ML17345A397

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SALP Repts 50-250/88-15 & 50-251/88-15 for June 1987 - June 1988
ML17345A397
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 09/13/1988
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17345A396 List:
References
50-250-88-15, 50-251-88-15, NUDOCS 8809260148
Download: ML17345A397 (88)


See also: IR 05000250/1988015

Text

ENCLOSURE

SALP

BOARD REPORT

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT

OF LICENSEE

PERFORMANCE

INSPECTION

REPORT

NUMBER

50-250/88-15

50-251/88-15

FLORIDA POWER

AND LIGHT COMPANY

TURKEY POINT UNITS 3 AND 4

JUNE 1,

1987

THROUGH JUNE 30,

1988

ssom6ocas

Siovis

pDR

ADQOK p500025p

6

PNU

0,

INTRODUCTION

The

Systematic

Assessment

of Licensee

Performance

(SALP) program is

an

integrated

Nuclear

Regulatory

Commission

(NRC) staff effort to collect

. available

observations

and

data

on

a periodic

basis

and

to evaluate

licensee

performance

based

on this information.'he

SALP

program is

supplemental

to normal

regulatory

processes

used to determine

compliance

with

NRC rules

and

regulations.

The

SALP

program

is

intended

to

be

sufficiently diagnostic

to provide

a rational

basis

for allocating

NRC

resources

and

to provide meaningful

guidance

to licensee

management

in

order to promote quality and safety of plant construction

and operation.

An

NRC

SALP Board,

composed

of the staff

members listed below,

met

on

August 23,

1988, to review the collection of performance

observations

and

data

to assess

licensee

performance

in accordance

with guidance

in

NRC

Manual

Chapter

0516,

"Systematic

Assessment

of Licensee

Performance."

A

summary of the guidance

and evaluation criteria is provided in Section II

of this report.

This report is the

SALP Board's

assessment

of the licensee's

safety

and

management

performance

at

Turkey Point Units

3

and

4 for the

period

June

1,

1987, through June

30,

1988.

SALP Board for Turkey Point Units 3 and 4:

L. A. Reyes,

(Chairman), Director, Division of Reactor Projects

(DRP),

Region II (RII)

A. F. Gibson, Director, Division of Reactor

Safety

(DRS), RII

J.

P. Stohr, Director, Division of Radiation Safety

and Safeguards

(DRSS),

RII

B. A. Wilson, Chief, Reactor Projects

Branch

2 (RPB2),

DRP, RII

H.

N. Berkow, Director, Project Directorate II-2, Division of Reactor

Projects,

Office of Nuclear Reactor

Regulation

(NRR)

G.

E. Edison,

Senior Project Manager,

Turkey Point, Project Directorate

II-2, Division of Reactor Projects,

NRR

Attendees at

SALP Board Meeting:

M. L. Ernst,

Deputy Regional Administrator, RII

R.

V. Crlenjak, Chief, Reactor Projects

Section

2B,

RPB2,

DRP, RII

H. 0. Christensen,

Project Engineer,

RPB2,

DRP, RII

R.

C. Butcher, Senior Resident Inspector,

Turkey Point,

DRP, RII

G. A. Schnebli,

Resident

Inspector,

Turkey Point,. DRP, RII

P.

M. Madden,

Reactor Engineer,

Technical

Support Staff (TSS),

DRP, RII

T.

C. MacArthur, Radiation Specialist,

TSS,

DRP, RII

P.

A. Balmain, Reactor Engineer,

TSS,

DRP, RII

CRITERIA

0

Licensee

performance is assessed

in selected

functional areas

depending

on

whether

the facility has

been

in the

construction,

preoperational,

or

operating

phase

during

the

SALP review period.

Each

functional

area

normally represents

an area which is significant to nuclear safety

and .the

environment

and

which is

a

normal

programmatic

area.

Some

functional

areas

may not

be

assessed

because

of little or

no licensee activity or

because

of

a lack of meaningful

NRC observations.

Special

areas

may

be

added to highlight significant observations.

One or more of the following evaluation criteria was used to assess

each

functional area;

however,

the

SALP Board is not limited to these criteria

and others

may have

been

used

where appropriate.

A.

B.

C.

D.

E.

F.

G.

Management

involvement in assuring quality

Approach

to

the

resolution

of technical

issues

from

a

safety

standpoint

Responsiveness

to

NRC initiatives

Enforcement history

Operational

and construction

events (including response

to, analysis

of, and corrective actions for)

Staffing (including management)

Training and qualification effectiveness

Based

upon

the

SALP Board

assessment,

each

functional

area

evaluated

is

classified into one of three

performance

categories.

The definitions of

these

performance

categories

are:

~Cate or

1:

Reduced

NRC attention

may

be appropriate.

Licensee

management

attention

and

involvement

are

aggressive

and oriented

toward nuclear safety;

licensee

resources

are

ample

and effectively

used

such

that

a

high

level

of

performance

with respect

to

operational

safety or construction quality is being achieved.

~Cate or

2:

NRC attention

should

be

maintained at

normal

levels.

Licensee

management

attention

and

involvement are evident

and are

concerned

with nuclear

safety;

licensee

resources

are

adequate

and

are

reasonably

effective

such that satisfactory

performance

with

respect

to

operational

safety

or

construction

quality is

being

achieved.

~Cate or

3:

Both

NRC

and

licensee

attention

should

be increased.

Licensee

management

attention

or

involvement

is

acceptable

and

considers

nuclear

safety,

but

weaknesses

are

evident;

licensee

resources

appear

to

be strained

or not effectively used

such that

minimally satisfactory

performance with respect

to operational

safety

or construction quality is being achieved.

The functional

area

being evaluated

may

have

some attributes

that would

place

the

evaluation

in Category

1

and

others

that

would place it in

either Category

2 or 3.

The final rating for each functional

area

is

a

composite

of the attributes

tempered

with the judgment of NRC management

as to the significance of individual items.

The

SALP Board

may also include

an appraisal

of the performance

trend of a

functional

area.

This performance

trend will only be

used

when

both

a

definite trend of performance within the evaluation period is discernable

and

the

Board believes

that continuation of the trend

may result in

a

change of performance

level.

The trend, if used, is defined as:

~Im rovin

Licensee

performance

was determined

to be improving near the

close 'of the assessment

period.

~Declinin

Licensee

performance

was

determined

to

be declining near the

close of the assessment-

period

~

III. SUMMARY OF

RESULTS

A ~

Overa 1 1

Fac i 1 ity Eva 1 uati on

The

licensee

has

continued

to

make

improvements

during this

SALP

period.

Although the initial portion of this period

indicated

a

definite

need for improvement,

which resulted

in the

issuance

of

a

Confirmatory

NRC

Order

in

October

1987,

management

attention

to

deficiencies

identified

in

the

Confirmatory

Order

has

produced

results during the latter portion of the rating period.

The licensee

has

made

a series

of personnel

changes

using

people

not previously

assigned

to the Turkey Point facility in order to obtain

a

new look

at the problem areas.

The initiation of several

new programs,

such

as

Management

on Shift,

an in-depth plan of the day, shift briefings,

and

an emphasis

on accountability

and ownership

have

had

an impact

on

reversing

adverse

characteristics

of culture

and climate previously

existing at the plant.

There

has

been

a definite shift in management

philosophy in the conservative

direction to shut

down the plants

or

extend

shutdown periods to allow equipment repairs to be completed to

help

improve unit reliability.

The

security

program continues

to

show

a weakness

as indicated

by the continued

number of violations

which are repetitive in nature.

The

new maintenance

building and the

simulator were completed during the period

and

should

show tangible

benefits in the future.

Corporate

management

has committed to expend

tremendous

resources

at the site to enhance

the

safe

and reliable

operation

of the units.

Throughout

the rating period,

there

have

been

numerous

meetings

between

the licensee

and the

NRC to resolve

issues

over

the licensee's

proposed

Technical

Specifications

(TS),

which were submitted in October of 1986.

These modified standard

TS

will provide

a significant improvement over the old custom TS.

In April

1988,

an

Independent

Management

Appraisal

(IMA) of the

Turkey Point facility was

completed

and

submitted to the

NRC.

The

IMA was

evaluated

by the Office for Analysis

and

Evaluation of

Operational

Data

(AEOD) and

immediately after the

SALP period, this

evaluation

was provided to

FPL.

Initial indications

show that

FPL

has

been very responsive

to implementing

the

recommendations

of the

IMA and the

AEOD evaluation.

However,

due to the history of poor

performance

in

a

number

of functional

areas, it is incumbent

upon

FPL and the

NRC to maintain close

management

scrutiny of performance

indicators,

site

organizations

and

effectiveness

of the

various

corrective actions.

B.

Facility Performance

Summary

The performance

categories

for the current

and previous

SALP period

in each functional

area

are

as follows:

Functional

Area

May 1, 1986-

Ma

31

1987

June

1, 1987

June

30

1988

Plant Operations

2

Radiological Controls

2

Maintenance

2

Surveillance

2

  • . Fire Protection

N/R

Emergency

Preparedness

1

Securi'ty and Safegurds

3

Outages

2

guality Programs

and Administrative

Controls Affecting equality

2

Licensing Activities

2

Training

and

equal

ificati on

Effectiveness

3

Engineering

Support

3

3 Improving

2

3 Improving

2

2

2

3

2

N/R = Not Rated

IV.

PERFORMANCE ANALYSIS

~

~

A.

Plant Operations

l.

Analysi s

During the first half of this

SALP period, licensee

performance

in the

area

of Operations

was

marginal

as

demonstrated

by

equipment

problems,

plant availability,

number

of escalated

enforcement

actions,

and

number

of special

NRC

inspections.

Recent

management

changes

and

implementation

of

program

improvements

have significantly improved Operations

toward the

end of the

SALP period.

For the last

six

months

of 1987,

Unit 3

had

an availability

factor of less

than

10%.

During the first half of 1988 this

improved to about

71%.

Following the. repairs

to the

conoseal

leak, Unit 4 returned to service in July and

had

an

up and

down

operational

history for the

remainder

of

1987.

Availability

factors for Unit 4 were about

63% for the first half of the

SALP

period and

73% for the

second half.

The previous

SALP report

noted

improvements. in the Operations

area,

although

an event that occurred at the

end of the

SALP

period,

which resulted

in loss of the required boric acid flow

paths,

was discussed.

A special

NRC inspection

condu'cted

in

June

1987 resulted

in escalated

enforcement

action

and

a civil

penalty (violation b).

In July 1987,

another

event

occurred

resulting

in

a Severity

Level III violation.

This involved

a

turbine operator

who closed

backup nitrogen supply valves to the

Auxiliary Feedwater

System

(AFW).

Then

in

September

1987,

an

unauthorized,

unlicensed

individual

was

allowed to manipulate

the dilution controls of Unit 3 with the reactor at

power.

At

least

four

licensed

operators

observed

the

event

without

intervening.

A

management

observer

reported

the

event

to

several

members

of the plant

management

who hold or have

held

Senior

Reactor

Operator

licenses.

However,

appropriate. action

was not taken. to evaluate

and resolve the circumstances

leading

to the event for over one week.

This event,

along with other observations

made

by the management

observer,

raised

concerns

as

to the

adequacy

of professional

conduct

on shift.

Continuous

NRC control

room observations

were

conducted

in late

September

and early October

1987 to evaluate

'control

room demeanor

and conduct of operations.

In October

1987, voids were detected

in the Unit 4 reactor

head

region with the plant at cold

shutdown.

Evaluation determined

that nitrogen from an accumulator

had entered

the primary system

through

a leaking accumulator isolation valve.

A total of seven

voiding events

occurred

between

October

21 and

November 3,

1987.

Several

of these

were avoidable

had the desired

valve lineups

been

maintained.

A special

NRC inspection

was

conducted

in

November

to

investigate

the

circumstances

surrounding

these

occurrences.

A review of the

Operations

related

violations,

special

NRC

inspections

and

Licensee

Event

Reports

(LERs)

shows

the

preponderance

of these to occur in

1987'.

The

NRC's Office for

Analysis

and Evaluation of Operational

Data

(AEOD) reviewed

65

LERs for the

two Turkey

Point units

over this'ALP period.

Fifty-one

LERs were

submitted

in the last

seven

months of 1987

and

14 were submitted in 1988.

Further analysis

of these

LERs

is later in this section.

Four reactor trips occurred

during this evaluation

period for

Unit 3.

Unit 4 did not trip during this period.

Three of the

trips

were while operating

above

15% power.

Two were

due to

personnel

error

and

one

due

to

equipment

malfunction.

This

represents

an

improvement

over the previous

evaluation

period

and is slightly above

the national

average

for trips per

1000

critical hours for 'plants of this type.

The deficiencies

identified in the

summer

and fall of

1987

resulted

in licensee

generated

corrective actions,

which were

confirmed

by an

NRC Order

(87-85)

issued

on October

19,

1987.

One

confirmatory

item

included

a

commitment

to

conduct

an

Independent

Management

Appraisal

(IMA) to

be

performed

by

a

third party,

qualified,

outside

organization.

The

IMA was

performed

between

December

14,

1987,

and

March 30,

1988,

and

included

interviews,

document

reviews,

surveys

and

direct

observations

at

the

Turkey Point Plant

and the

FPL corporate

offices:

A final report -was

issued

in April 1988.

An

NRC

evaluation

of the

IMA to determine its quality and completeness

7

was

completed

in June

1988.

The licensee'

response

and action

plan to implement the

IMA findings were submitted for NRC review

after the close of the evaluation period.

It was

determined

that. operational

performance

issues

stemmed

from root causes

related to operations

ownership

and leadership,

training

and

implementation

of Technical

Specifications.

Poor

performance

was

caused,

in part,

by past

focus

on near

term

plant availability rather than long term plant reliability and

a

lack of

strong

sense

of plant

ownership

in the

Operations

Department.

Over

the

long

term, this resulted

in operators

using

compensatory

measures

and

backup

methods

to operate

the

plant safely

when

equipment

was

not operating

properly.

These

practices

resulted

in operators

who did not

.ake

a leadership

role in the operation

and maintenance

of the plant.

The

leadership

of the

operators

has

also

inadvertently

been

diluted

through corrective

actions

in

response

to identified

problems.

For

example,

several

incorrect

Technical

Specification interpretations

have

been

documented

over the past

several

years.

In

an effort to prevent

recurrence,

support

groups,

such

as

the Regulatory

Compliance

Group and Operations

Department

Supervisors,

were utilized to confirm the decisions

of the

control

room supervisors.

Over time, this

led to

a

dependence

on outside

help in complying with required actions.

This

problem

has

been

compounded

during

the

upgrade

of the

custom Technical Specifications to

a standardized

format.

The performance

problems which occurred early in the assessment

period were analyzed

by the licensee

and corrective actions

were

implemented.

It was

recognized

that

an

increased

emphasis

on

management

and accountability

was

necessary,

and to thi s end

a

series

of

personnel

changes

were

made

which

spanned

the

assessment

period.

