administrative Procedure (AP) 0103.4, entitled In-Plant Equipment Clearance
- Orders, revision dated March 10,
- 1987, specifies in section 5.4.1 that it is the responsibility of the clearance executor to follow the clearance tag-out and/or 'tag removal in the order given. If any step cannot be executed exactly in the order given, he shall request clarifica-tion from the originator of the order before proceeding.
Contrary to the above, on May 7, 1987, while restoring from maintenance on the 3D 480 volt load center, clearance order release instructions were not executed in the order given on clearance 87-5-XI-131.
As a result, a
protection logic actuation stripped the 3B 4160 volt bus and the B
Emergency Diesel Generator (EDG) started and auto-connected to the 3B bus.
Subsequent automatic loading of the 3D load center caused the B
EDG to be connected without synchronization to offsite power through the 3A 4160 volt bus.
This is is a Severity Level IV violation (Supplement I).
Pursuant to the provisions of 10 CFR 2.201, Florida Power and Light Company is I
hereby required to submit to this Office within 30 days of the date of the letter transmitting this Notice a written statement or explanation in reply including:
(1) admission or denial of the violation, (2) the reason for the 8706250245 870625 PDR ADOCK 05000250 8
Florida Power and Light Company
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Turkey Point Units 3 and 4
)
2 Docket Nos. 50-250 and 50-251 License Nos.
DPR-31 and DPR-41 violation if admitted, (3) the corrective steps which have been taken and the results
- achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved.
Where good cause is shown, consideration will be given to extending the response time.
FOR THE NUCLEAR REGULATORY COMMISSION PgGW, ]~Le P ALS)G~ED BV V)RGlLL. BRO Luis A. Reyes, Director Division of Reactor Projects Dated at Atlanta, Georgia this 15th day of June 1987