ML17345A689
| ML17345A689 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 05/05/1989 |
| From: | Gloersen W, Marston R, Potter J, Shortridge R, Testa E NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17345A688 | List: |
| References | |
| 50-250-89-14, 50-251-89-14, NUDOCS 8905250274 | |
| Download: ML17345A689 (35) | |
See also: IR 05000250/1989014
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
%"i ~
l%5)'NCLOSURE
2
Report Nos.:
50-250/89-14
and 50-251/89-14
Licensee:
Florida Power and Light Company
9250 West Flagler Street
Miami, FL
33102
Docket Nos.:
50-250
and 50-251
Facility Name:
Turkey Poirt
3 and.4
Inspection
Conducted:
March 20-24,
1989
irspecters:
.. g.
(s
r7
E.
D. Testa,
Team Leader
(
/.
g
g
- oersen
cm (').S'.
R.
R. Marston
License Nos.:
and
55
Da e
igned
(.
r r'j
bate
igneo
c-,>>
/('a
e Signed
1-
S
R.
B. Shortri
ce
Approved by:
. Potter,
C
1e
Facilities Radiation Protection Section
Emergency
Preparedness
and Radiological
Protection
Branch
Division of Radiation Safety
and Safeguards
Dat
sglIcd
> SJ'y
Si gne
SUMMARY
Scope
This was
a special,
announced
assessment
in the area of the licensee's
program
to maintain occupational
radiation
exposures
as
low as'. reasonably
achievable
(ALARA).
Results
The licensee
has in place
II'any of the elements
o,
an effective
ALARA program.
Plogram
strengths
noted
during
the
assessment
included
good general
worker
knowledge
ard
awareness
of
ALARA concepts
and responsibilities,
holding
department
mansaaement
accountable fcr achieving
exposure
goals,
innovative use
p'OO~s ac'('I~y4
Pop
pj,
C
85'O~~s J g
Q
~
(+~<OLIO xrosO
PDI,'
of personnel
(ALARA Zone Coordinators) for dose reduction,
and self-identified
improvements
for the
ALARA program.
However,
several
weaknesses
were also
identified in the
program that should
be addressed
to ensure
that collective
annual
personnel
radiation
dose
is
reduced
to the
maximum extent possible.
.These
weaknesses
were in the areas
of:
Lack of health
physics
(HP) involvement in maintenance
department
mock-up training,
lack of design-related
ALARA training for design
engineers,
and
minimal retraining
or requalification
program for
returning
HP technicians
(Paragraph
5.a, 5.b,
and 5.c).
Large
percentage
of the radiation control
area
(RCA) maintained
as
contaminated
(Paragraph
3.b).
Poor worl
coordinaticr,
and
low man-hour
estimates
resulting in low
dose projections
(Paragraph
6.d).
Post-job
ALARA review only conducted for jobs with a collective dose
exceeding
50 person-rem
(Paragraph
6.a).
Lack
of formalization
of the
ALARA Zone
Coordinator
concept
(Paragraph
4.a).
Lack of full attendance
at the
ALARA Coordinating
Committee meetings
(Paragraph
4,b).
Limitation of
the
suogestion
program
for
ALARA improvements
(Paragraph 8.a(3)).
Discrepancies
in correlation
of pocket
ion
chamber
(PIC)
and
thermoluminscent
dosimeter
(TLD) measurements
(Paragraph
6.c).
Within the area
inspected,
no violations or deviations
were identified.
REPORT
DETA1LS
Persons
Contacted
Licensee
Employees
+0. Bates, Jr., Assistant
to, Health Physicist
- W. Brown, Project Construction Supervisor
- S. Chappelle,
OA Engineer
T, Coleman,
Health Physics
ALARA Supervisor
D. Cooper,
ALARA Shift Supervisor
0. Cross,
Plant Manager
- 8. Danek,
Corporate
Health Physicist
- R. Earl,
gC Supervisor
- T. Finn, Training Superintendent
- S, Franzone,
Lead Engineer - TPNS
v. Gianfrancesco,
Maintenance
Superintendent
- S. Hale, Engineering Proiect
Vianager
D. Hall, Corporate
ALARA Coordinator
- R. Hart, Regulation
and Compliance Supervisor
- II. Jimenez,
Acting Health Physics
Supervisor
C. Kelly, Naintenance
Specialist Training Program
- E. Lyons, Compliance
Engineer
- H. Hercer,
Health Physicist,
St. Lucie
G. Nadden,
Principal
Engineer,
Nuclear Licens'ing
- J.
Odom, Site Vice President
- K. Payne,
ALARA Supervisor,
St. Lucie
- L. Pearce,
Operations
Superintendent
H. Powell, Planning
and Scheduling Coordinator
Yi. Stantori,
JC Department
Supervisor
Supervisor
Other
licensee
employees
contacted
during this
inspection
included
engineers,
maintenance
mechanics,
technicians,
and
administrative
personnel.
"Attended exit interview
Background
(83528/83728)
Turkey Point Onits
3 and
4 went into commercial
operation in December
1973
and
September
1974,
respectively.
Between
1975
and
1988,
the
annual
. collective radiation
dose at Turkey Point
exceeded
the national
average
for Pressurized
Water Reactors
(PWRs) for 13 of the last
15 years.
From
1974 through 1986, Turkey Point ranked fifth in the nation in PWRs with an
average
cumulative plant exposure of 685 person-rem
per year.