Each

change

was implemented

using personnel

not previously

assigned

to the

Turkey Point facility in

an

effort to obtain fresh insight into problem areas.

A new Site Vice President

was appointed

in August 1987.

Shortly

after his arrival,

a significant initiative was taken to place

a

management

representative

on operating shifts to help identify

deficiencies

in performance.

This

"Management-On-Shift"

(MOS)

program

was

instrumental

in

identifying

areas

needing

improvement.

A

corrective

action

tracking

program

was

established

for identified discrepancies.

The

MOS

program

provided

increased

sensitivity

relative

to

plant

material

condition,

planning

and

scheduling,

leadership

and

professionalism,

procedural

compliance

and

inter-departmental

communications.

Subsequent

to the

September

1987 operation

of

the Unit 3 dilution controls by an unauthorized individual, the

MOS

program

was

expanded

and

confirmed

by

NRC

Order

. It is

significant that

the

professionalism

questions

raised

by the

dilution

event

were initially identified

by

a

MOS observer

participating

in the then voluntary

enhancement

program.

One

important

initiative

derived

from *analysis

of

the

MOS

observations

was

the

development

of

a Plan-of-the-Day

(POD)

document

to

correlate,

schedule

and

manage

daily

plant

activities.

The

POD addresses

'the daily work lists for each

plant

department,

surveillance

schedules,

. chemistry

results,

plant modification schedules,

priority maintenance

item status

and status

of all Technical

Specifications

limiting conditions

for operation.

The

POD is evaluated daily at

a planning meeting

attended

by all plant departments.

The

MOS

program

successfully

emphasized

improving the shift

turnover

process.

Shift briefings,

performed

by

a

licensed

Senior

Reactor Operator,

are performed after each shift assumes

its duties.

These

briefings

provide

information relative

to

goals

and

objectives

for

the

subsequent

shift.

They

are

attended

by

all

shift

personnel

including

maintenance

disciplines.

As

a

result

of the

POD

and shift briefing

programs,

general

awareness

of site activities

has

been

enhanced

and complex evolutions

have

been

performed

more smoothly.

In

December

1987,

a

new Operations

Superintendent

joined

the

Turkey Point staff.

This change resulted in improved department

morale, just

as

the

change

in the Site Vice President

resulted

in

improved

site

morale.

Promptly

apparent

was

a

renewed

emphasis

on personal

accountability

and operations

"ownership"

of

the

decision

making

processes

that

impact

equipment

operability.

Additional initiatives included the involvement of

the licensed

Senior

Reactor

Operators

in the

MOS

program

to

assist

in

establishing

and

improving their visibility as

managers

of

the

power

block.

Also

a

"Standards

of

Professionalism"

document

was. developed

to clearly define the

responsibilities

of personnel

assigned

to each

licensed

shift

position.

This document,

which was developed with considerable

input

from licensed

operators,

sets

out in clear

terms

new

stringent

standards

of conduct

and performance

against which the

operators will be evaluated.

A new Plant Manager

was appointed late in the assessment

period.

His initial efforts to develop accountability

on the supervisory

level

have

been

well received

and

appear

to

be

succeeding.

Although,

he

has

not

been

in the position

long

enough to have

had

a

clear

impact

on

sustained

performance,

his

renewed

emphasis

on leadership,

professionalism

and

accountability

.have

had

an immediate

impact

on reversing

adverse characteristics

of

culture

and climate, which have existed at the plant.

Operations

has

made

and continues

with efforts to equalize

and

minimize

overtime

for

on

shift

personnel.

Trainees

were

utilized

where

possible

to

perform duties

not

requiring

a

licensed operator.

Although the current staffing level provides

for enough operators

during normal plant operations,

overtime is

routinely utilized during outages,

forced

load reductions,

and

to fill vacancies

during

vacation

periods

or illness.

At

present,

21 operator

and senior

operator trainees

are

scheduled

for

exams

in October

1988.

This

should

aid in reducing

the

amount of overtime presently

required.

In August of 1988,

an

individual will be

assigned

full time to coordinate

advanced

scheduling

and filling of

vacancies.

This

should

aid

in

minimizing excessive

use of overtime

by arranging

in advance for

off-shift personnel

to work vacancies

where possible.

The

NRC Office for Analysis

and Evaluation of Operational

Data

(AEOD) reviewed

65

Licensee

Event

Reports

( LERs) for the

two

Turkey Point units in the

assessment

period

from June

1,

1987,

through

June

30,

1988.

Of the

LERs reviewed, eight were

deemed

to

be significant by AEOD's screening

process.

Four of those

LERs

reported

long-standing

design

deficiencies

that

were

discovered

by the licensee's

selected

safety

system/design

basis

reconstitution

review.

The other four significant events

are

listed

below in violations

a,

b,

and j

and

the

unauthorized

manipulation

of reactor

controls

which

was

included

in the

Confirmatory Order.

The

AEOD

review of the

preliminary notifications

issued

on

events

which occurred

during

the

SALP period

found that the

licensee

submitted

LERs

which

adequately

addressed

the

reportable

events.

The

LERs adequately

described

the major aspects

of each event,

including component or system fai lures that contributed to the

event

and the significant corrective actions

taken or planned to

prevent recurrence.

The reports

were complete,

well written and

easy

to

understand.

The

root

causes

were

identified

as

appropriate.

Previous

similar

occurrences

were

properly

referenced

in the

LERs

-as applicable.

Violation a described

an event involving operation of the intake

cooling water

(ICM) system

outside

the plant design

basis,

and

was

an

example

where

lack

of

communications

of required

information to supervisory

personnel

was

a contributing factor

to poor performance.

This item was discussed

in the last

SALP

report.

Violations c, e, f; i, j, and

m, document

a number of occasions

where

plant

personnel

manipulated

valves without procedural

justification or approval

from supervisory personnel.

The major

areas

of

concern

included

personnel

departing

from approved

procedures,

failing to notify supervisors

of changes

in system

lineups,

the

'loss

of

configuration

control

over

the

safety-related

systems,

and

system

engineers

directing plant

operators'o

perform valve operations

without first obtaining

the proper authorization

from the control

room staff and without

using approved

procedures.

Violation .h,

identifies

a

similar,

though

less

extensive,

misalignment which occurred in January

1988.

On that occasion

a

single nitrogen bottle was inadvertently isolated for the Unit 4

10

AFW nitrogen

system.

Minor

AFW nitrogen

valve

misalignments

also

occurred

once

in

February

and

twice

in

March 1988.

Violation j,

which

occurred

in

June

1988,

resulted

when

a

technician

locked

closed.

a normally

open

valve in the diesel

fuel system,

contrary to procedural

requirements.

These

failures

by

plant

personnel

indicate

a

lack

of

appreciation

for procedural

compliance,

system

configuration

control,

and

receipt

of

appropriate

authorization

for

realignments

from the control

room.

Comprehensive

co~rective

actions

are being implemented.

Thirteen violations were identified:

a.

Severity Level III violation for failure to take corrective

action

to prevent

component

cooling water heat

exchanger

degraded

performance.

(Unit 3 only 87-27)

b.

Severity

Level III violation for failure to establish

or

implement

adequate

procedures

to

assure

configuration

control over the emergency boration

system.

(87-28)

c.

Severity

Level III violation

for failure

to

follow

procedures

which resulted in isolation of the

AFW nitrogen

system.

(87-33).

d.

Severity

Level

IV violation for failure to determine

hot

channel

factors

when quadrant

to average

power tilt ratio

was exceeded.

(Unit 4 only 87-33)

e.

Severity

Level

IV violation

for

fai lure

to

follow

procedures.

Three

examples:

manipulating

heat

tracing

thermostat,

failure to transfer

the

comparator

channel

defeat

switch

on

a power

range

nuclear

instrument,

and

a

boric acid storage

tank valve was not properly locked open.

(87-43)

f.

Severity Level

IV violation for failure to follow procedure

in that

a

manual

isolation valve

was not in its required

position.

(Unit 4 only 87-46)

g.

Severity Level

IV violation for failure to translate

design

inputs

into

correct

operating

procedures

and

system

descriptions.

(87-54)

Severity

Level

IV vi,olation

for failure

to

follow

.

procedures.

Four examples:

fire watch

was

found asleep,

failure

to

independently

verify

AFW

nitrogen

valve

position,

maintenance

performed

on

Unit 3

rod

control

system without documented instructions

and failure to enter

an

o'n the

spot

change

to

a procedure.

(Example

one is

a

fire

protection

violation

and

example

three

is

a

maintenance

violation, 87-54).

11

Severity

Level

IV violation

for failure

to

follow

procedures.

Three

examples:

failure to maintain

a valve

in

an

open

position

as

per

a

clearance

procedure,

no

temporary

system

alteration

for

removed flow indicators,

and

inadequate

surveillance

procedure.

(Example

two is

a

maintenance

violation, 88-02).

-j .

Severity Level IV violation for failure to follow procedure

which resulted in isolation of the diesel

fuel oil system.

(88-11)

k.

Severity Level

V violation for failure to follow procedure.

Two examples:

a locked valve not locked

and

a fire watch

was

found

asleep,

(Example

two is

a fire- protection

violation, 87-35).

1.

Severity Level

V violation for failure to follow procedure,

Two examples:

shift relief turnovers

were not documented

and actions

were not documented

in the Plant Supervisor's

logbook.

(87-51)

m.

Severity

Level

V

violation

for

failure.

to

follow

procedures.

Three

examples:

AFW nitrogen

vent valve

was

mispositioned,

on three

occasions

a boric acid transfer

pump

discharge

pressure

indication

isolation

valve

was

mispositioned

and

an intake cooling water heat

exchanger

inlet isolation valve was not fully opened.

(88-07)

2.

Conclusion

Category:

3

Trend:

Improving

3.

Board Recommendation

During the first half of the

SALP period,

licensee

performance

was marginal

as

demonstrated

by

a

number of Severity

Level III

violations.

Recent

management

changes

have

had

positive

results.

This has

been demonstrated

by a number of conservative

actions to shut

down the plants or keep

them shut

down

so that

equipment

repairs

could

be

completed

to -help

-improve plant

reliability.

This action

has resulted

in an, improved operating

record

at

the

end of the

SALP period.

The

licensee

should

continue to address

the problems with procedural

adherence.

Radiological Controls

l.

Analysi s

During the assessment

period,

inspections

were performed

by. the

resident

and

regional

inspection

staffs.

There

were

four

12

regional

inspections:

two radiation protection

inspections,

a

radiological effluent inspection

and

a chemistry inspection.

The licensee's

health physics

(HP) and radwaste

staffing levels

were appropriate

and compared

well to other utilities having

a

facility of similar size.

During the

assessment

period,

the

staff consisted

of both

permanent

licensee

and

contract

HP

technicians.

The

permanent

staff

was

supplemented

with

corporate staff and contract technicians

during

nonroutine -or

outage

activities.

In general,

HP

foremen

and first line

supervisors

were

knowledgeable

of their authority

and assigned

duties within the radiation protection organization.

Vacancies

existed for an onsite

radwaste

supervisor

and

HP engineer.

The

licensee

was actively recruiting experienced

personnel

to fill

these positions.

As noted during the previous

SALP assessment

period,

a strength

of the radiation protection

program was the

low turnover rate

among the

HP staff positions.

The

knowledge

and experience

level of the site health

physics

staff was

good.

The licensee's

training program for radiation

protection activities

was well

defined

and

applied

to all

staff.

The

licensee's

health

physics

technician

training

program

has

been

accredited

by

INPO.

Improvements

in

the

general

employee

training

(GET)

were

reflected

in

improved

knowledge

of

HP

principles

and

practices

among

a

wide

cross-section

of

workers

interviewed

at

the

site

during

inspections.

Management

support

and

involvement

in

matters

related

to

radiation protection

and radioactive

waste

were

adequate.

The

health physics

supervisor

received

the support of other managers

at the plant in implementing

the radiation protection

program.

During the

assessment

period,

licensee

management

initiated

several

programs

concerned

with identifying

and

resolving

radiation protection

issues

at the facility.

However,

licensee

programs

designed

to

identify,

review,

track

and

resolve

radiation protection

issues

reported in audits,

incident reports

and

employee

concern

were not fully effective.

These

programs

were poorly organized,

did not

have

clear

lines of authority,

and the responsibility of several

quality assurance

groups

was

not clearly defined.

Details regarding the programs

were poorly

documented.

The

effectiveness

of

these

programs

for

identification of radiation protection

issues

at

the facility

was minimal.

The

licensee's

Performance

Monitoring

Section

(PMONS)

has

initiated

a

monitoring

program,

which

augments

the

audit

program.

Typically, activities monitored under

PMONS were of a

discrete

or one-time

nature,

such

as resolution of unresolved

items

or correction of identified

problems.'he

licensee

continued

the

upgrade

of the plant's

radiation

protection

procedures.

The

involvement of site

and

corporate

13

staff in the

procedural

upgrade

and the

comprehensiveness

of

their technical

reviews of procedures

by the site

and corporate

HP staff

were

less

than

adequate.

For

example,

a violation

concerning

inadequate

procedure

guidance for radiation controls

during

removal

and transfer

of reactor

coolant

system

(RCS)

spent filters

was

identified

during

the

assessment

period

despite

the fact that radiation controls for this activity had

been

previously

reviewed

earlier

in

the

assessment

period

following

an

event

which

exposed

workers

to high radiation

levels.

In addition,

procedures

did not require

documentation

of personnel

contaminations,

even in an instance

when extensive

decontamination

of an individual was required.

Licensee

action

in replacing

several

primary components

of the

post

accident

sampling

system

was

timely

and

demonstrated

licensee initiative in problem solving.

The licensee

did not effec.ively address

technical

issues

in the

radiation

protection

area

such

as electronic drifting of the

invivo counter.

The

licensee

did not

develop

complete

and

technically

sound procedures.

These findings,

combined with the

violations identified in the radiation protection

area

during

,the

assesment

period,

indicate

a decline

in what

had

been

in

previous

assessment

periods identified as

a strong,

aggressive

and

technically

sound

radiation

protection

program,

with

effective leadership

from management.

During

the

assessment

period,

the

licensee's

radiation

work

permit

and

respiratory

protection

programs

were

found to

be

satisfactory.

Control

of contamination

and radioactive materials within the

facility

was

generally

adequate.

At

the

beginning

of

January

1987,

approximately

27,000

square

feet (ft~) or

38% of

the radiation controlled area

(RCA), excluding containment,

were

controlled

as contaminated.

Although the licensee

had

a goal of

'reducing

the

area

contaminated

by

20% in . 1987,

the

actual

reduction

was less

than

12%.

At the

end of December

1987,

the

licensee

maintained

34% of the

RCA as contaminated.

This is the

largest

percentage

of any Region II facility.

Toward the end of

this assessment

period, the licensee

began

an extensive

upgrade

of the contaminated

control program including decontamination

of

plant

areas,

use of contamination

containments

and preventive

maintenance

of leaking valves.

As of July 15,

1988,

the total

area maintained

as contaminated

was reduced to 12,600 ft~ or

18%

of

the

RCA,

which

is still

greater

than

most

Region II

facilities.