Key contributors
to the higher than
average
annual
dose
over the years
included:
(1) excessive
steam
generator
maintenance
and
subsequent
replacement:
(2) addition of unplanned
work resulting in increased
outage
work scope,
(3) large percentages
of dose accumulated
by contractors,
and
(4) out of core
source, term
and
associated
high
dose
rates
from the
Resistance
Thermocouple
Detector
In 1985,
the licensee
created
a
Man-Rem Quality Inspection
Team
(MR-QIT)
to develop
and implement
dose reduction measures.
To date,
the MR-QIT and
increased
management
support for the
ALARA program
have
been
primary
factors
in reducino
annual
collective
dose
from the
600 person-rem
per
unit range to 335 person-rem
per unit in 1988.
Table
1
shows
a comparison
of Turkey Point
annual
collective
dose with
that of the
average
anrual
dose
per reactor for all
PWRs in the United
States.
TABLE
1
Comparison of Turkey Point per Reactor
Dose With Average
Collective per Reactor
Dose
From Commercial
Year
1974
1975
1976
1977
197S
1979
1980
1981
1982
1983
1984
1985
1986
1987
1988
PWR Averaoe
Dose
Per Reactor
331
318
460
396
429
516
578
652
570
592
552
416
390
371
346
Turkey Point Dose
Per
Reactor
(Rem)
227
438
592
518
516
840
826
1,126
1,060
1,341
628
627
473
685
335
Performance
In discussions
with inspectors,
licensee
representatives
stated
that in
the past,
unplanned
or emergent
work, contractor
dose,
and steam generator
maintenance
and replacement
had
been contributors to the station's
annual
collective
dose
exceedino
the national
average for PWRs.
The following
sections
discuss
these
and
other
factors
which
have
affected
the
collective dose.
a.
The
inspectors
reviewed
NUREG/CR-425<,
Occupational
Dose
Reduction
and
ALAPA at Nuclear
Power Plants:
Study
on High-Dose i~obs,
Radwaste
Handling,
and
ALARA Incentives,
dated
April 1985,
with licensee
personnel.
contains
data
on
dose. experienced
throuohout
the industry for typical high dose jobs.
The inspectors
compared
the licensee's
dose
history for several
jobs with those
listed in the
NUREG as indicated in Table 2.
Table
2
Comparison of the Turkey Point Dose
For
High Dose Jobs
(Person-Rem)
Mith Averages Listed in NUREG/CR 4254
Job
83
84
85
86
87
88
NUREG/CR-
4254
Ava.
Hanger,
535
216
116
89
95
11
Anchor Bolt Inspection/
Repair
110
Eddy Current Testino
Reactor
Assembly/
Disassembly
In Service Inspection
Plant Decontamination
Primary Valve
Naintenance
and Repair
Insulation
Removal
Replacement
44
22
23
24
19
59
107
64
66
60
135
59
84
57
81
136
60
30
67
54
29
71
52
36
24
25
26
38
38
51
37
16
50,
48
46
45
30
18
Reactor
Coolant
Pump Seal
Replacement
12
6
3
8
6
20
17
Nanway Removal/
Replacement
Instrumentation
Repair
and
Calibration
6
6
--
7
19
6
31
41
22
16
12
Job
83
84
85
86
87
88
NUREG/CR-
4254
Ava,
Secondary
Side
And Repair
Fuel Shuffle/
Sipping And
Inspections
Operations-
Survei llance,
Routines
and Valve
Lineups
10
9
6
7
8
35
8
10
10
18
20
11
19
13
Cavity
Decontamination
3
4
3
6
Pressurizer
Valve
Inspection, Testing,
and Repair
11
11
7
40
24
Radwaste
System
Repair, Operation,
And Maintenance
6
32
23
18
17
10
Residual
Heat
Removal
System
Repair
And
Maintenance
3
10
10
7
17
The inspectors
noted that, for most jobs
reviewed,
the licensee's
dose
performance
per job
was
higher
than the industry
average
indicated
in
( 1974-1984 data)
~
b.
Control of Contaminated
Areas
The
inspectors
reviewed
the
licensee's
program for controlling
contamination
in the
RCA of the plant.
For the years
1987
and 1988,
the licensee
had the highest
percentage
of contaminated
area
versus
RCA in comparison
to the
other plants
in Region II.
In 1987,
34 percent (/) of the
RCA was contaminated.
- In January of 1988,
33%,
or 22,985
square
feet (ft~) of the
RCA was contaminated.
This was
reduced to 11,239 ft'r 16'~ of the
RCA in June.
However,
due to the
Unit 4 refueling outage,
the contaminated
square
footage
in'creased
to
29'y
December
1988,
The licensee
has estiblished
a
1989 goal of
104
contaminated
square
foctage.
The
large
percentage
of
contaminated
RCA was identified as
a weakness.
c.
Dose Reducti on Initiatives
During
discussions
on
dose
reduction
initiatives,
licensee
representatives
stated
that
the Unit 4 refueling
outage
was their
first experience
with holding vendors
accountable
for their dose
by
contract.
A major Nuclear
Steam Supply System Yendor, with previous
plant specific experience,
was contracted
to perform
a fixed scope of
refueling related work.
The vendor established
that it would require
more
than
120 person-rem
to perform the
work outlined.
In accord
with the
proaram
to maintain collective
dose
ALARA, the licensee
reviewed
the
jobs
involved
and
estimated
the
work
could
be
accomplished
for 72 person-rem.
The vendor
was able to complete the
work within the
amount
contracted
and
earned
an
incentive
by
completing the job at
65 person-rem.
The inspection
team indicated
that this
was
a positive
means
to help reduce
maintenance
dose
and
was indicative of an innovative
means
to cont'rol
dose
4.
Organization
(83528/83728)
a.
ALARA Staff
The licensee
ALARA organization
consisted
of a staff of eight
Zone
Coordinators
(AZCs)
reporting
through
two
ALARA Shift
Supervisors
to the
ALARA Supervisor.
An
ALARA Technician
and
a
Shielding Technician
also reported directly to the
ALARA Supervisor.
Licensee
representatives
stated
that
the
ALARA Organization
was
a
temporary
group that reported
to the NR-/IT and that
a proposal
was
before the
ALARA Comnittee to establish
the
ALARA Organization
as
a
permanent
group.
(1)
Staff Responsibilities
The
ALARA Shift Supervisor
was
responsible
for reviewing the
performance
of the
AZCs, attending
pre-job planning meetings,
and maintainino
an awareness
of the dose status of all radiation
work permits
(RWPs).
The Shielding Technician
was responsible
for interfacing with engineering
and crafts to ensure
prompt and
proper
documentation
of
surveys
to
show
the
shielding
effectiveness.
The
ALARA Technician
was
responsible
for
maintaining job histories,
generating
a weekly dose/work report
on man-hours
and
dose
expended
on each
RWP,
and development
of
the
annual
dose
report,
The
AZCs
were
responsible
for
overseeing
coordination
of all
work taking
place
in their
respective
zones with the priority of reducing
dose at the job
site.
(2)
ALARA Zone Coordinators
Licensee
representatives
stated
that the work performed
by the
AZCs has
been
a positive force in reducing collective person-rem
at the station.
The
AZC concept
was
a result of initiatives by
the
MR-/IT to
reduce
collective
dose
by direct
job site
surveillance
of
personnel
experienced
in
techniques/methods.
The licensee
stated
that they considered
the
49% reduction
in collective
dose
from 1987 to
1988 to be
largely the effort of the
AZCs,
ALARA group,
and acceptance
of
the
ALARA program at the station.
Eight
HP technicians
were
assigned
as
AZCs for the Unit 4
refueling
outage
in September
1988.
Four
were assigned
to day
shift and four
AZCs provided coverage for the night shift.
The
ALARA group
and
AZCs were temporarily established
to support the
outage
and report directly to the MR-(IT.
All data collected
by
the
ACZs are in a job history report format and are input weekly
to the MR-/IT.
The inspection
team reviewed the
ACZ concept in
detail
and
evaluated
the
reports
they
generated.
The
AZC
reports outlined their participation in mock up taining, pre-job
planning
and
post
job
interviews,
as
well
as
job
critiques/reports. for specific jobs.
Based
on the inspection
team's
review of AZC reports,
the team determined that the
AZCs
were
able
to
document
in detail
that
8% of dose
accumulated
during
the
outage
was
unnecessary.
The
information
was
transmitted
to the MP-(IT on 'a weekly basis
to be evaluated
at
the
end of the refueling
outage.
The inspectors
noted that,
during
some
weeks,
unnecessary
dose
ranged
as
high
as
28K.
Through March IO, 1989,
51.5 of 631.9 collective dose
was proven
to
be the result of poor planning, job coordinating
personnel
errors,
or repetitive work.
During an interview with an AZC, an inspector inquired about the
acceptance
of the
AZC program
by plant workers.
The
AZC
indicated that, at first, the
AZCs were in a difficult position,
in that they were constantly critiquing jobs.
However, the
AZCs
have
been able to develop
a good working relationship with plant
workers
and this rapport
has
resulted
in the collective effort
to reduce plant dose,
Based
on interviews with licensee
personnel
and
a review of
data,
the inspection
team determined
that the work to date
by
the
AZCs appeared
to be
one of the most comprehensive
and best
documented efforts to reduce
dose in Region II.
The inspection
team
recommended
that the
ALARA group
and the
AZC concept
be
adopted
and
formalized
by incorporating their functions
and
responsibilities
into plant procedures.
The team also suggested
that
the
data
regarding
accumulation
of unnecessary
dose
be
analysed
during the outage rather
than waiting until the end of
the
outage.
This
should
allow the licensee
to incorporate
needed
changes
ano
recommendations
for job
improvement .in
a
timely manner
and
help
reduce
job site
dose
as well.
The
licensee
agreed
with
the
recommendation.
The
lack
of
formalization of the
AZC concept
was identified as
a weakness.
ALARA Coordinating
Committee
The
ALARA Coordinating
Committee
was
established
to appraise
the
effectiveness
of the
ALARA program,
review job exposure
records
and
related
audits,
review relevant
experience
at other plants,
and
review job task
data
for
ALARA planning.
The
group
included
representatives
from key station
departments.
Additional duties
included
dose accountability
and awareness,
planning
and scheduling
for outages,
and
the
review of repetitive
jobs
resulting
in
unnecessary
dose.
The inspector
reviewed the monthly meeting minutes
for 1986 through
1988,
and determined that overall attendance
at the
meetings
from June of 1987 to November
1988 was approximately
48%.
During 'this .time period,
key departments
such
as
operations
and
technical
support
did not attend
any
meetings.
Instrument
and
Control
(IKC) ard
maintenance
attended
only
14'A
and
28% of the
meetings
respectively.
The
inspectors
discussed
attendance
and
effectiveness
of the
ALARA Coordinating
Committee
with licensee
management
and
the
licensee
agreed
that
improvement
in attendance
should
increase
the committee's
effectiveness
and that this would be
addressed.
The poor attendar ce at the
ALARA Coordinating
Committee
was identified as
a weakness.
ALARA Suggestion
Program
In discussions
with licensee
representatives,
the inspectors
learned
that there
was
no formal program prior to 1989 for ALARA suggestions.