The licensee

reported

437 instances

of personnel

contamination

in

1987,

of

which

186 events

were

identified

as

skin

contamination.

These

numbers

represented

an

increase

relative

to 1986,

when

a total of 257 contamination

events

were reported.

The higher

number of personnel

contaminations

was related to the

unscheduled

outage

work conducted

in 1987.

The total

number of

personnel

contaminations

for

1987

was

above

average

for

Region II PWRs.

The

1987 collective radiation

dose

was

645 person-rem

per unit

which

was

approximately

75io

above

the

national

average

of

368 person-rem

per

PWR.

The increased collective dose for 1987

was attributed to increase

outage activities.

A comparison of

Turkey Point radiation protection attributes

to Region II plant

averages

is listed in section

V.

K.

During this

SALP period,

the chemistry supervisory staff

had

been

reorganized

and administrative

programs

were initiated to

more

effectively

address

qualification

of

personnel

and

chemistry control.

A new training staff and training laboratory

had

been

provided;

however,

the

small

size

of the chemistry

staff continued

to

be

an

impediment to initating the training

program.

Also,

insufficient

personnel

resources

created

an

obstacle

to

upgrading

chemistry

procedures.

In

1984,

the

licensee initiated

a chemistry

improvement

program for upgrading

facilities, equipment

and analyses

for controlling chemistry in

the

secondary

water cycle.

This program

was in line with the

recommended

guidelines

of the

Steam

Generators

Owners

Group

(SGOG)

and

the

Electric

Power

Research

Institute

(EPRI).

Completion of the total

improvement

program

has

been

delayed

because

of assignment

of lower priorities as part of the Turkey

Point

Nuclear

Plant

Integrated

Schedule.

Completion

of the

secondary

chemistry

inline

monitors

is

scheduled

for

November

1991,

and

November

1992,

for

Units 3

and

4,

respectively.

Construction

of

a

new

secondary

chemistry

laboratory is scheduled for March 1992.

The licensee

continued to encounter difficulties in controlling

chemistry

because

of degradation

of condenser

tubes

and problems

associated

with the

equipment

conditions

of the

makeup

water

treatment plant.

Liquid radwaste

processing,

using

a contractor

and

a portable

demineralizer

system,

maintained

excellent

control

over

the

release

of

radioactive

effluents.

The

mixed

fission

and

activation

products

in

liquid

effluents

for

1987,

were

0.75 curies for both units,

which was consistent with previous

years

and less

than the 0.5 curies per unit industry aVerage for

PWRs

for

1983,

the

last

year for which industry

data

was

avai 1 abl e.

There

were

no significant changes

in the quantities of gaseous

effluent during this

SALP period

from previous

periods.

The

effluent releases

for the past three years

are

summarized

in the

Supporting

Data

and Summaries

Section

V.K.

The licensee's

quality assurance

program for the counting

room

was

adequate.

The

licensee

participated

in

a

quarterly

15

cross-check

program. with

a

vendor

whose

quality

assurance

program was traceable

to the National

Bureau of Standards.

As

part

of

the

NRC's

confirmatory

measurements

program,

the

licensee

analyzed

samples

for

selected

beta-emitting

radionuclides.

The

results

were

in

agreement

for tritium,

strontium-90

and iron-55.

The

maximum

environmental

radiation

doses

attributed to plant

relea'se

were

a

small

fraction of

10 CFR 20

and

10 CFR 50,

Appendix I limits and criteria.

Maximum total

body dose to

a

hypothetical

individual

from liquid effluents

was calculated to

be 0.0156

mrem per unit, which was

0.524 percent

of the

annual

limit.

Maximum

gamma

air

dose

and

beta

air

dose

to

a

hypothetical

individual from gaseous

releases

were less

than 0.2

percent of the annual limit.

During

1987,

the

volume of solid radioactive

waste

shipped

by

the

licensee

totalled

4,300 cubic

feet

(ft~)

containing

903 curies of activity.

This volume of waste

shipped offsite is

one of the

lowest of any facility in Region -II.

During 1987,

the licensee initiated the

use of a vendo'r to super

compact the

waste prior to shipment for burial.

Increased

decontamination

efforts for equipment

and material

leaving the

RCA, as well as

control of material

being

brought into the

RCA, resulted

in

a

significant

reduction

in radioactive

waste

volume relative to

1986,

when

approximately

11,420 ft~

were

shipped

containing

approximately '89 curies.

Three violations were identified:

a.

Severity

Level IV violation for failure to follow radiation

work permit

(RWP) requirements

(87-36).

b.

C.

Severity

Level

IV violation

for failure

to

properly

complete

a

manifest

for

a

radioactive

waste

shipment

(87-36).

Severity

Level

IV violation (four examples) for failure to

follow and

have adequate

procedures

(87-48).

Conclusion

Category:

2

Board Recommendations

Licensee

management

should

give continued

attention

to:

(1)

addressing

the continuing higher, than average

annual

collective

occupational

doses

and (2) efforts to reduce plant and personnel

contaminations.

In addition, licensee

management

should

assure

that

there

is

an

adequate

level

of

resources

and

support

provided to effectively deal with these

issues.

16

Maintenance

1.

Analysi s

During thi s

a'ssessment

peri od

inspections

were

performed

by

resident

and regional

inspectors.

Several

deficiencies

were

noted in the plant work order

(PWO)

process

during this

SALP period.

These deficiencies

included:

Numerous

items identified with deficiency tags in the field

were

not entered

in the

work control

system.

This is

caused

by the time lag

between

identification

and actual

entry intc the computer.

The indicated

number of

PWOs is artificially lower due to

the method of tracking them.

The unplanned

work orders

are

not entered into the

system until the planner

has completed

,

his portion of the

PWO.

Deficiency

tags

for

items

repaired

were left

on

the

component in the field even after the work was completed.

The

PWO job packages

were

weak in the

areas

of planning,

the

use

of machinery

history,

up to date

drawings

and

procedures,

and root cause

determination.

Assignment

of priorities

was

weak in several'nstances

where the item was not worked

when required.

This caused

inadequate

job

planning

which resulted

in

an

increased

workload

on

the

maintenance

staff.

Also,

priorities

continued

to

be 'changed

as

the

PWO

was

processed.

The

licensee

has

made

several

attempts

to

correct

this

deficiency

however,

the problem continues

to exist.

Late

in the

SALP period,

the licensee

instituted

a

new program

to

address

this

issue.

The

program

involves

more

operations

control

over the

assignment

of

PWO priority

during

a daily meeting

between

the Plant Supervisor

Nuclear

(PSN)

and the operations

coordinator.

The

program

appears

to

be working,

however,

since

implementation

was late in

the

SALP period, it is too early to accurately

assess

its

impact.

There

were

several

instances

where

PWOs

were

cancelled

without the originator's

knowledge or approval.

Normally,

cancellation

was

due

to

not

finding the

problem

as

described

on the

PWO.

This

has

caused

additional

PWOs to

be

generated

by

the

originator until

concerns

were

addressed.

.The

licensee

continues

to

have

a

large

number

of corrective

maintenance

PWOs',

approximately

1,000 at the

end of this

SALP

period.

Howeve~, this is

an

improvement

over

the

same

period

17

last year

which

showed

an

average

of about

1,800 corrective

maintenance

-PWOs.

It should

be

noted

that

the

reduction

in

PWO'

was

accomplished

by

better

management

of

available

resources

and not by increasing

the work force.

During previous

SALP periods,

a

reduction

in

PWO's

was also

noted

near

the

end of the period.

This was attributed to

a

temporary

increase

in the work force with contract

personnel.

Upon termination of the temporary help,

the backlog increased.

The

licensee

continues

to strive for maintaining

the total

PWO backlog in accordance

with the

INPO guidelines of having

no

more

than

50 percent of the corrective maintenance

PWOs greater

than three

months old. They normally meet this target criterion.

In order to reduce

the total

PWO backlog to

an acceptable

and

more

manageable

number,

the licensee

has

developed

several

new

programs

late in this

SALP period.

The first involves

a

team

developed

to resolve the la'rge

number of control

room deficiency

tags.

The team,

which was established

May 23,

1988, is center-

ing on repeat control

room deficiencies

to determine

and correct

the root cause.

The initial effort indicates

an

improvement,

a

reduction of about

60 deficiency tags

between

May 23,"

1988 and

June

30,

1988 (from about

255 to 195).

The

second

program

was

initiated

by the Electrical

Department

and has

shown

a dramatic

reduction

in the backlog of ready

to work

PWOs

since starting

the

program

on June

14,

1988.

Backlog

was reduced

from 206 to

about

65 at the end of this rating period

on June

30,

1988.

The

program

included:

discussions

with the

shop

personnel

as to

what constituted

backlog;

a status

board displayed

in the

shop

area listing all ready-to-work

PWOs

and graphs

tracking daily

progress;

and

a separation

of the department's

workforce into

crews being responsible for .their assigned

units (Unit 3, Unit 4

and

common).

Although this

concept

was

implemented

late

in

the

SALP period, initial indications are positive.*

Communications

between

Operations

and

Maintenance

Departments

have greatly improved during this

SALP period and Operations

i s

being treated

more

as

a customer of the Maintenance

Department.

The improvement

was due to a more in-depth Plan-of-the-Day

(POD)

meeting,

and the

POD document

containing:

work scheduled

for

the

current

day; priority items;

LCOs presently

in effect;

surveillances

due

and past due;

and other information pertinent

to daily plant operation.

In addition,

the

oncoming

Plant

Supervisor

Nuclear

(PSN) or Assistant

Plant Supervisor

Nuclear

(APSN) conducts

a briefing for their shift to update

the shift

for work planned

or in progress.

These

briefings

are

also

attended

by supervisors

from the other departments

so that all

departments

are working toward the

same goals.

18

The

licensee's

Analytical

Based

Preventive

Maintenance

(ABPM)

Program,

which was

implemented

during the last

SALP period to

augment

the Preventative

Maintenance

(PM) Program

has

proven to

be

an effective tool for predictive maintenance.

This program

initially started with vibration and oil analysis for pumps

and

motors,

and

was

recently

expanded

to

include

infrared

thermography.

The thermography

has

been

useful

in identifying

numerous

equipment

problems

throughout

the

plant

prior to

fai lure.

Examples

include:

the

location

and

repair

of

condenser

air

inleakage;

hot

spots

in electrical

equipment

caused

by

loose

electrical

connections

or

overload;

and

identification of valve seat

leakage.

An average

of 50 to

100

components

per month were analyzed

using thermography.

The original

Performance

Enhancement

Program

(PEP)

goal of 560

maintenance

and operations

procedures

was met

on April 1,

1988.

In addition,

the licensee

has

added

103

new. approved

PM proce-

dures

during this

SALP

period

and

the're

are

329 left to

complete.

The additional

procedures

are part of the

Enhanced

PEP currently scheduled for completion in May of 1993.

A recent audit in the area of performing

PMs indicated about

300

PMs past

due.

Increased

management

involvement rapidly reduced

the

number to 79 by late June

1988.

However,

continued

manage-

ment attention is required in the area of performing

PMs within

their required

schedule.

Maintenance-related

deficiencies

caused

two manual

reactor trips

and

one

automat,ic trip during this period.

This is

a marked

improvement over the last rating. period which attributed

eleven

reactor trips due to maintenance.

The two manual trips were both

associated

with Unit 3.

One

was initiated

due to

an

equipment

malfunction,

sticking electrical

contacts,

and

the

other

was

related to personnel

error that resulted

in multiple rod drops

during

a

shutdown.

There

were

a large

number of shutdowns

or

forced

power reductions

due to maintenance/engineering

related

deficiencies

(see

the

Outage

section

for

a

more

detailed

discussion

of outages).

The shutdowns

(4 for Unit 3 and

6 for

Unit 4)

and

load

reductions

(2 for Unit 3 and

9 for Unit 4)

were, for the most part,

due to equipment malfunction or failure

which could be attributed to poor design or material condition.

Increased

management

attention

is

needed

for

repetitive

equipment failure, in particular in the balance of plant area.

Examples

include the following.

The

pressurizer

spray

valves

have

caused

three

forced

shutdowns

due

to controller malfunction or

spray

valve

failure.

In addition,

a pressurizer

spray

valve failed

while Unit 3

was

in

Mode 3,

causing

a negative

pressure

transient

which resulted in partial discharge

of a cold leg

accumulator into the

RCS.

19

The

steam

generator

feedwater regulating valve to actuator

coupling

has

caused

two

forced

power

reductions

to

facilitate repairs.

The turbine control oil system for Unit 4

has

caused

one

shutdown

and

several

load

reductions.

Unit 3

has

been

relatively free of problems with the oil

system

since

a

major

cleaning

was

accomplished

during

the

last

SALP

period.

The

licensee

completed

replacement

of all intake cooling

water

( ICW)

pump

couplings

during this period after

a

failure required

a load reduction.

However, the

ICW system

continues

to remain

a large

maintenance

item,

accounting

for increased

time in

LCOs.

Major problems

include

heat

exchanger

fouling caused

by calcium carbonate

buildup

and

strainer

plugging

caused

by marine

growth.

The

Amertap

system

was installed in Unit 4 late in this

SALP period and

should

reduce

the

heat

exchanger

fouling

problems.

Increased

attention

should

be

focused

on the

ICW strainer

problems

and future heat

exchanger

replacement

or retubing.

As mentioned

in previous

assessments,

the

area

radiation

monitor

system

(ARMS)

and

the

process

radiation

monitor

system

(PRMS),

continue

to

have

numerous

problems.

The

PRMS

failures

of

R-11

and

R-12

have

resulted

in

the

initiation of

seven

LERs

due to containment

and control

room ventilation

system

isolations.

The

system

drawers

were replaced

with new upgraded

drawers

during this

SALP

period (Unit 3 on November 5,

1987,

and March 24,

1988 for

Unit 4)

and

this

has

resulted

in

improved

system

performance.

However, the series circuit type power supply

for the system,

which has also caused failures,

has yet to

be corrected.

The licensee

currently plans to modify the

power supply in August 1988.

Personnel

errors continue to remain

a problem,

as indicated

by the violations identified't the

end of this section.

The licensee

is improving in this area,

as evidenced

by the

reduced

number of

LERs in the

maintenance

area attributed

to personnel

error, versus

equipment malfunction.

However,

continued

licensee

emphasis

is required

on

the

need for

attention

to

detail

and

individual

accountability

as

indicated

in the following- additional

examples

related to

personnel

error:

Not knowing the effects .of pulling certain

CROM fuses

caused

multiple rod drops

which required

a

manual

reactor trip.

Use

'of

carbon

steel

gauge fittings in

a

seawater

system

caused

an

ICW pump to be placed out of service

and entrance

into TS 3.0. 1.

20

An improperly installed

RCP shaft

shim contributed to

a uni-t shutdown

during startup

and

increased

outage

time.

A review of the safety

system failures for the units indicated

that they were slightly above

the national

average

for older

plants of this type during this

SALP period.