However,
in January
1989,
the licensee
implemented
a "Bright Ideas
Program" to elicit ideas for plant improvement from personnel
and to
generate
interest in,
and
awareness
of, ways to reduce
dose at the
station.
This prooram is coupled with incentives
but is only open to
licensee
personnel.
The inspectors
indicated that there
may
be
a
problem with the
program
because
"bright ideas"
associated
with
recommendations
for reducing
dose
are
not currently
scheduled
for
review by the
ALARA Review Board.
Licensee
representatives
agreed to
consider this potential
problem.
ALARA Review Board
The plant
ALARA Review Board was established
to provide guidelines to
implement
ALARA concepts
in all aspects
of facility construction
and
operation,
and
to provide radiation
protection
input to facility
design
and
operationa'1
planning.
The
group
was
comprised
of
managers,
supervisors,
and. technicians
from key station departments.
The inspectors
reviewed
the quarterly minutes
of the
ALARA Review
Board
meetings
from 1983
through
1988.
Based
on the
review of
meeting
minutes
and interviews with plant manager
and supervisors,
the inspectors
determined
that the
ALARA Review Board
was actively
involved in efforts to reduce
dose
at the station.
The minutes
reflected
good participation
by members
from key departments,
an
aggressive
approach
to investioating
and implementing
dose reduction
action items,
and
an active roll in pursuing
methods currently used
in the industry to reduce out of core =source
term.
5.
Training (83528/83728)
The inspectors
reviewed the licensee's
training program to determine
which
groups
of employees
received training in
ALARA policies
and practices
beyond what was given in basic
General
Employee Training (GET).
a ~
b.
Mock-up Training
The licensee
provided specific
ALARA training to individuals involved
with
steam
generator
maintenance
and
non-destructive
=testing
activities
and
individuals
involved
with
other
maintenance
activities.
It was apparent
to the inspectors
that the licensee
had
placed
a significant amount of emphasis
and resources
in the mock-up
training program for maintenance
personnel.
In addition to the steam
generator
mock-up for the
channel
head,
the licensee
had
a mock-up
training facility established
in the nuclear training center.
Some
of the
pump
and value mock-ups included:
pump seal;
connoseal
charging
pump; safety injection pump; residual
heat
removal
pump;
boric
acid
transfer
pump;
and
a
waste
gas
compressor.
Additionally, the
inspectors
reviewed
Lesson
Plan
Number
1302402,
Revision 0, dated
November 3,
1988, entitled "Refueling Activities,"
which was basically
a pre-outage
slide presentation.
The lesson
plan
covered
methods
to reduce
exposure
and discussed
A2C's function, use
of shielding,
and multi-badging.
During the review of the mock-up
training
program,
the inspectors
noted that
HP personnel
were not
involved with the mock-up training exercises.
Additionally, the use
of protective clothing
(PC)
and respirators
(when applicable)
have
not
been
used
to simulate
working conditions
during the training
sessions.
The licensee
had identified this weakness
in the mock-up
training
program
and
was
considering
using
personnel
and
PC/respirators
during future training sessions
to ensure realistic
job/training conditions.
The lack of
HP involvement in maintenance
department
mock-up training was identified as
a weakness.
Additional
ALARA Training
With regard to specific
ALARA training provided to other work groups,
the
inspectors
noted
that
the
design
engineering
group
was
not
provided with specific
ALARA training other than what was provided in
GET.
The inspectors
discussed
with licensee
representatives
the
benefits
from specific
ALARA training for the engineers,
especially
since
those
individuals are involved with plant
and
system
design-
change
reviews that ultimately could effect workers'oses.
The lack
of desion-related
ALARA training 'for design engineers
was identified
as
a weakness.
c.
Continuing
HP Training
The inspectors
also reviewed the licensee's
contractor
and continuing
HP training
programs.
The inspectors
observed
that there
was
no
retrainina
or requalification
program for returning
contract
technicians.
It should
be noted that this finding and the contractor
HP training
program
was
reviewed
during
the
maintenance
team
inspection
(Inspection
Report
No.
50-250,
251/88-32)
and
the
aforementioned
inspection report should
be referred to for a detailed
discussion.
With regard
to the continuing
HP training program,
the
inspectors
reviewed
O-ADl~i-360, "Radiation Protection
manual
Health
Physics
Training,"
dated
Parch
22,
1988.
Additionally,
the
inspectors
reviewed
the continuing health
physics training proaram
lesson
plan for 1989/cycle
1, 1988/cycle 2,
and
1988/cycle
1.
Some
of the topics covered in the lesson
plans included:
Radiography Safety
Incore !nstrumentation
Chemical
Volume Control
System Filter Chanoe
Outs
Plant Safety
Personnel
Decontamination
Hot Particles
Sources of Radiation
PWR Overview
The inspectors
discussed
the
scope
of the training with licensee
representatives.
The
licensee
committed
. tc evaluate
adding
the
following subjects
in future training
cycles:
conduct
evaluations
for active
RWP work; participate in mock-up training for
radiological control; perform pre-job
and post-job reviews; initiate,
track,
and
complete
ALARA projects;
interface with scheduling
and
outage
management
groups for processing
work documents;
perform
a
shielding review; and use of the Nuclear Information Management
System
(NIYiS).
The lack of 'a retraining or requalification
program for
returning radiological
control
HP technicians
was identified as
an
weakness,
d.
Program
Improvements
The
inspectors
also
discussed
the
licensee's
self-identified
improvements
for the
ALARA training
program.