However, only one

failure could be attributed to

a maintenance

related deficiency,

which concerned

the failure of an

ICW pump coupling previously

di scussed

in this section.

The licensee's

approach

of resolving technical

issu'es

by using

Event

Response

Teams

(ERTs)

has

continued to

be

a useful tool

for identifying and resolving the root cause of a deficiency.

A

total of 23

ERTs

were initiated during this assessment

period,

some of which were for multiple problems.

One

ERT concerning

the multiple failures of the

125

VDC battery chargers identified

an

inadequate

component

provided

by the vendor during circuit

modifications.

This deficiency

was not initially recognized

by

the vendor

and its identification was not only a benefit to the

licensee

but also to the industry.

The

new maintenance

building was

completed

during this assess-

ment period.

This should aid in improving maintenance

trends

by

centrally locating all maintenance

disciplines.

Three violations were identified.

(Two additional

maintenance

related

violation

examples

are

identified in

the

Operations

section):

a.

Severity

Level

IV violation for failure to

report to

management

a pin hole leak

on

an

AFW steam line.

(Unit 4

only, 87-33)

b.

Severity Level

IV violation for improper fuses installed in

the reactor

safeguards

protection circuitry.

(87-39)

c.

Severity

Level

IV violation with two examples:

failure to

perform

a functional test

on

an instrument

loop

and the

improper installation of a check valve.

(87-39)

2.

Conclusion

Category:

3

Trend:

Improving

3.

Board Recommendations

The

Board recognizes

the

improvements

made

in the maintenance

area

but remains

concerned with the significant number of plant

equipment

problems

that

have

not

been

repaired

through

the

corrective

maintenance

program

or are

overdue

for preventive

21

maintenance.

Additional licensee

management

and

NRC attention

in thi s area is recommended.

0.

Surveillance

Analysi s

During the evaluation period, routine reviews of the operational

surveillance

testing

program

were

conducted

by

the

resident

inspector

staff.

Regional

inspectors

reviewed

surveillance

testing

in the

areas

of fire protection,

chemistry,

-and

core

physics testing.

During the last

SALP period, the majority of the missed

survei 1-

lances

were

caused

by

a

poor

surveillance

tracking

program.

The

licensee

corrected

that

problem with

an

improved

manual

tracking

system,

but during this

SALP period

nine

LERs

were

generated

as

a result of survei lian"es.

Personnel

error caused

four missed

survei 1 lances.

These

were in the area of failure to

perform the

scheduled

surveillance.

The other five

LERs were

due to inadequate

procedures,

and resulted

in failed or missed

survei llances.

The violations listed

below

concern

missed

TS

survei llances.

However, the root causes

for each

were different:

violation b

was

due to misinterpretation of the applicable

mode for the test

performance;

violation

a concerned

TS interpretations

and

was

a

result of the licensee's

decision to omit, rather than meet,

the

TS requirement

for sampling

the safety injection accumulators;

violation c

was

due

to operations

personnel

anticipating

the

return

to service

of the

EDG before

the

TS time limit for

testing

the other

EDG expired;

and violation d was

a result of

an inadequate

surveillance tracking program.

The

~ Quality

Control

(QC)

surveillance

gro'ups'eview

of

completed test procedures

and testing activities

was evident by

the low frequency of missed

survei llances.

This is due to the

group surveillance tracking program.

The licensee

has developed

a computerized

surveillance tracking

program,

which is scheduled

to.be

implemented

in July 1988.

The

major benefit

of this

program will

be

to

reduce

manpower

necessary

to track

survei llances.

QC surveillance

personnel

should

be

able

to witness

more test activities

instead

of

reviewing

documentation.

The

surveillance

tracking

program

currently

in

use

will

be

run

in parallel

with the. new

computerized

system until the

end of

1988.

This will ensure

that the

new

system is able to track the survei 1.lances

as well

as the current

system.

The

Procedure

Upgrade

Program

(PUP)

has

continued

to improve

existing

surveillance

procedures

to

increase

the

quality,

content

and to aid in reducing

personnel

errors.

In general,

22

the surveillance

procedures

were technically accurate

and well

written.

Some difficulties resulted,

as

expected,

with the

upgrade

and

generation

of

new

surveillance

procedures.

Personnel

performing

testing

have

encountered

some

minor

difficulties with the

new procedures,

especially

during

the

initial

use.

However,

management's

policy

of

verbatim

compliance to procedures

has helped to avert problems.

When the

procedures

have

been unclear or technically inaccurate,

the test

personnel

have

stopped

the test to

seek

a change/clarification

to the procedure.

Test

personnel

routinely exhibited conservative

approaches

to

'resolving

safety

significant issues

and were

knowledgeable

of

the surveillance

they were performing.

Management

involvement

in assuring

quality

was

evidenced

by the

low occurrence

of

procedural

noncompliance

related

to

surveillance

testing.

Additionally,

the

surveillance

records

were

complete,

well

maintained

and

readily

available

for review.

However,

the

licensees

poor

management

of the

surveillance

schedule

was

reflected

by the routine

use of TS allowed grace

periods.

An

example

of this

was

the

Unit 3

and

4

containment

tendon

surveillance.

This surveillance is performed every

5 years

and

was last performed in early 1982.

The licensee

had not started

the tendon surveillance until May 1988, with the Unit 3 end of

grace period expiring June

30,

1988,

and the Unit 4 end of grace

period expiring July 31,

1988.

The surveillances

were completed

on

time but

the

licensee

utilized

almost

the entire alloted

grace period. If an

unforeseen

problem would have arisen,

the

licensee

would not

have

had sufficient margin to complete

the

surveillance within the allowed

TS time limits.

The most recent post-refueling startup tests

on both units were

satisfactory.

They

were

representative

of good technique

and

attention to detail, which indicate

an understanding

of the test

and

a

sound

and thorough

approach

toward performance

of these

,

required activities'he initial criticality for both

units

showed

a reactivity overshoot.

This could

have

been

avoided

with an improved procedure

and/or

a

more conservative

approach

toward 'restart.

One inspection

on heat tracing records

and procedures

identified

a weakness

concerning

a lack of

. review of surveillance

records

by management.

When brought to the attention

of the l.icensee,

the

data 'was

immediately

checked

by performing

retests

and

verified to be adequate.

Four violations were identified:

a.

Severity

Level

IV violation for failure to 'perform the

boron concentration

analysis for the

4C accumulator (Unit 4

only', 87-35).

23

b.

Severity

Level

V violation for failure to

perform the

monthly surveillance

on Unit

3

spent

fuel pit

exhaust

monitors (Unit 3 only, 87-27).

c.

Severity

Level

V

violation

for failure

to

verify

operability

of the

B emergency

diesel

generator

when

the

A diesel

was out of service (87-35).

d.

Severity

Level

V violation

for failure

to

perform

surveillance test

on electric fire pump (87-42).

Conclusion

Category:

2

Board Recommendations

None

E.

Fire Protection

Analysi s

During this assessment

period, inspections

were conducted

by the

regional

and resident

inspection staff to review the licensee'

implementation of the fire protection

program

and follow up

on

previously identified enforcement

matters.

The

licensee

has

issued

revisions

to

procedures

for the

administrative

control

of fire

- hazards

within

the

plant,

surveillance

and maintenance

of the fire protection

systems

and

equipment,

and

organization

and training of the

plant fire

brigade.

These

procedures

were

reviewed

during

the staff

inspections

and found to meet

NRC requirements

and guidelines.

The

inspectors

also

reviewed

the licensee's

implementation

of

the

fire

prevention

administrative

controls.

General

housekeeping

and control of combustible

and

flammable materials

in safety-related

plant

areas

were

found to

be satisfactory.

The fire extinguishing

systems, fire detection

systems,

and fi, e

barrier

assemblies

protecting plant

systems

required

for safe

shutdown were found to be functional.- In addition, the surveil-

lance

inspections,

tests

and

maintenance

instructions for the

plant fire protection

systems

were found to be satisfactory

and

met the criteria of the plant Technical Specifications.

The fire protection/prevention

annual audit, triennial audit and

audits

conducted

to

verify

implementation

of

10 CFR 50,

Appendix R,

requirements

were

reviewed.

These

audits

were

conducted

within the specified

frequency

and

covered all the

essential

elements of the fire protection program.

These audits

covered procedures,

fire brigade organization

and training,

and

fire protection

systems

and housekeeping.

The audits identified

minor discrepancies.

None of the audit findings were of major

safety

significance.

The

licensee

has

implemented

the

corrective actions for discrepancies

identified by these audits.

During

a

design

basis

review, it

was

determined

that

insufficient

emergency

power

exists

(assuming

worst

case

accident

design basis) to operate air conditioning units in the

battery

charger

rooms.

Consequently,

fire doors

have

been

required to be propped

open for the past year along with the use

of portable

fans, to assure

adequate

ventilation during accident

conditions.

One fire door requires that

a continuous fire watch

be present

to shut the door

under certain circumstances.

Twice

in

the

past

year,

individuals fulfilling this

compensatory

action

have fallen

asleep.

This

haq resulted

in examples

of

violation

h and

k of the Operations

section.

The

management

involvement

and control in assuring

quality in

the

fire

protection

program

was

evident

due

to

the

well

developed,

issued

and implemented fire protection administrative

procedures'he

licensee's

approach

to resolution of technical

fire protection

issues

indicated

an understanding

of issues,

and

was

sound

and timely.

The

responsiveness

to

NRC initiatives

were generally timely and thorough.

When violations did occur,

effective corrective action

was promptly taken.

Fire protection

related

events

and discrepancies

identified by the licensee

were

properly analyzed,

promptly reported,

and effective corrective

actions

were taken.

Staffing

for

the

fire protection

program

is

adequate

to

accomplish the goals within normal work'hours.

The fire protec-

tion staff is identified,

and authorities

and respons'ibi lities

are clearly defined.

Personnel

appear. well qualified for their

assigned

duties.

The organization,and

staffing of the plant

fire brigade

met

NRC guidelines.

The training

and drills for

the

brigade

members

met

the

frequency

specified

by

the

procedures

and

NRC guidelines.

One violation was identified.

Severity

Level

IV violation for inadequate

procedure

for the

control of deluge isolation valve positions (87-33).

2.

Conclusion

Category:

2

3.

Board Recommendations

None

F.

Emergency

Preparedness

Ana lysi s

t

25

During

the

assessment

period,

inspections

were

performed

by

resident

and

regional

inspection

staffs.

These

included

an

annual

emergency

preparedness

inspection,

and

an

emergency

response facilities

(ERF) appraisal.

One revision to the Turkey

Point Radiological

Emergency

Plan

(REP)

was

submitted for

NRC

review.

The

emergency

program

inspection

and

ERF appraisal

disclosed

that the licensee

has

the capability to promptly identify and

correctly classify

emergency

events,

and

implement

the

key

elements

of the

REP

and respective

procedures

in

response

to

emergency

events.

The

annual

radiological

emergency

preparedness

exercise

was

not evaluated

duri ng this assessment

period;

however,

the effectiveness

of the

ERFs

were evaluated

during the exercise.

No significant findings, other

than

those

discussed

below, were identified during either the appraisal

or

related

interviews

of emergency

response

personnel

regarding

adequacy

of

the

licensee's

emergency

response

program

and

faci 1 ities.

Malkthroughs

with shift

supervisors,

performed

during

the

inspection,

disclosed that the licensee

continued to demonstrate

the

capability

to

promptly identify

and

correctly classify

emergency

events

consistent

with

the

current

REP

and

implementing

procedures.

The shift supervisors

were cognizant

of their authorities

and responsibilities

regarding

accident

assessment

and

protective

action

decision-making,

including

onsite

protective

measures

and

recommendations

appropriate

to

offsite protection.

Additionally,

the

inspection

identified that

the

following

emergency

programmatic

elements

were adequate:

notification and

communications;

shift staffing and augmentation;

emergency

plan

and

implementing

procedures;

emergency

facilities

including

equipment,

instrumentation,

and

supplies;

emergency

response

organization

and

management

control; training;

and

independent

'reviews

and audits.

The

ERF appraisal

performed during this period included detailed

review

and

evaluation

of the

onsite

meteorological

facility,

Control

Room,

Technical

Support

Center

(TSC),

Emergency

Operations

Facility

(EOF),

and all

emergency

equipment

and

supplies,

provided therein.

.The appraisal

disclosed

that

ERF

equipment

and

supplies

were

adequate

to

support

response

to

emergency

events.

The emergency

program evaluation

and the

ERF

appraisal

also

confirmed

management's

continued

attention

to

maintenance

of an effective

emergency

preparedness

program

and

provision

of

emergency

facilities

required

to

implement

the

program.

The following findings,

were

disclosed

which

could

'esult

in nonconservative

dose

estimates

following an offsite

radioactive release:

(1) failure to

use

required

time-averaged

meteorological

data

( 15

minutes)

defined

in

the

emergency

procedure

addr essing

offsite

dose

calculation

and failure to

26

inform

Control

Room

personnel

of

changes

made

at. the

meteorological

tower

regarding

delta

temperature;

and

(2) failure

to establish

and

implement

a

computer

software

control procedure

to ensure

maintenance

and control of the Class

A Model

Dose Assessment

computer.

Two violations were identified.

a.

Severity

Level

IV violation (two examples)

for failure to

use required time-averaged

(15 minutes) meteorological

data

as

defined

in

the Offsite

Dose

Calculation

Emergency

Procedure,

and for failure to inform Control

Room personnel

and reflect respective

change to Control

Room analog chart

records

of hardware

changes

made to meteorological

tower

equipment

addressing

delta temperature

(88-01).

b.

Severity

Level

IV violation for failure to establish

and

implement

a

computer

software control

procedure

to ensure

maintenance

and control of Class

A Dose Assessment

Computer

Model (88-01).

2.

Conclusion

Category:

2

3.

Board Recommendations

The

SALP rating

should

not

be

construed

as

representing

a

dramatic

reduction

in performance

but is indicative of needed

improvement to reach

the level of excellence

achieved

in the

past.

During the period,

problems

were identified in this area

which

indicated

that

more

aggressive

action

is

needed

in

striving for an excellent

program.

Security

and Safeguards

1.

Analysi s

Inspections

were

performed

by the resident

and regional staff.

Additionally, security

wa.

discussed

with the

NRC during monthly

management

meetings

held onsite.

The licensee

had established

a program to upgrade

the security

systems,

barriers,

and

computer.

This effort is part of the

integrated

schedule

and is currently estimated to be complete in

1992.

The

licensee

had

dedicated

four

employees

to

the

maintenance

of the

system until the

upgrade

can

be completed.

There

has

been

some

progress

in maintenance

late

in the

SALP

period.

Recently,

a guard force captain

was detailed to track

maintenance

and related

compliance issues'wo

projects related

to the

upgrade

program

are

near

completion,

the

new Contractor

Entrance

Building and the vehicle

entrapment

and

search

area.

With regard to both of these projects,

a weakness

has

been

shown

27

on the part of the security organization to recognize

regulatory

requirements

and to manage

the program upgrade effectively.