Some
of the
items
recently identified by the licensee
included:
Develop more formal preoutage/prejob
training
Develop "system cleanliness"
control training program
10
Upgrade
the
program to include
ALARA policy discussions,
suggestions
program,
and hot particles
Develop specific
exposure
reduction training for engineers
and
HP personnel
Develop
component
location video displays
to aid in equipment
location
The inspectors
recognized
the licensee's
initiative to improve the
ALARA training.
6.
ALARA/RWP Procedure
Implementation
(83528)
The
inspectors
reviewed
the following
HP procedures
that pertained
to
ALARA practices:
O-ADM-360, Radiation Protection Man/Health Physics Technician
Training, March 22,
1988
O-ADM-600, Health Physics
Manual,
March 31,
1988
O-ADN-701, Plant
Work Order Preparation,
October 26,
1988
O-HPA-001, Radiation
Work Permit Intitiation and Termination,
December 2,
1988
O-HPA-005,
Yian-Rem Reporting,
Yiay 22,
1985
O-HPA-006,
ALARA Program, July 9,
1987
HP-55, Temporary Shielding,
January
14,
1986
PTP 100-14,
ALARA Evaluation, July 23,
1984
a.
Post-job
Reviews
The
inspectors
reviewed
the
licensee's
criteria for conducting
post-job
ALARA reviews,
and
observed
that
procedures
O-ADM-600,
Health Physics
Manual
and O-HPA-001, Radiation
Work Permit Initiation
and
Termination,
required
post-job
reviews
when the total
actual
collective
dose
was
greater
than
50
person-rem.
Additionally,
0-ADYTA-600 required
a post-job review to be conducted
by the corporate
group
when
the
actual
collective
dose
~ was
greater
. than
100 person-rem.
The post-job
review
was
intended
to capture
the
success
or failure of the
ALARA techniques
used for the task.
The
inspectors
reviewed
the post-job reviews that were performed for the
present
outage
and previous
outage.
It was observed
that only one
formal
post-job
review
was
performed
during
the
present
outage
(reactor
head ductwork).
During the previous outage,
only one formal
post-iob
review
was
preformed
(control
rod drive
mechanism
repair)
and
one informal post-job review was performed
(environmental
qualification electrical
splice work).
The inspectors
discussed
the
post-job
review prooram with licensee
representatives,
noting that
few formalized
post-job
ALARA reviews
were
conducted
and
the
unrealistically high criteria for requiring
a post-job
ALARA review.
The licensee
agreed that the post-job
ALARA review criteria should
be
revised
so that
more jobs would be critiqued for later application
towards
dose
reduction.
Several
methods for establishing
post-job
ALARA review criteria were
discussed
with the
licensee
including
consideration
of the following:
(1) estimated collective dose
less
than
one
person-rem
and
the
actual
dose
is greater
than
one
person-rem
and
150K greater
than
the
estimate;
(2) estimated
collective
dose
is oreater
than or equal
to one person-rem
and the
actual
dose .in
150~ greater
than
the estimate;
and
(3) estimated
collective dose is greater
than or equal
to five person-rem
and the
actual
dose is greater
than
25~ of the estimate.
Also discussed
was
the
involvement of the
ALARA Coordinating
Committee
in post-job
reviews
when
the
estimated
dose is greater
than or equal
to five
person-rem
'and the actual
dose
is
150K greater
than the estimate.
The post job ALARA review program
was identified as
a weakness.
b.
Exposure Tracking
The inspectors
observed
that the licensee
manually tracks
the time
spent in performing jobs in high radiation areas.
This process
was
labor-intensive
for the
HP staff.
As
a result,
the licensee
was
unable
to provide job-specific man-hour
information
on
a real
time
basis
and obtaining collective dose
data for,a specific job was often
delayed.
Through discussions
with the licensee,
the inspectors
noted
that the licensee
had
budgeted
funds to install
a
NIMS which would
have
as
one
of its functions
the ability tc track job-specific
man-hours.
c.
Exposure Correlation
The
inspectors
reviewed
the correlation
between
the
TLD and
measurements
for 1988,
The following is
a
summary of the
data
reviewed:
Table
3
PIC and
TLD Correlation
month
1/88
2/88
3/88
4/88
5/88
PIC,
Person-rem)
75
39
132
18
41
Person-rem
63
. 29
103
12
Ratio
~(PIC/TLD
1.19
1.34
1.28
1.50
1.41
.
6/88
7/88
8/88
9/88
10/88
11/88
12/88
18
13
23
63
223
202
157
12
11
7
12
41
160
171
126
1.64
1.86
1.92
1.54
1.39
1.18
1.25
In general,
during outage
months,
the licensee's
PIC readings
were
25~ greater
than
TLD measurements.
During non-outage
months,
the
PIC/TLD ratios
were
much larger.
On the average,
the
PIC readings
were approximately
55~ greater
than
TLD measurements.
The inspectors
and
licensee
representatives
discussed
these
discrepancies
and the
need to investicate
the reasons
for them.
The licensee
believed that
part of the problem
may be
due to the practice of resetting
the PIC
after
exitino
the
RCA,
even if
no significant
exposure
was
accumulated
on the ion chamber.
The licensee
believed that the
dose tracking computer operators
may have the tendency
to enter, for
example, five milliroentgen,
even if the individual's PIC indicated
a-
value close to zero.
The licensee
was considering
the adoption of
a
policy of not resetting
the
PIC to zero after
each
use.
The
discrepancies
in correlations
of
and
TLD measurements
was
identified as
a weakness.
d.
Dose Estimation
The inspectors
also
reviewed
a
summary of
12 completed
RWPs with
particular attention to the comparison of actual collective dose
and
budgeted
or estimated
collective dose.
Of the
12 completed
RVPs,
seven
were
over the estimate,
ranging
from approximately
=125~ to
710K.