The

Contractor Entrance Building work required

a reconfiguration

of

the protected

area barrier,

alarm and surveillance

systems.

The

licensee failed to implement compensatory

measures

and to timely

submit

the

required

security

plan

change.

This failure to

implement

regulatory

requirements

was

not

recognized

by

the

licensee,

but

was identified by the Senior Resident

Inspector.

'everal

layers

of security

management

had

an opportunity to

recognize

this

problem

and failed to do

so.

Subsequently,

a

failure

in

communications

within

the, Security

Department

precluded

the prompt implementation of compensatory

measures.

Work

on

the

vehicle

entrapment

area

was

initiated without

consideration

of

the

necessary

regulatory

requirements;

compensatory

measures

are

currently

in

place

while

an

engineering

redesign is accomplished

to ensure

conformance

with

the

Physical

Security

Plan.

Late in the

SALP period,

the Site

Security

Superintendent

was

assigned

to oversee

the

upgrade

program.

Weaknesses

in the security program

have continued to prevai

1 in

this

SALP period

as indicated

by the

number of violations.

The

violations

continue

to

be repetitive

in nature,

involving

a

failure of the guard force to implement the security program,

an

inability of security

personnel

and

supervisors

to

recognize

violations and

a lack of management

oversight..

These violations

included escalated

enforcement

in the areas

of access

control,

compensatory

measures,

and

the

control

of

Safeguards

Information.

The

licensee

continues

to

show

a

lack

of

initiative in self-identification

of

problems

but

remains

responsive

to

NRC initiatives.

The

1 icensee'

Security

Department

has

failed

to

take

responsibility for the complete security program

and associated

program

problems

and

solutions.

This

was highlighted

by the

licensee's

inaccurate

responses

to

escalated

enforcement

violations.

Statements

were

made to the inspectors

while onsite

and later in an

enforcement

conference

that were not accurate.

More

inaccurate

statements

were

'sent

to

the

NRC

in

the

licensee's

response

to the violations.

This

necessitated

the

licensee

to submit revised

responses

to Reports

87-38 and 87-47.

The

inaccurate

information

can

be attributed to the security

management failing to verify data,

dates,

and

causes,

prior to

providing the

information to other organizations

within FPKL,

which formulate the formal responses

to the

NRC.

In one

case,

Security Management

stated that

a preventive

maintenance

program

had

been

implemented

when in fact no program was

implemented

and

the

hardware

which

had initially failed was

found to

be in

a

failure mode again.

28

The mindset

appeared

to

be

one of writing a response,

handing

responsibility to another

licensee entity to implement

and then

failing to follow up to

see if the other entity

had

performed

the

work necessary

to

ensure

reliable

operation

of security

equipment.

. Ownership

of

the

security

program

was

poorly

managed.

Although

the

licensee

has

made

extensive

plans

to

upgrade

security

facilities

program

and

systems

and

has

provided

additional training

and manpower resources,

these

measures

have

not yet

been

implemented

or have failed to

be effective.

As

di scussed

previously,

the security force failures

and lack of

regulatory sensitivity at all

levels

of the

security

force,

demohstrate

that

although all

members

of the force

have

been

trained,

the

training

management

of

the

force

has

been

ineffective in ensuring

compliance with regulatory requirements

during most of the

SALP period.

Recently,

licensee

corporate

and plant management

have

begun to

provide

support

to the

security

program.

Monthly management

meetings

between

high level licensee

and

NRC management

include

security

program

issues

on

the

agenda.

The

licensee

has

directed

substantial

resources

to improvement of the

security

program

shown by the upgrade

program

and hiring of new managers.

However,

these efforts

have

had limited improvement during the

current

SALP

period.'he

licensee

has

made personnel

changes

in the positions of Site

Security

Superintendent,

Site

Security

Manager

and Assistant

Site Security

Manager

and

had

added

one onshift

FP&L security

supervisor,

with four more scheduled

to be hired.

These

changes

came too late in the

SALP rating period to have

an impact

on the

current analysis.

Seven violations were identified during this rating period.

Severity

Level III violation

for failure

to

maintain

positive

access

control,

six

examples:

fai lure

,to

adequately

control access

to the protected

area; failure to

adequately

control

access

to

the

Unit

4

containment

personnel

hatch; failure to adequately

control

access

to

the Unit 3 containment

equipment hatch; officer sleeping

in

defensive

tower; failure to adequately

control

access

to

the

protected

area;

and

an officer leaving

a vital area

compensatory

post without proper relief.

(87-38)

b.

Severity

Level III violation for failure to recognize,

properly mark and protect Safeguards

Information-.

(87-38)

c.

Severity

Level

IV violation for inadequate

protected

area

lighting.

(87-47)

29

d.

Severity

Level IV violation for inadequate

search of vital

area prior to revitalization.

(87-47)

e.

Severity

Level

IV violation for inadequate

compensatory

measure.

(88-03)

f.

Severity

Level IV'iolation for inadequate

protected

area

barriers.

(88-03)

g.

Severity

Level

IV violation for inadequate vital area

alarm

testing.

(88-03)

Conclusion

Category:

3

3.

Board Recommendations

The licensee

has finally given attention

and

resources

to the

security

area,

but continued

to perform at

a category

3 level

during this

SALP period.

It wi 1 1 take

continued effort by the

licensee

to improve performance.

H.

Outages

Analysis

During this evaluation period, inspections

were conducted

by the

resident

and regional

inspection staff.

At the beginning of the

period,

both Units

3

and

4 were in the

shutdown

mode.

Unit 3

entered

a scheduled

refueling outage

on March 11,

1987.

Unit 4

entered

an

extended

outage

on

March 13,

1987,

to repair

corrosion

caused

by boric acid buildup from

a conoseal

leak

on

the vessel

head.

Both outages

were extended to allow extensive

replacement

of environmentally qualified

(Raychem)

electrical

splices

inside

the

containments.

Additionally,

the

Unit 4

. outage

was

extended

in June. 1987 to allow for replacement

of

defective

piping

in

the

post

accident

hydrogen

monitoring

system.

There were four region based

inspectiohs

performed of activities

defined

as Outage related.

The first arid third inspections

were

primarily to review the licensee's

response

to

NRC open

items

including Bulletin 83-06; the

second inspection

was

a review of

primary coolant

system

pressure

isolation (Event V) valves

and

the

pump and valve inservice test (IST) program

and procedures;

and the fourth inspection involved the status of the licensee's

corrective action in response

to Bulletins 79-02 'and 79-14.

The

inspectors

found that

the

level

of management

awareness

and

initiative varied

from adequate

to excellent

depending

on the

particular issue.

Resolution of technical

issues

also varied in

the

same

areas

depending

on which part of the

company

had the

lead in developing

the resolution (e.g.,

the resolution of the

30

problems

associated

with, material s

supplied

by

GULFALLOY

[Bulletin 83-06j

was

handled

in

an

excellent

manner,

while

resolution

of

issues

involvi'ng

Event

V valves

and

the

IST

program were only average).

Throughout this

assessment

period,

there

were

numerous

forced

outages

due to equipment failure caused

by design or maintenance

deficiencies.

There were

a total of eight non-refueling

outages

for Unit 3 and six for Unit 4 during this period.

When required

to enter

a forced

outage

of significant duration,

the licensee

utilized their

Short

Notice

Outage

Work

(SNOW) list, which

identifies all

maintenance

items

requiring

a

shutdown.

New

maintenance

items identified during power operation that require

a plant shutdown to repair are continuously

added to this list.

During this evaluation

period,

a positive

change

in management

philosophy

was

noted in that the

emphasis

is

no longer being

placed

on meeting

startup

schedules

at the

expense

of

needed

maintenance.

This philosophy change

has

been

observed

since the

fall of 1987.

During subsequent

outages,

a

good

number of the

maintenance

activities

were

being

performed

to

enhance

the

physical

condition of the plant

and

not

because

they

were

requi red to return the unit to service.

This

change

in philosophy

has

produced

a

more reliable plant

during the latter part of the period,

as

noted

by the

improve-

ments

in availability

of the

units.

Several

examples

of

extending

outage

times are discussed

below.

The forced outages

demonstrated

adequate

planning

and scheduling

through

use of the

SNOW list and daily meetings to discuss

work

progress

and critical path issues.

One weakness

in the area

of

personnel

accountability

and responsibility was noted.

This has

resulted

in extending

equipment

down

times

due

to

no single

individual

assuming

responsibility

and following up

on delays.

An example

was the recent installation of the Amertap system

on

Unit 4

ICW/CCW heat

exchanger s.

Some changes

in accountability

and responsibility

'were

noted

late

in the

SALP period,

due

mainly to the

new Plant

Manager's

increased

emphasis

in this

area.

Unit 3 encountered

numerous

material

problems

during the first

part of the period,

which required

forced

shutdowns

to repair

defective

equipment.

In August of 1987, while coming out of the

refueling

outage,

a

leak was identified in the inner reactor

vessel

o-ring seal.

A conservative

management

decision

was

made

to correct

the deficiency,

although

plant operation

was

not

disallowed by Technical Specifications.

The repairs

added about

two weeks

to the

schedule

and

required

reactor

vessel

head

removal.

In

September

1987,

the

unit

experienced

one trip

and

one

shutdown

due to equipment malfunction.

During the outages,

the

31

faulty equipment

was repaired,

which included the reinstallation

of

RCP

3B

shim that

was

installed

incorrectly

during

the

previous

outage

due to personnel

error.

Additional events that

occurred

during

the

outage

that

resulted

in

an

extension

included:

repair of

RHR leaks,

motor,

and

pump;

seal

table

leakage

repair;

containment

purge valve repair';

RPI repair;

and

replacement. of

RHR recirculation

lines,

which

was

a generic

concern identified by the licensee.

There

were two short forced outages

in December

1987; the first

to repair

a stuck

open pressurizer

spray valve

due to control

circuit malfunction,

and the

second to repair

a defective relay

in the turbine generator

overspeed

protection circuitry.

Again

in January

1988 there

were

two forced outages,

one to balance

the

main turbine

due to excessive

vibration

and the other to

correct

pin engagement

on

CROM connectors.

The latter caused

a

dropped

rod and

an eventual

manual trip due to personnel

error

in removing the

CRDM fuses- for testing

(see violation

h in the

Operation

Section).

While preparing

to return

the

unit to

service

the

licensee

was performing

a leak inspection

of all

accessible

areas

inside the containment

and

found

a

small

leak

in

a

CROM canopy

seal

weld.

The leak inspection

was instituted

by management

as

a result of the conoseal

leak discussed

in the

last

SALP report.

Repair of the canopy

seal

extended

the outage

39

days

and

showed

effective

preplanning

in that

welders

practiced

on

a non-radiated

reactor vessel

head at Westinghouse

headquarters

prior to performing the repair to conserve

man-rem

and provide experience

in this type of repair.

The repair work

was documented

by the licensee

on, video tape

and distributed to

other

plants

in the

industry that

may

experience

this

same

failure, thus providing

a free flow of information throughout

the industry for newly identified problems.

In addition,

the

licensee

installed

a radiation monitoring

system

in the

upper

head

region during this outage

to detect future leaks in this

area.

Two short

outages

were required

in March 1988

and

were

caused

by balance-of-plant

(BOP) failures.

One

was

due

to

failed welds in a moisture separator

reheater

(MSR) baffle plate

and the other

was

due to a condenser

tube rupture.

In the

MSR

repair,

the licensee

again

showed conservatism

by inspecting all

other

MSRs and repairing questionable

welds even

though only one

MSR had failed.

Unit 4

also

required

several

forced

outages

throughout this

period

due mainly to

BOP failures.

Two short outages

occurred

in July and

September

of 1987 to repair

a condenser

tube leak

and

a

condenser

vacuum

leak.

In October

1987

the unit was

.

placed

in cold

shutdown

as- a precautionary

measure

due to

a

hurricane

warning.

Several

maintenance

items were accomplished

during this

shutdown

which extended

the outage,. including the

replacement

of the

RHR recirculation line,

several

major valve

and actuator

repairs,

and recovery

from high chlorides

in the

CCW system.

In February

1988,

the unit was in a forced outage

due to

a

common

mode failure of the battery chargers.

An

ERT

32

was initiated to determine

the root cause of the failures.

The

ERT identified that the vendor was supplying replacement circuit

cards with capacitors

that were not suited for this application.

This resulted

in the selection

of replacement

capacitors

that

benefited

others

in the industry using this type of charger

as

well as the licensee.

The unit required

two forced

outages

in April 1988 to repair

a

turbine generator'control

oil leak,

due to a failed weld caused

by

a

vendor

manufacturing

deficiency,

and

to

repair

a

pressurizer

spray valve leak.

During the

outage

to repair the

turbine generator

failed welds,

the licensee

rewelded all the

control oil lines that were susceptible

to this failure,

and not

just the failed weld.

During repair of the pressurizer

spray

valve

leak, 'he

licensee

opted

to

extend

the

outage

to

facilitate partial installation of the

Amertap

system

on

the

ICW/CCW heat

exchangers.

This installation

could

have

been

accomplished

with the

unit

on line,

however

the

licensee

accomplished it during the outage to prevent entering

an

LCO if

performed while at power.

In addition,

a design

deficiency in

the

containment

purge

valve air

supply/discharge

lines

was

identified and corrected.

Conclusion

Category:

2

Board Recommendations

None

I.

Quality Programs

and Administrative Controls Affecting Quality

Analysi s

During the assessment

period,

inspections

were conducted

by the

regional

and resident

inspection staffs

on

a routine basis.

For

the

purposes

of this assessment,

this area

is defined

as the

ability of

the

licensee

to identify and correct their

own

problems.

It

encompasse's

all

plant activities,

all

plant

personnel,

as well

as

those

corporate

functions

and personnel

that provide services

to the plant.

The plant

and

corporate

Quality Ass'urance

(QA) staffs

have responsibility for verifying

quality.

The rating in this area specifically denotes

results

for various groups in achieving quality as well as the

QA staff

in verifying that quality.

The plant

QA organization

is divided into two sections.

The

Regulatory

Compliance

Section

and

the

Performance

Monitoring

(PMON) Section.

The Regulatory

Compliance

Section

consists

of

ten auditors

with experience

in various disciplines

such

as

chemistry,

health

physics,

training,

design,

metallurgy,

and

instrumentation

and controls.

This Section is responsible

for

33

performing the traditional

QA audits.

This includes,

but is not

limited to,

audits

of

TS,

QA program,

Emergency

Plan,

plant

procedures

and

verification

of

accuracy

of

licensee

correspondence

to

the

NRC.

An

improvement

in this Section

included

conducting

audits

on "real-time" ,plant

issues.

This

has

helped to identify problems

as they occur,

which results in

more timely resolutions.

Another improvement is the involvement

of

QA

personnel

with the

Event

Response

Teams

(ERT).

QA

personnel

have

been

involved

in

providing

technical

and

regulatory/quality

inputs for various

ERTs including:

failure

of containment

purge valves;

high chloride concentrations

in the

CCW; formation of voids in the Unit 4 reactor vessel

head during

a cold shutdown condition;

4B and

4C

ICW pump failures;

and

MSIV

nitrogen

backup regulator discrepancies.

The licensee

is also

implementing Vertical Slice Audits (VSA);

VSAs are

intended

to

evaluate

the

operational

readiness

and

design

basis

functionality of

selected

plant

systems.

The

QA

Guidance

Document

was

issued

in March 1988,

and

a

VSA on the

ICW system

was

commenced

in early July 1988.

.The

VSA will be

an

ongoing

program

and the licensee

plans to conduct

VSAs for at least

two

systems

per year.

Audits

by

the

Regulatory

Compliance

group

have

resulted

in

several

LERs

being

issued

by

the

plant

concerning

fire

protection,

diesel

fuel oil sampling

and rotation

of battery

pilot cells.

Another audit identified problems with the control

of non-fuel special

nuclear material

(SNM) prior to issuance

of

Information Notice 88-34, which expressed

similar concerns.

The

PMON

section

currently

consists

of

nine

auditors

that

provide more of a Quality Control

(QC) role by monitoring plant

operation,

maintenance,

and

root

cause

analysis

on technical

issues.

Improvements

in thi s area

include dedicating

an auditor

to

monitor

balance

of

plant

(BOP)

activities.

Events

investigated

thus far include:

Unit 3 condenser

tube failure;

Unit 3 moisture

separator

reheater

(MSR) internals failure; and

the Unit 4 guarded oil

system

leak.

Instituting

a dedicated

auditor will help provide

a quality perspective

in determining

root causes

for

BOP

system

problems.

PMON

has

also

provided

support

to operational

enhancements

such

as

the

computerized

clearance

system,

computerized

surveillance tracking program

and

also

the centralized

scheduling

organization.

The

PMON group

activities

have

generated

numerous

findings

including:

operation of the waste

gas

system in an alignment not addressed

in the Final Safety Analysis Report

(FSAR);

and

LERs 250/87-25

and

87-28

which involved

mi ssed

surveillance

of control

rod

positions verification and undocumented

surveillance

of ,coolant

loop operability.

Based

on

the

review of

the

QA

Department

audit

findings,

schedules,. corrective action requests

and other site activities,

it appears

that the

QA Department is conducting timely, thorough

and technically.

sound reviews of site activities.

34

The

Regulation

and

Compliance

Group

(Licensing)

has

provided

effective

support

to plant departments

for interpretations

of

regulations

and

Technical

Specifications.

In addition, thi s

group

has actively participated in the review of the revised

TS

project with

NRR

and

has

supported

Region II. personnel

in

resolving

and

closing

approximately

900

open

items.

The

Regulation

and Compliance

Group continues to demonstrate

an open

and effective interface with

NRC inspectors,

which facilitates

the resolution of issues that arise.

The licensee

was able to identify and correct problems relating

to safety

as evidenced

by the following actions:

The

establishment

of

a Management-on-Shift

(MOS) program

which

is

instrumental

in

identifying

areas

needing

improvement.

4

The

issuance

of

a "Standards

of Professionalism"

document

to

clearly

define

the

responsibilities

of

licensed

personnel.

The

management

involvement

in the

reduction

of the

PWO

backlog.

Management's

initiative in reducing control

room

PWOs,

to

facilitate efficient operations.

Management's

policy

on

verbatim

compliance

with plant

procedures

to reduce

personnel

errors.

Event

Response

Teams

identification of root

causes

of

significant plant problems

and determination of appropriate

corrective actions.

The

expansion

of

the

Analytical

Based

Preventive

Maintenance

Program

to

include

new

testing

methods,

resulting

in

the

identification

of

numerous

equipment

problems prior to failure.

Design

Bases

Reconstitution

which identified several

plant

design deficiencies.

The

licensee

exhibited

an

inability to either

identify or

correct

(once

identified)

problems

relating to safety

in the

following areas:

Management's

failure

to

develop

effective

corrective

actions

to

resolve

numerous

AFW backup

nitrogen

system

misalignments.

Failure to adequately

control activities in the operations

area

which

resulted

in

nine

examples

of

procedural

noncompliances.

'I

35

Numerous repetitia'e violations in the security area.

Repeti tive maintenance

pr obl ems,

such as:

def ici ency tags

not entered into the tracking system; priorities not worked

on time or are

changed

during

PWO process;

high preventive

maintenance

backlog;

high amount of rework items

on various

safety-related

systems.

Management's

fai'ture to

assure

adequate

staffing

in the

Operation's

Department: to prevent excessive

overtime.

One violation was identified:

Severity

Level

IV '. violation for failure to take

prompt

corrective

action

l to i have

operators

and

non-licensed

operators

review iand acknowledge training reports.

(87-32)

2.

Conclusion

Category:

2

3.

Board Recommendations

The

Board acknowledges:. signtifiicant action taken

by the licensee

to identify and correct. problems.

Specifically, efforts in the

areas

of design

basis;~reconstitution,

independent

management

appraisal,

and management

changes

have

been effective.

However,

the Board noted that 'these efForts were, in part, in response

to

concerns

expressed

by

~ the.

NRC.

The

Board

encourages

the

licensee

to be more proactive in the future.

J.

Licensing Activities

1.

Analysi s

The

licensee

managements's

role

in attempting

to

assure

quality in

licensing-,related

activities

showed

certain

weaknesses

during. the

SALP period, with signs of possible-

improvement

near..the

nend

of the

period.

An

apparent

weakness

in

the<i licensing

organization

has

been

the

interface

and

coordinathon

between

corporate

licensing,

'ite

licensing,;and

operations/modifications

planning

and

scheduling.

Thei lack

of

unification

under

strong

leadership

in thel licending area

was also noted

by Enercon

in their Independent

Management Appraisal.

There

needs

to

be sufficient communiaption

between

these

groups to permit

advance

planning

of liaensing

proposals

such

as relief

requests

and Technical. Specifications

changes

so that they

can

be processed

i.n

an: orderly

manner.

One

example

where

sufficient

communciation

did

not

exist

concerned

containment

tendon

surveillance'lthough

there

are

several

years

between

tendon

surveillances,

a last-minute

proposal

surfaced

hnd both licensee

and

NRC resources

were

36

spent

discussing

a change

in tendon surveillance

Technical

Specifications.

This effort

was

ultimately

abandoned

because

there

was

not

enough

time to

process

a

change

before

the

next

surveillance..

Another

example

was

relaxation

of

Technical

Specifications-

for

CCW

heat

exchangers.

In order

to install

the

Amertap

system

on

Unit 4,

a proposal

was

made to relax the permissible

outage

time for one heat

exchanger

to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The proposal

was

made

for

an

emergency

amendment.

However, this could not

be supported

on the basis af

10 CFR 50.91

and

instead

the

proposal

was

processed

by

the

staff

as

an

exigent

amendment.

Better

coordination

and

planning

would .have

foreseen

the

need for the'S

relaxation

and

avoided

the

need for an exigent

amendment.

Throughout

most of the

SALP period there

was

no apparent

mechanism

by which the licensee

identified; prioritized,

scheduled

and

tracked

ongoing

and future

open

licensing

actions.

Instead it

was

the

practice

to

use

the

NRC-generated list of open

licensing actions

as

a vehicle

to monitor status of licensing actions.

This approach

was

not effective

because

the licensee's

priorities

were

not

apparent,

and future licensing actions

were not identified.

Near

the

end of the

SALP period,: at

the

NRC

Project

Nanager's

recommendation,

the

licensee

created

a

new

licensing

action

status

report.

This

report

lists

priorities

and

attempts

to identify future

actions

far

enough

in

advance

to permit planning for resources

and

orderly processing

of proposals.

The

new status

report

has

the potential

to improve the licensing

interface

between

the licensee

and

NRC.

Significant

improvements

can still

be

made in formatting and layout of the report,

which will

give

a better visual perspective

of issues,

focus

on future

actions

and

schedules,

and

document

the history of key

communications

on open actions.

The

commitment

to

an

Integrated

Schedule

(I/S)

process

indicates

a desire to control licensing activities

as well

as

prioritize

plant

modifications

and

allocation

of

resources.

The

licensee

made

a significant effort to

develop

a

computer-assisted

program

for

integrated

scheduling of planned plant modifications.

The licensee's

particular

I/S proposal

'was

considered

to

be especially

comprehensive

and well thought-out;

A license

amendment

was

issued

incorporating

the

I/S during this

evaluation

period,

and it is

clear

the

process

is

being

used

extensively

to control

schedules

.and priorities.

The

Integrated

Schedule

represents

a

clear

improvement

to

management's

control of plant- modifications.

The licensee's

approach

to resolution of technical

issues

has

been

adequate.

A special

inspection

was

held during

the

week of December

7, 1987'o

examine activities in the

37

areas

of safety

review pursuant

to

10 CFR 50.59,

and the

on-site

and off-site review committees.

Steady

improvement

in the quality

and

completeness

of

10 CFR 50.59

safety

evaluation

documentation

was

observed'.

Recent

safety

evaluations

audited during the inspection

were sufficiently

detailed

to

demonstrate

the

logic

and

bases

for

determinations

regarding

potential

unreviewed

safety

questions.

A weakness

was identified in that the large

volume of material

requiring

PNSC review resulted

in long

,and

frequent

meetings,

diverting

management

from other

duties.

Some

method of screening

the material'or

PNSC

review seemed

to be needed.

A broad technical

issue that has existed for some time has

been the early vintage Technical Specifications

which were

part of the initial operating

license of the plant.

Many

technical

improvements

in

Technical

Specifications

have

been

developed

in the industry

and at

NRC over the years,

and the'icensee

volunteered

several

years

ago to upgrade

their

TS to modified Standard

TS.

During this

SALP period

a significant effort was

made

by the licensee

to resolv'e

technical

issues

related

to the

upgrade

and to

make

many

refinements

in their original proposal.

The vast majority

of the

TS

changes

are

in

a

more

conservative

safety

direction

than

the

original

TS,

and

the

licensee

is

commended for this effort.

Another

broad

issue that

has

existed for some time is the

reliability of A. C. electrical

power (station blackout).

The licensee's

a'pproach

to this issue

has

been

to

make

a

very significant

commitment

in financial

and

personnel

resources

to enhance

emergency

power supplies

by committing

to

add

two

new

safety-grade

diesel

generators

with

associated

equipment.

The licensee

has

increased

planning

and design

work during this

SALP period

as this effort

begins to grow in magnitude.

In

a meeting held on March 29,

1988,

the licensee

proposed

relaxing the allowable outage

time for CCW heat

exchangers

and

ICW

pumps.

The

technical

basis

for the

CCW heat

exchangers

was

thoroughly

evaluated

and well

presented.

This permitted

rapid technical

review and

issuance

of a

license

amendment

at

a later date.

Such

was

not the

case

for the

ICW pumps.

Even

though the

ICW is

an important

heat

removal

system

and Turkey Point operating

experience

with the

ICW system

has

shown

a

number of failures,

the

licensee

proposed

removal of the

TS on the third ICW pump.

Operating experience

in the industry and, in particular, at

Turkey Point could not support

such

a relaxation

and the

request

was

denied.

At the

end of the

SALP period the

licensee still

has

not proposed

an alternate

TS for the

third ICW pump.

38

In another

matter regarding

the allowable

outage

time for

diesel

generators,

the

licensee

made it clear

that

the

issue

was

important

to

plant

operation.

However,

conference calls to resolve

the issue

were twice postponed

by

the

licensee

and,

when

finally

held,

evidenced

inadequate

technical

preparation

to fully address

the

issue.

The'issue

remains to be resolved.

The licensee's

responsiveness

to

NRC licensing initiatives

has

been

very good.

An example

was the cooperation

with

the

NRC

effort

to

document

historically

the

completion/implementation

status of requirements

in the

NRC

Safety

Issue

Management

System.

Other

examples

were the

provision of information related

to

surveys

of

reactor

vessel

support

structures,

and

the

use

of Bunker

Ramo

containment

penetration

assemblies.

The

response

to

requirements

of bulletins

and

generic

letters

has

been

timely.

The licensee

has volunteered to be the

lead plant

in the

NRC staff's effort to modify generic

requirements

related

to the

need for

an

Operations

Superintendent-

to

hold an

SRO license.

The

spent

fuel

pool rerack

hearings

were completed during

this

SALP period.

The licensee

was especially

responsive

and

expended

significant

resources

to

reassure

the

licensing

boards

and

intervenors

that

they

had taken

appropriate

design

and monitoring measures

to provide for

safe

storage of spent fuel.

The licensee

has generally provided appropriate

members of

their

organization

at

meetings

with

the

staff.

The

corporate

licensing supervisor

has

shown

good judgement

in

controlling meeting

attendance

and

has

been very responsive

to

NRC inqui ries.

The corporate

licensing staff includes

a

former

Turkey Point reactor operator,

providing

a valuable

perspective

for

the

group.

The staffing

level

of the

corporate

(4 positions)

group

appears

to

be the

minimum

able

to

keep

up 'with the

extra

improvement

programs

underway

during

the

past year

in addition to the

normal

workload.

The site licensing group

has

been heavily burdened with its

role

i'n interpreting Technical

Specifications,

evaluating

root

causes,

preparing

reports

to

NRC,

and

translating

operational

needs

into licensing actions.

The Independent

Management

Appraisal

by Enercon

recommended

increasing

the

size

of that

group.

In

response,

the

licensee

has

increased

the

number of authorized positions

from 5 to 9.

As part of the effort to improve performance

in the area of

10 CFR 50.59

reviews,

the

licensee

issued

equality

Instruction 3.9

on April 20,

1988, entitled

"Evaluations

Performed

by Power Plant Engineering."

This gI is intended

39

to provide guidance to the licensee's

staff for conducting

50.59

reviews

and

preparing

reports.

Training

on

the

procedure

was provided at the corporate offices and at the

Turkey Point site.

Conclusion

Category:

2

Board Recommendations

None

K.

Training and (qualification Effectiveness

Analysi s

Early in the

SALP period, close out inspections

conducted

in the

area

of training indicated that the licensee

has

continued

to

make

improvements.

The licensee

has addressed

inadequacies

and concerns identified

during

the

previous

SALP

period

in

the

Licensed

Operator

Requalification

Program

by providing more qualified instructors,

hiring qualified contractor

instructors,

enhancing

instructor

classroom training,

and implementing

an effective tickler system

to ensure

the incorporation of emergent

training

and briefing

m'aterial

into

permanent

lesson

plans.

The licensee

has

also

prohibited Senior

Reactor

Operator

(SRO)

licensed

instructors

who

have failed

NRC requalification

examinations

from 'teaching

licensed operators,

eliminated contract instructors

who were not

commercially

SRO

licensed

from the license training programs,

contracted

15 formerly licensed

SRO instructors,

and

implemented

a five week site specific

systems

training course for contract

instructors.

Another

improvement

was

the

development

of

the

Training

Information

Management

System

(TRIMS) which'ensures

that only

qualified personnel

are

assigned

to perform maintenance

tasks.