The difficulty in making realistic
man-hour
estimates
for
collective
dose
was
discussed
with the
licensee.
The licensee
perceived
the
man-hour
estimation
problem
as
three-fold:
(1) unplanned
work as
a result of Engineering
Department evaluations;
(2)
new work scope for which
no historical
data
are available for
man-hour estimates;
and
(3) low man-hour estimates
from the Planning
Department.
Although the
licensee
was
aware
of the
m'an-hour
estimation difficulties, there
were
no
apparent
proposals
for a
solution,
The
inspectors
stressed
the
importance of the
design
engineers
to work more closely with the planners
and schedulers
so
that the
amount of unplanned
work could
be minimized.
The licensee
understood
and
acknowledged
the inspectors'oncerns.
The
poor
coordination of work and
low man-hour estimates
were identified as
a
weakness.
7.
Audits and Appraisals
(83538)
The inspectors
reviewed
both Corporate
audits
and plant Quality Assurance
(QA) audits for calendar
year
1988.
Additionally, the inspectors briefly
reviewed
a draft of the Turkey Point
ALARA Design Review Report conducted
by Westinghouse
on
December
12-15,
1988.
Although this report
was
a
13
draft, the inspectors
noted that this assessment
identified several
good
dose
reduction
and
source
reduction initiatives that were in place
or
planned
and
several
sugaestions
for additional
plant
improvements.
The
Corporate
audits referred to above
were basically performance
based plant
walkthroughs of the
RCA and did not address
the
ALARA program.
The plant
gA audits
focused
on radiation protection,
postings,
and high radiation
areas.
Only one of the
seven audit reports
reviewed identified an
program related
finding.
The inspectors
found, in general,
that the
audits
lacked
the
depth
to identify radiological
and technical
issues
necessary
for ALARA improvement.
8.
Interviews
(83528/83728)
a
0
Employee Discussions
The inspectors
discussed
with licensee
employees
their knowledge,
involvement,
and perspective
of the utility's ALARA Program,
including
the
employee's
knowledge
of
ALARA goals,
concepts,
policies
and
procedure
documents;
individual responsibilities,
personal
doses
and
personal
dose limits; the
employee's
involvement in special
training,
communication
with
co-workers
and
supervision,
and
participation
in the
ALARA suggestion
program;
and
the
employees
perspective
on
how to
improve the
ALARA program,
what
events
or
conditions
have
caused
increased
personnel
doses,
and
on what events
or conditions
had helped
reduce
personnel
doses.
(1)
Employees
All employees
interviewed entered
the
RCAs on
a daily to weekly
basis
depending
on plant conditions.
(2)
Knowledge of ALARA Program
Each of the
employees
interviewed
was familiar with,the basic
ALARA concepts
taught
in the
Radiation
Protection
Training
portion of GET.
This portion of is training in referred to as
Red
Badge Training in the
GET program.
Each of the
employees
knew that they
had
a basic responsibility for implementing the
utility's
ALARA program
by
performing
tasks
in
a
manner
consistent
with the utility's ALARA policy.
In general,
the
employees
knew their current
radiation
exposure
and their
exposure limit and
knew that
a daily dose printout was available
at the entrance
to the
RCA.
The employees
generally were aware
of where
the
ALARA requirements
originated
and what documents
described
the
ALARA program objectives.
Most of the employees
interviewed
knew that each of their sections
has
an
ALARA goal.
The employees
knew that they could find out their section's
goal
from the
HP staff.
ALARA Program Involvement
The
employees
interviewed
had not received
any
ALARA training
other
than that given in the
GET course.
A larae
number of
those
interviewed
had received
some informal
ALARA training on
jobs requiring
ALARA pre-job planning
and on-the-job training.
Employees
reported
frequent
discussions
of ALARA objectives
on
major jobs during outages
with co-workers
and supervisors
and
also
AZCs.
The employees
reported
good
and open communications
with the
AZC and
HP staffs.
Only a small fraction of employees
interviewed
had
participated
in the
formal
"Bright Ideas"
suggestion
program.
Other employees
reported that they had made
suggestions
to supervisors
informally and
had
not
used
the
formal sugoestion
program believing it was only for "significant
suggestions."
It was
determined
that currently
the "Bright
Ideas"
program incentives
were only available to the licensee's
employees.
A majority of the backfit and plant modification
work
was
scheduled
for contractors.
The licensee
agreed
tc
evaluate
the
use
of the "Bright Ideas" incentive
program with
contractor personnel.
Findings
Host of the
employees
had suggestions
on
how the
ALARA Program
could be improved.
The suggestions'ncluded
better planning
and
scheduling
of work to ensure
that
appropriate
equipment
and
tools were readily available to perform task expeditiously.
The
majority of employees
had opinions
on what had contiibuted to
decreases
and
increases
in personnel
exposures.
Employees
believed that the following actions
had contributed to exposure
reductions:
use
of
temporary
shielding,
special
tools,
permanent
shielding
such
as the reactor
vessel
head shielding,
flushing
of
various
system
components
and
lines,
and
decontamination
of contaminated
areas within the
RCA.
Employees
believed that the following action 'had contributed to increases
in personnel
doses:
poor maintenance
planning
and scheduling in
the
past;
proficiency of contract
personnel;
and failure to
include
input
from craft maintenance
personnel
on
proposed
engineering
changes.
Overall the employees
expressed
a positive
feeling
on management's
support for ALARA and
HP.
.The use of
the Turkey Point
news letter
"To the Point"
and the
TY video
screen
news monitors which provided periodic
ALARA messages
were
deemed positive by the employees
during the interview.
b.