The

TRIMS program is also

designed

to provide:

configuration

control

of training materials;

management

of

personnel

and

program training records;

maintenance

of examination

questions

and relative statistical

data;

maintenance

of class

data

and

training

program

schedules;

and

maintenances

of the tracking,

documenting,

and updating of training commitments.

The

licensee

has

made

improvements

in the

required

reading

program,

which

provides

operational

" experience

feedback

.

information

to

Operations

personnel

on

a

regular

basis.

Improvements

include

upgrades

in the procedural

controls

over

documentation

and timeliness of operational

experience

feedback

reviews,

and the screening

of revised procedures

to ensure that

only

relevant

information

is

forwarded

to

the

operators.

40

However,

as noted in the

gA section,

a violation was issued

due

to management'

failure to take

prompt corrective

action for

identified deficiencies

pertaining to licensed

and non-licensed

operators

who

h'ad

- assumed

unit

responsibilities

without

completing

the required

reading.

This violation indicates that

improved management

control over the required reading

program is

needed.

On

January

26-28,

1988,

replacement

examinations

were

administered

to

seven

'SRO

candidates

and

one

individual

was

administered

an

SRO retake written examination.

All candidates

passed.

Two.areas of below normal

performance

were noted in the

written examination.

These

areas

were

knowledge

of bypasses

associated

with the manipulator crane interlocks,

and

knowledge

of whole body dose

emergency

exposure limits for various reentry

situations.

No areas

of generic

weakness

were noted during the

oral examinations.

With respect

to the licensed

operator requalification

program,

the

last

requalification

exams

were

administered

in

February

1986.

The results

of these

exams

wer e considered

in

the

previous

SALP report,

which stated

that

the

licensee's

performance

on

the

exams

was

poor

and

the requalification

program

was

unsatisfactory.

In this

current

SALP

period,

requalification

examinations

were

not administered at, Turkey

Point

because

the

NRC

has

suspended

its

requalification

activities in the industry.

The licensee's

program will receive

reevaluation

at

a future date,

pending

resumption

of the

NRC

administered requalification examinations.

Other

non-licensed

employee training

was

assessed

during this

SALP

period.

As

noted

in

the

Radiological

Controls,

Fire

Protection,

Emergency

Preparedness

and

Engineering

Support

sections of this report, training in these

areas

was

determined

to

be

adequate,

with improvement

noted

in the health

physics

area of the general

employee training program.

In

the

area

of

Survei llances;

the

training

of technica'l

personnel

was satisfactory,

yet the training of personnel

who

specify

and write repair

and retest

procedures

needs attention.

In the Security. and Safeguards

area, it was noted that training

measures

were either

not

implemented,

or

have failed to

be

effective in ensuring

compliance with regulatory

requirements.

It was

noted that

in the

Operations

'area,

some

performance

issues

stemmed

from root causes

related to training.

Six

training

programs

received

accreditation

by

INPO

in

December

1987,

resulting

in all ten original training programs

being accredited.

Conclusion

41

Category:

2

Board Recommendations

None

L.

Engineering

Support

Analysi's

The licensee

has successfully

implemented

a number of corrective

actions

to

improve

technical

support.

These

have

included

detailed

reviews of selected

safety

systems,

reconstitution of

system

design

bases,

standardization

of design

packages

for

controlling

changes,

increased

staffing

and training

on

the

plant change

process.

The

design

.basis

reconstitution

effort,

in conjunction with

system

reviews

and walkdowns,

has

been particularly beneficial

in

that

numerous

design

related

deficiencies

have

been

identified and corrected.

The Engineering

Departments

have,

in

all instances,

responded

promptly and adequately

to, identified

problems.

Several

of the problems

were corrected

on

a real time

basis,

although

administrative

justification

for

continued

operation until scheduled

outages

could have

been

pursued.

The

efforts to minimize operating

the

plant

around

problems

has

shown

improvement.

The

licensee

has

been

conducting

repairs

when

required.

Examples

of safety-related

deficiencies

which

were identified

and

addressed

on

a

real

time basis

include;

waste

gas

system

operation

in

an

unevaluated

configuration

(October

1987),,

inappropriate

design

of

the

residual

heat

removal, 'ecirculation

flow

path

(October 1987),

and

post-injection

recirculation

valve

alignment

resulting

in

insufficient net positive

suction

pressure

to safety-related

pumps

(Nay 1988).

Corrective actions

to preclude

recurrence

of boric acid leaks

similar to the

conoseal

leak during the last

SALP period

have

been

implemented,

resulting

in

a vigorous

program to identify

and correct

even minor primary leakage.

This effort resulted in

the identification and correction of small conoseal

leaks

on the

Unit 3 reactor

in July 1987.

Additional sensitivity to primary

leakage

was demonstrated

in August 1987,

when

a decision

was

made

to

remove

the Unit 3 reactor

head to correct

a leaking

inner 0-ring.

Continued plant operations

with this deficiency

could

have

been

justified

had it occurred

during

power

operation.

However,

the licensee's

position

was that quality

precepts

dictated that

a post-refueling

power cycle not begin

with an avoidable deficiency.

During this assessment

period,

reviews were performed to assess

th'e adequacy

of engineering

evaluations.

The

NRC found evidence

of significant improvement in the quality of safety evaluations

42

over

those

performed

during

the

previous

SALP

period.'dditionally,

trends

were

identified

which

indicated

that

continued

improvement

would result

as

procedures

and training

continued to be implemented.

In

general,

safety

evaluations

reviewed

were

sufficiently

detailed to demonstrate,

as stand-alone

documents,

the logic and

basis for determinations

regarding

potential

unreviewed

safety

questions.

Safety

evaluations

were

performed

for all plant

modifications,

even

those classified

as non-safety

related,

to

preclude

the possibility of unexpected

adverse

impact

on the

plant.

Detailed

equality Instructions

have

been

developed

and

implemented after completing training to control the methodology

'used

in completing

10 CFR 50.59

reviews

and design

equivalent

engineering

packages.

The design

equivalence

program

has

been

particularly effective in verifying that appropriate

component

substitutions

are

selected

when current

equipment is no longer

available.

The procedures

for controlling Temporary

System Alterations are

detailed

and effective.

Evaluations to support the alterations

meet

the

requi rements

of

10 CFR 50.59

and

receive

numerous

reviews

including

the

Shift

Technical

Advisor,

Technical

Department

Supervisor,

Plant

Supervisor-Nuclear

and

Plant

Nuclear Safety

Commi.ttee.

The temporary alterations

are audited

quarterly to ensure

.continued validity.

The

level

of detail

included

in

the

safety

evaluations

has

increased

over that

.

existing during the previous

assessment.

Violation i,

in

the

Operations

functional

area,

documents

a

single

isolated

example

of the failure to perform

a required

Temporary

System Alteration evaluation.

Violation a,

in the

Operations

functional

area,

occurred,

in

part,

due to an unacceptable

safety evaluation, performed

on the

intake cooling water.

Although the

problem

was identified in

June

1987, it should

be noted that the deficient evaluation

was

issued

in August 1986.

The

safety

evaluation

allowed brief

system

operation

in

a

mode

which

was

susceptible

to single

failure.

Consequently, it constituted

an

unreviewed

safety

question

which was not recognized

by the Engineering

Department.

Additional

reviews

of safety

evaluations

indicate

that this

problem is not programmatic.

Some

engineering

resolutions

to identified deficiencies

have

been resolved

by administratively controlled compensatory

action

in the short term.

Some significant plant modifications must be

implemented to allow completion of long term fixes.

Plans exist

to install two additional

emergency

diesel 'generators

on site by

late

1991.

This is necessary

to provide a'dditional

margin for

emergency

loads

assuming

the loss of offsite power, failure of a

single diesel

and the initiation of a loss of coolant accident;

Until this upgrade is completed,

the plant must rely on portable

43

instrument air compressors

'to operate

the instrument air system.

The temporary

compressors

have

been in use since

1986

'ong

term compensatory

action

has

been required to ensure that

a

valve with single failure deficiencies

in the

Intake

Cooling

Water

system will shut

under

certain

accident

conditions.

Periodic

valve watches

have

been

required

since

1985.

Unit 3

corrective

action in mid 1987,

included the installation of an

automatic

cleaning

system for the

system

heat

exchangers.

A

similar

system will be

functional

on Unit 4 by October

1988.

However,

the corrective action

has

reduced,

but not alleviated

the

need for the Unit 3 valve watch.

On

one

occasion

in the

spring of 1988, the compensatory

valve watch was found asleep

at

his post.

The

use of non-seismic

pressure

gauges

in engineering

designs

has

contributed

to

problems

described

in

the

Operations

functional

area.

For example,

several

non-seismic

gauges

were

installed

in

the

auxiliary

feedwater

(AFW)

backup

nitrogen

system.

Since

the

AFW nitrogen

system

must

meet

seismic

requirements,

the

gauges

were

normally

isolated.

Several

nitrogen

system violations occurred

when the gauges

were valved

in contrary

to

procedure.

Violation m,

in

the

Operations

functional area,

documents

three

examples of the plant personnel

opening

a

non-seismic

boric

acid

transfer

pump

discharge

pressure

gauge required to be shut.

Non-seismic

pressure

gauges

also exist in other safety related

systems,

which have

had minor

valve misalignments.

Violation g,

listed

in

the

Operations

functional

area,

represents

an

isolated

example

of the failure

to translate

design

input into

operating

procedures

for the

AFW backup

nitrogen

system.

Modifications to the

nitrogen

system

were

performed for Unit 4 in mid 1986,

and Unit 3 in the spring of

1987.

The

engineering

packages

were

essentially

identical.

Calculations

were performed to assure

that the expanded

nitrogen

capacity

allowed

the requisite

duration of

system

operation.

The

bases

for the calculations

were not fully explained in the

engineering

package.

Consequently,

design

basis

nitrogen

usage

rates

were

taken

out of context

and incorporated

in AFW system

surveillance

procedures.

This

resulted

in

surveillance

procedures

with

non-conservative

acceptance

criteria,

which

failed to verify full system operational capabilities.

This

problem

occurred

because

site engineering

personnel

were

not supplied with the original calc'ulations

used

by a contract

organization

in

developing

design

consumption

rates.

A

description

of

the

consumption

rates

contained

in

the

engineering

package

summary

was too vague to supply the proper

context

for their

inclusion

in

surveillance

procedures

as

acceptance

criteria.

The

existence

of this

type of deficiency

was

the result

of

ineffective

use

of

the

licensee's

system

engineers.

The

program,

which is designed

to centralize

knowledge

of system

characteristics

and requirements

in

a single engineer,

has not

resulted

in

the

identification

of

the

kinds

of

concerns

discussed

above.

An additional

example

includes

violation a

listed in the Operations

functional

area.

The system'ngineer

for the intake cooling water

system failed to ensure

that the

heat

exchangers

were cleaned

on

an appropriate

schedule

and in

the correct

sequence.

Additionally, although

a

system existed

requiring detailed analysis of heat

exchanger

efficiencies,

the

engineer failed to realize that design

basis

assumptions

were

'not met.

In part, this problem area existed

because

the

system engineers

did not monitor closely

enough

the

status

of their assigned

systems

through

work order

reviews,

design

change

analyses,

frequent

system walkdowns

and status

evaluations.

,Consequently,

identifiable problems

may not be identified in a timely manner.

For

example,

violation 1,

in the

Operations

functional

area,

documents

that certain

intake cooling water

flow meters

were

removed

from the

system without administrative justification.

Although the

meters

were

absent

for

many

months,

the

system

engineer

did

not

independently

pursue

the

discrepancy

and

therefore

remained

unaware

of the

problem.

Also, the engineer

was

not aware that plant log sheets

allowed

an intake cooling

water

pump

dis'charge

pressure

band

which

was

so

large that

conformance

with design

flow rate

requirements

might not

be

possible.

A new administrative

procedure

was implemented during

this

assessment

period which

requires

the

system

engineer

to

perform regular reviews of system logs and instrumentation,

and

to perform periodic system walkdowns.

These

requirements

should

prevent

some of the problems discussed

above

from occurring.

The

recently

completed

Independent

Management

Appraisal

concluded

that

problems

associated

with the

system

engineering

~

program

included;

lack of

management

follow-up to

assure

effective

system

engineer utilization, lack of clear definition

of system

engineer

responsibilities,

lack of authority to obtain

the

support

needed

to

resolve

problems,

and

inadequate

fulfillment of assigned

responsibilities.

The

system

engineers

spend

a large percentage

of time processing

paperwork instead of

solving system problems.

These

deficiencies

have

resulted

in

an

environment

in which

system

engineers

primarily react to problems.

They do not have

sufficient

time,

nor

are

they

directed

to

prevent

future

problems.

There

is little trending

of

performance

data.

Reliability engineering

has not been achieved

because

potential

system

problems

are not resolved before they occur.

In the spring of 1988,

a

new Technical

Department Supervisor

was

appointed.

A number

of initiatives

are

being

developed

to

45

address

the

above

concerns.

These

include

less

reliance

on

contractor

personnel

to perform

system

engineering

functions,

increased

staffing to reduce

the

number of systems

assigned

to

each

engineer,

increased

training 'nd

increased

supervisory

involvement.

While it is expected

that these

initiatives will

have

a favorable

impact, it is too

soon to determine

whether

they will ultimately be successful.

Two violations were identified:

a.

Severity

Level

IV violation

for failure

to

conduct

modification

testing

as

a

result

of

an

inadequate

procedure.

(87-41)

b.

Severity

Level

IV violation for fai lure to use the proper

material

in intake cooling water system.

(88-14)

2.

Conclusion

Category:

2

3.

Board Recommendations

Although improvement

has

been

noted

in the Engineering

Support

area,

continued

management

attention is warranted.

V.

SUPPORTING

DATA AND SUMMARIES

A.

Licensee Activities

At the start of the assessment

period, Unit 3 was in a refueling and

maintenance

outage

that

started

March 11,

1987.

On

September

12,

1987, the unit returned to power operations;

the extended

outage

was

caused

by repair work on Raychem splices,

diesel

generator

sequencer

wiring checks

and testing,

and

a reactor vessel

0-Ring leak.

Other

outages

included those discussed

under Item J

Reactor Trips,

and the

following non-scheduled

maintenance

outages:

On September

25,

1988,

a

maintenance

outage

occurred

to

investigate

and

repair

high

vibrations

on

a reactor

coolant

pump

and to repair

a pressurizer

spray

valve.

The unit remained

down to repair additional

items

including

a

design

deficiency

with

the

residual

heat

removal

recirculating piping.,

The unit returned to service

on

December

22,

1987.

Additional

maintenance

outages

occurred

from

March

16 to

March 23,

1988,

due to weld repairs

to cracked

moisture

separator

reheater

baffle plates

and

on March 24,

1988, to repair

a condenser

tube

leak.

On

March 30,

1988,

the

unit

returned

to

commercial

operations

and

remained

at

power through the remainder

of the

SALP

period.

Unit 4 was in an extended

maintenance

outage at the start of the

SALP

period

and did not return to service unti 1 July 8,

1987.