Hanagement
Discussions
The inspectors
discussed
with licensee
manaaers
and supervisors
the
utility's ALARA Program,
including their knowledoe of
ALARA goals,
concepts,
policies
and
procedure
documents,
individual
responsibilities,
personal
exposure,
and
personal
exposure limits,
and their involvement in special
ALARA training,
communication with
15
co-workers
and supervision,
and participation in the
ALARA suggestion
proaram;
and
the managers'r
supervisors'erspective
on
how to
improve the
ALARA program,
what events
or conditions
have
caused
increased
personnel
exposures
and
what events
or conditions
have
helped
reduce
personnel
radiation exposures.
Managers
and Supervisors
All individuals interviewed
entered
the
on
a weekly to
monthly basis
depending
on plant conditions.
Knowledge cf ALARA Program
Each individual interviewed
was familiar with the basic
concepts
taught
in the
GET program
and
knew that they
had
a
basic
responsibility
for
implementing
the utility's
program
by performing
a task
in
a
manner consistent
with the
utility's
ALARA policy.
In
general,
the
managers
and
supervisors
interviewed
were
knowledgeable
of the
current
,
radiatior.
exposure
and
exposure
limits for their departments.
The
managers
and
supervisors
understood
where
the
requirements
originated
and what corporate
and plant documents
described
the
ALARA program objectives.
All the managers
and
supervisors
interviewed
knew their department's
ALARA goals
and
knew that their
annual
performance
appraisal
contained
elements for which they were held accountable
in meeting their
ALARA goals.
ALARA Program
involvement
The majority of the managers
and supervisors
interviewed
had not
received
any
ALARA training other than that given in the
"Red Badge"
course.
Each department
had
a dedicated
individual
to serve
on the'LARA Review Committee
(ARC), which met
on
a
quarterly basis
or as needed.
The
ARC members
represented
their
departments
in discussions
of
ALARA objectiveness
for major
outage
jobs with coworkers
and
supervisors.
None of the
managers
or
supervisors
interviewed
had participated
in the
formal
"Bright
Ideas"
suggestion
program
with
an
suggestion.
However,
generally
most
of the
managers
or
supervisors
interviewed
were
aware of formal or informal
suggestions
submitted
by their departments
in the
past
or
current year.
These
ALARA suggestions
were usually submitted
by
employees
during
a pre-job briefing.
There
appeared
to
be
a
strong
management
commitment to use innovative initiatives
and
excell in collectiv'e person-rem
reduction.
Findings
All managers
and supervisors
interviewed
had sugoestions
on how
the
ALAPA program could
be improved.
The suggestions
included
16
9.
Chemistry
recommendations
for better
scheduling
and
planning of work;
ensuring
that
appropriate
equipment
and
tools
were
readily
available,
and
a
commitment to increase
the
awareness
of the
ALARA concept to all levels of plant personnel.
At the start of
the
Unit 4 outage,
some
26
unapproved
and
unscheduled
Plant
Change
and
Yiodifications
(PCNs)
were
working through
the
approval
process
for the outage work.
In addition, at least ten
have
been initiated
and were to be worked prior to outage
completion.
This unanticipated
and unplanned
work has resulted
in significant increases
to the person-rem totals
thus far in
the
unit
outage.
Person-rem
reductions
associated
with
efficient, well
planned
jobs
have
not
been
realized.
As
a
result,
at the time of the
team visit, contractor
person-rem
goals were. being overrun
by approximately
250K.
The majority of managers
and supervisots
had opinions regarding
the
contributors
to
decreases
and
increases
in
personnel
exposures.
Individual
managers
and
supervisors
interviewed
believed that the following actions
had contributed to exposure
reduction:
use of AZC, use of temporary shielding,
and
reduced
work activities in high radiati'on areas.,
Individual managers
and
supervisors
interviewed
believed
that
poor planning
and
scheduling
of maintenance
had
contributed
to
increases
in
collective dose.
Also, several
personnel
interviewed believed
that namino
a permanent
Radiation Protection
Manager replacement
would provide
a strong leadership
and program stability.
The
inspectors
discussed
the water
chemistry
program with cognizant
licensee
representatives
and
reviewed
pertinent
procedures
with the
objective of determining water chemistry's role in dose reduction.
Licensee
representatives
stated that prior to shutdown,
hydrogen peroxide
was
added to the Reactor
Coolant
System.
This resulted
in crud releases
from components
to the coolant,
which
was
cleaned
up
by the
letdown
demineralizers.
The inspectors
reviewed the coolant activity curves for
the Unit 3 outage
in 1987.
These
curves
showed that coolant activity
increased
sharply
upon addition of the hydrogen peroxide,
then decreased
with use of the demineralizers.
Another method
was throuoh lithium-boron coordination
and constant lithium
(pH) control.
This program
had
been
used for the past three years,
and
the licensee
stated
that the
dose
in the vicinity of the hemispherical
bottom head of the steam generator
"bowl" dose
has trended
downward during
this period.
This type of chemistry control kept radioactive materials
suspended,
rather than plating out.
The letdown dpmineralizers
then could
remove the crud.
The licensee
representative
stated that
when Unit 4 is
started
up,
elevated
pH control will be used.
It was anticipated that
initial coordination
would be at
a
pH of 6.9, then, later in core life,
17
increasing
to
a
pH of 7.2.
The licensee
would eventually coordinate at
a
pH of 7.4 if fuel vendor approval
was received.
The
Chemistry
Department
closely
monitored
primary
chemistry
and
calculated
Fuel Reliability Index (FRI) which was plotted
and tracked.