On July 15,

1987,

the unit was

shut

down to repair

a condenser

tube

leak

and

returned to power operations

on July 21,

1987.

On September

6,

1987,

46

the unit was

shut

down for 576 hours0.00667 days <br />0.16 hours <br />9.523809e-4 weeks <br />2.19168e-4 months <br /> to repair

a damaged

drain line

which was

causing

a

condenser

vacuum

problem.

The unit operated

at

power

until

October

12,

1987,

when it

was

shut

down

as

a

precautionary

measure

for

a hurricane

warning.

The unit remained

down until

December

4,

1987,

to repair

a safety injection

pump,

a

leaking

PORV,

and correct

a, design deficiency with the residual

heat

removal

recirculation piping.

On

February 7,

1988,

the unit shut

down

on declaring

two battery charges

out-of-service.

While the unit

was

down,

work was

performed

on

a reactor

coolant

pump

motor

and

control

rod drive mechanism

cables.

The unit returned to service

on

February

24,

1988.

On April 6,

1988,

the unit was shut

down for a 33

hour

period

to repair

a

turbine

control oil

system

leak.

On

April 28,

1988,

the

unit

was

shut

down

to

repair

a

leaking

pressurizer

control

spray

valve

and

remained

down

to

repair

a

containment

purge

isolation

valve.

The

unit

returned

to

power'perations

on

May 28,

1988,

and

remained

at

power

through

the

remainder

of the

SALP period.

B.

Inspection Activities

The routine inspection

program

was performed during this period, with

special

inspections

conducted

to augment

the program

as follows:

1.

June

15-19,

1987,

concerning

of

a series of loss of boric acid

flowpath events,

the status

of licensed

operator training,

and

instructor qualifications.

2.

September

22

October 25,

1987,

in the areas

of unauthorized

dilution event

and resolution of issues

raised

by

a

licensee

personnel.

3.

November 4-6,

1987,

in the area of void formations in the Unit 4

reactor

vessel

upper

head

region

during

cold

shutdown

conditions.

December 7-11,

1987,

in the area

of safety

review activities,

including

10 CFR 50.59

determinations

and

safety

review

committee functions.

December

14-16,

1987, in the area of IE Bulletin 83-06.

6.

February 22-25,

1988, in the area of Emergency

Response

Facility

Appraisal.

C.

Licensing Activities

1.

NRR/Licensing Meetings

The

licensee's

presentations

were

generally well'tructured.

The licensee

was generally well prepared

for meetings with the

NRC staff'nd handled

the staff'

questions

adequately.

A list of NRR/Licensee

meetings is

shown below:

Date

Pur ose

June

4,

1987

Discussion of Emergency

A.

C.

Power

Enhancement

June

17-18,

1987

June

23,

1987

Discussion of TS Improvement Project

Discussion of Boraflex in Spent

Fuel

Pool

Racks

June

22-23,

1987

August 26-27,

1987

'September

2,

1987

Discussion of TS Improvement Project

Discussion of TS Improvement Project.

Discussion of FP&L Electrical

Transmission

System

October 20-22,

1987

December

15-17,

1987

January

6,

1988

Discussion of TS Improvement Project

Discussion of TS Improvement Project

Discussion of Schedule for Technical

Specification

Conversion Project

January

28,

1988

Clarification of Use of Technical

Specification in Control

Room

February 23-26,

1988

Discussion of Technical Specification

Improvement Project

March 15,

1988

Discussion of ICW/CCW TS and

Operability of

CCW Heat Exchangers

March 28-31,

1988

Discussion of Technical Specification

Improvement Project (Electrical)

May 18,

1988

Discussion of Improvements to

Integrated

Schedule

June

2,

1988

Discussion of Seismic Adequacy of

Components

(Generic Letter 87-02)

I

2.

Commission Meetings - None

3.

Schedular

Extension

Granted

None

4.

Reliefs Granted

48

June

15,

1987

March 28,

1988

S.

Exemptions

Granted

August 12,

1987

Relief

Request

No.

16

Relief

From Visual

(UT-2) Examination (Unit 3)

Relief

Request

No.

17

Relief

From Visual

(UT-2)'Examination (Unit 3)

Technical

Exemption

from

10 CFR 50,

Appendix

R Requirements

6.

Emergency or Exigent Technical Specifications

Issued

Apri 1 29,

1988

Exigent

Technical

Specification

to

the

Component

Cooling Water System.

7.

Discretionary Enforcement

December

31,. 1987

Discretionary

enforcement

granted for

a

24

hour extension

of TS 3.4.5.a

concerning

ICW

pump operation.

January

15,

1988

Discretionary

enforcement

granted

for

TS

Chapter

6,

figure

6.2-2

concerning

the

requirement for the Operation

Superintendent

to hold an

SRO license.

Febr vary 24,

1988

Di scretionary

enforcement

granted for a

24

hour extension

of

TS 3.0. 1

concerning

the

recalibration

of

the

steam

generator

instrument channels.

8.

License

Amendments

Issued

Amendment

Numbers

Unit 3

Unit 4

Descri tion

Date

124

118

Revise the

TS for the auxiliary

06/08/87

feedwater

system

and the condensate

storage

tanks

125

119

126

120

127

121

128

122

Incorporate

TS for reactor vessel

level monitoring system

Integr ated Scheduling

Revise the

TS for the D.C. power

source

Delete remaining Sections

1.0

and 5.0 of the environmental

TS and replace it with an

Environmental

Protection

Plan

07/28/87

11/23/87

04/18/88

04/25/88

49

129

123

Organization

changes

per Generic

04/28/88

Letter 88-06

130

124

Revise the

TS for the component

cooling water system

04/29/88

D.

Investigation

Review

An investigation

was conducted

on the events

surrounding

the

manipulation of reactor controls

by a non-licensed

person.

E.

Escalated

Enforcement Actions

1.

Civi 1 Penalties

a

~

A Notice of Violation (Severity

Level III, Supplement I),

and

a

Proposed

Imposition of Civil Penalty

(EA 87-97) for

$ 100,000

were

issued

on July 21,

1987,

for failure

to

adequately

evaluate

and correct

a reactor coolant leak and

failure to assure

the required prerequisites

were met prior

to

commencing

core alterations.

This violation, although

issued during the current

SALP period,

was addressed

in the

previous

SALP.

b.

Three Notices of Violation (Severity Level III, Supplement I)

and

a Proposed

Imposition of Civil Penalty

(EA 87-85) for a

total of $225,000 were issued

on October

18,

1987, for the

following:

1) fai lure to adequately

establish

or implement

procedures

to assure

configuration control over the safety-

related

emergency

boration

system; .2) failure to meet the

Technical

Specification

requirement

for

maintaining

auxiliary

feedwater

system

for Unit 4 operable;

and

3)

operation

of the intake cooling water

system

outside

the

plant

design

basis.

These

violations,

although

issued

during

the

current

SALP period,

were

addressed

in

the

previous

SALP.

c.

Two Notices of Violation (Severity Level III, Supplement III)

and

a Proposed

Imposition of Civil Penalty

(EA 87-98) for a

total of $ 100,000 were issued

on July 28,

1987, for failure

to maintain access

cont'rol

and to conduct

adequate

vehicle

'earch.

The

licensee's

request

for mitigation of the

Severity

Level

and Civil Penalty

resulted

in the Civil

Penalty

being mitigated

on

November 5,

1987,

to

$75,000.

These violations,

although

issued

during the current

SALP

period,

were addressed

in the previous

SALP analysis.

d.

Two Notices, of Violation (Severity

Level III, Supplement

III) and

a Proposed

Imposition of Civil Penalty

(EA 87-179)

for $ 150,000 were issued

on February ll, 1988, for failure

to

maintain

positive

access

control (six

examples)

and

fai lure to protect safeguards

information'

4

50

Orders

An

order

imposing

the

licensee's

commitments

to

have

an

independent

review of management

and operational activities,

and

an

assessment

of required

changes

was

issued

on

October

19,

1987.

F.

Licensee

Conferences

Held During Appraisal

Period

June

5,

1987,

Enforcement

Conference

to discuss

the following

issues:

inadequate

protected

and vital

area

access

control;

emergency

diesel

generator

sequencer

wiring errors; failure to

establish

containment

integrity during

core alterations;

and

inadequate

safety evaluation of the conoseal

leakage.

June

24,

1987,

Working

level

discussions

on

Turkey

Point's

Performance

Enhancement

Program

(PEP).

July 29,

1987,

Enforcement

Conference

to di scuss

the loss of

boric acid flowpath and auxiliary feedwater

system inoperability

due to i'solation of the safety-related

nitrogen supply.

July 30,

1987,

quarterly

Performance

Enhancement

Program

management

meeting.

July 30,

1987,

Management

meeting to discuss

SALP assessment.

October 28,

1987,

Enforcement

Conference

to discuss

security

issues.

November

18,

1987,

Management

meeting

to discuss

the initial

independent

audit plan.

November 24,

1987,

Management

meeting to discuss

the Independent

Management

Appraisal

Plan

and

the

Management-on-Shift

Program

(MOS).

10.

December

21,

1987,

Management

meeting to discuss

the Independent

Management

Appraisal,

Management-on-Shift

Program,

SALP

category

3

areas,

and

an

Enforcement

Conference

on security

issues.

January

25,

1988,

Management

meeting to discuss

the Independent

Management

Appraisal

Plan, MOS,'nd the Performance

Enhancement

Program status.

12.

March 2,

1988,

Management

meeting

to discuss

the

Independent

Management Appraisal

Plan

and the

MOS Program.

April 21,'988,.

Enforcement

Conference

to di scuss

emergency

preparedness

issues.

II

~ ~

~

51

G.

13.

April 22,

1988,

Management

meeting

to discuss

the

MOS

Pr ogram

and

SALP category

3 areas.

14.

June

10,

1988,

Management

meeting

to discuss

the

Independent

Management

Appraisal,

MOS Program

and

Performance

Enhancement

Program status.

Confirmation of Action Letters

(CALs)

CAL 50-250,251/87-01

i ssued

on

October 6,

1987,

requiring that

a

specific reactor

operator

not

assume

his

normal duties without

NRC

approval.

H.

Licensee

Event Report Analysis

During the assessment

period,

51

LERs for Units

3 and

by the

NRC staff.

The distribution of these

events

determined

by the

NRC staff,

was

as follows:

Cause

Unit 3

Unit 4

4 were analyzed

by cause,

as

Total

Component Failure

Design

Construction,

Fabrication,

or Installation

Personnel

Operating Activity

Maintenance Activity

- Test/Calibration Activity

Other

10

8

10

2

Out of Calibration

Other

TOTAL

24

27

51

V

~l

I.

Enforcement Activity

52

UNIT SUMMARY

FUNCTIONAL

AREA

NO.

OF DEVIATIONS AND VIOLATIONS

IN EACH SEVERITY LEVEL

D

V

IV

III

II

I

UNIT NO.

-,

3/4

3/4

3/4

3/4

3/4

3/4

Plant Operations

Radiological Controls

Maintenance

Surveillance

Fire Protection

Emergency

Preparedness

Security

and Safegurads

Outages

Quality Programs

and

Administrative Controls

Affecting Quality

Licensing Activities

Training

Engineering

Support

3/3

3/2

5/7

3/2

3/3

2/3

0/1

1/1

2/2

5/5

2/2

2/2

TOTAL

6/5

21/25

5/4

FACILITY SUMMARY

FUNCTIONAL

AREA

No.

OF DEVIATIONS AND VIOLATIONS IN EACH

SEVERITY LEVEL

IV

III

II

I

Plant Operations

Radiological Co~trois

Maintenance

Sur veil lance

Fire Protection

Emergency

Preparedness

Security

and Safeguards

Outages

Quality Programs

and

Administrative Controls

Affecting Quality

Training and Qualifications

Licensing

'Engineering

Support

Total

6

7

3

3

3

1

1

2

5

2

25

5

53

Reactor Trip

Four unplanned

reactor trips and three

manual

shutdowns

occurred

during this evaluation

period for Unit 3.

Unit 4 sustained

six

manual

shutdowns.

The unplanned trips and shutdowns

are listed

below.

1.

Unit

September

13,

1987, Safety injection actuated

and the

reactor tripped from five percent

power

due to failed high

steam flow channels

and personnel

errors while performing

a

turbine generator

cverspeed trip test.

September

25,

1987, the unit was manually shut

down from

power operations

due to high vibration on

a reactor coolant

pump.

C.

Oecember

25,

1987, while attempting

a controlled shutdown,

the reactor tripped from subcritical conditions

when

a

source

range detector,

which had

been

taken out of service

without bypassing its trip signal,

spuriously energized

above its setpoint.

Insufficient procedural

guidance

was

cited as

a primary cause,

with circuitry problems

as

a

contributing cause.

d.

Oecember

29,

1987, the reactor

was manually tripped from

approximately

70:o power due to contact failures in the

turbine overspeed

protection relay and the resultant

loss

of turbine load.

f.

g.

January

13,

1988, the unit experienced

a turbine runback

from 1005 power and

a subsequent

manual reactor 'trip due to

dropped control rod assemblies.

Narch 16,

1988, the unit was shut

down to repair

a weld

crack on moi sture separator

reheator baffle plates.

Harch 24,

1988,

the unit was shut

down from approximately

30% power due to

a condenser

tube leak.

2.

Unit

b.

July 17,

1987,

the unit was shut

down to hot standby to comply

with Technical Specification

requirements

due to a steam

supply

leak in the auxiliary feedwater

system.

September

6,

1987, the unit= was shut down due to losing

vacuum

as

a result of a bearing drain failures

on the main

feedwater

pump.

~ C

'tl

54

c.

October

12,

1987,

the unit was shut

down as

a precautionary

measure for a hurricane warning.

d.

February 7,

1988, the unit was shut

down from 100K power

due to exceeding

the Technical Specification action state-

ment for inoperable battery chargers.

e.

April 6,

1988,

the unit was shut

down to investigate

and

repair

a leak in the turbine control oil system.

f.

April 28,

1988 the unit was shut

down due to increased

RCS

leakage

(3.2

gpm) caused

by a pressurizer

spray valve

bellows rupture.

K.

Radioactive Effluent Releases

(Ci/YR)

Activity Released

(Curies)

1.

Gaseous

Effluents

Fission

and Activation

Gases

Sodiums

and Particulates

Tritium

1985

3.12

0.015

310

1986

4.65

0.023

593

1987

1.70

0.025

820

2.

Liquid Eff1 vents

Fission

and Activation

Products

Tritium

0.9

869

0.506

727

0.75

540

3.

Personnel

Contaminations

a.

Turkey Point

b.

Region II PWR Average

4.

Contaminated

Area (ft~)

a.

Turkey Point

b.

Region II

5.

Collective

Dose

(Man-rem)

a.

Turkey Point

b.

Region II PWR Average,

6.

Solid Rad Waste

(fthm)

a.

Turkey Point

b.

Region II PWR Average

437

306

23,821

16,023

645

390

4,300

14,497