This index
was calculated
from measured
coolant levels of Iodine-131
and
Iodine I-134.
The Iodine-134
was
used to correct for tramp uranium in the
zircal 1oy fuel cladding.
Condensate
polishina demineralizers
were used during startups
and extended
shutdowns.
Normally these
would run for 12-13 hours before they had to be
taken off line.
A change
was
made in the precoat process,
and during the
last
startup,
the
demineralizers
were
run for
40
hours
with
no
breakthrough.
Licensee
representatives
stated
that the Chemistry Department
had
become
more
involved
in liquid
and
gaseous
effluent
releases.
Chemistry
procedurally
has
lowered allowable concentrations
in Waste Monitor Tanks
from 1E-4 microcuries
per milliliter (uCi/ml) to
1E-5 uCi/ml,
and
was
considering
ways to lower waste volume.
The Chemistry Department
was also
monitoring
a vendor's testing
program for increasing filter efficiency for
removal of cobalt in the reactor
coolant
system
by applying electrical
voltage across
the filter,
The inspectors
noted that these
actions
by the chemistry program should
contribute to lowerina collective dose.
The inspector
discussed
steam
generator
operations
and maintenance
with
licensee
representatives
with
the
objective
of
determining
the
contribution of
steam
generator
operation
and
maintenance
to
dose
reduction.
Licensee
representatives
stated- that
sludge
lancing
was
performed
during
each
outage
to reduce
deposits.
Foreign Object Search
and Retrieval
(FOSAR)
was
done using fluoroscopy.
FOSAR was
a method of
detecting
loose objects in the
which might cause
damage
through
impact or blockage of flow channels.
Licensee
representatives
stated
that in the future the target
was to perform. 100%
eddy current
testing of the tubes,
the only constraint
being that completion of the
outage not be delayed.
A licensee
representative
stated that
ALARA principles were applied in the
conduct of steam generator
maintenance
by the following means:
Using remote devices (robotics) where possible.
Providino
HP the
complete
plan for steam generator
work to be done
during the next outage well in advance.
Combining jobs
so that several
could
be done in each entry.
18
Training of workers in advance of job.
Working closely with HP for backfit work.
These
methods
appeared
to
be effective
in
reducing
exposure.
An
aggressive
chemistry
program
and close monitoring of system
parameters
appeared
to have helped in decreasing
the
amount of sludge to be
removed
and the good condition of steam generator
tubes
noted during eddy current
testing.
12.
Followup Items
(Closed)
Inspector
Followup Item (IFI) 50-251/88-25-03;
Review licensee
action
concerning
operation
of
the
spent
fuel
pool
cleanup
filter-demineralizer to limit radioactivity concentrations
in water.
The inspectors
verified that Nuclear Chemistry Procedure
NC-99,
Sampling
the Spent
Fuel Pit, and the Spent
Fuel Pit Demineralizer Inlet and Outlet,
dated
November
10,
1988,
required that if total isotopic activity exceeds
5.0 E-3 microcuries
per milliliter, the
NWE is requested
to have the spent
Fuel Pit recirculated
through
the demineralizer, if not being performed
already.
The inspectors
reviewed
curves of the total activity found in
the
Spent
Fuel
Pits
and verified that
since
implementation
of the
Procedure,
the Unit 3 Spent
Fuel Pit remained
below 5.0 E-3 uCi/ml total
concentration,
and the Unit 4 Pit has
not exceeded
6.0 E-3 uCi/ml except
for one period in December
1988.
13.
Conclusion
(83528/83728)
Considerable
steam
generator
maintenance,
subsequent
steam
generator
replacement,
and
a
high out-of-core
source
term contributed
to high
collective'dose
in past years.
However, increased
management
support for
the
ALARA program from both plant and corporate
groups
and implementation
of the
concept for on-the-job
dose
reduction
(AZCs)
has
resulted
in
a
significant reversal
of the past trend.
The following significant issues
were identified as weaknesses
during the inspection:
Lack of health
physics
(HP) involvement in maintenance
department
mock-up training, lack of design-related
ALARA training for design
engineers,
and
minimal retraining
or requalification
program for
returning
technicians;
Paragraph
5.a,
5.b,
and
5.c
(50-250/89-14-04).
Large percentage
of the radiation control
area
(RCA) maintained
as
contaminated;
Paragraph
3.b (59-250/89-14-01).
Poor work coordination
and
low man-hour
estimates
resulting in low
dose projections;
Paraoraph
6.d (59-250/89-14-07).
Post-job
ALARA review only conducted for jobs with a collective dose
exceeding
50 person-rem;
Paraaraph
6.a (50-250/89-14-05).
19
Lack
of formalization
of the
ALARA Zone
Coordinator
concept;
Paragraph
4.a (50-250/89-14-02).
Lack of full attendance
at the
ALARA Coordinating
Committee meetings;
Paragraph
4.b (50-250/89-14-03).
Limitation of
the
suggestion
program
for
ALARA improvements;
Paragraph
S.a(3)
(50-250/89-14-08).
Discrepancies
in correlation
of
ion
chamber
(PIC)
and
thermoluminscent
dosimeter
(TLD)
measurements;
Paragraph
6.c
(50-250/89-14-06).
14.
Exit Interview
The inspection
scope
and findings were summarized
on Yiarch 24,
1989, with
those
persons
indicated
in Paragraph
1.
The inspectors
described
the
areas
inspected
and
discussed
in detail
the
inspection
findings
(see
Paragraph
13).
The licensee
acknowledged
the inspection findings and took
no exceptions.
The licensee
did not identify as proprietary
any of the
material
provided to or reviewed
by the inspectors
during the inspection.
Cl'