ML17342A831

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Insp Repts 50-250/87-32 & 50-251/87-32 on 870706-10. Violations Noted.Major Areas Inspected:Closeout of Open Insp Items
ML17342A831
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 07/27/1987
From: Shymlock M, Stadler S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17342A829 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-1.A.1.2, TASK-1.A.2.3, TASK-1.C.5, TASK-TM 50-250-87-32, 50-251-87-32, NUDOCS 8708060061
Download: ML17342A831 (38)


See also: IR 05000250/1987032

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 30323

Report Nos.:

50-250/87-32

and 50-251/87-32

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami, FL 33102

Docket Nos.:

50-250

and 50-251

License Nos.:

DPR-31

and

DPR-41

Facility Name:

Turkey Point

3 and

4

'I

Inspection

Conducted:

July 6-10,

1987

Inspector:

S.

. Stadler,

Team Leader

Team Members:

T. J. O'onnor

M. J. DeGraff

R.

D. Starkey

Approved by:

M. B.

Iy

oc

,

hief

Operational

Programs

Section

Division of Reactor Safety

SUMMARY

V/X7r'gP

Date Signed

o87 rtg7

Da

Signed

Scope:

This routine,

announced

inspection

was. in the area of closeout of open

inspection

items.

Results:

One violation

was identified concerning

the failure to implement

approved

procedures

governing operational

experience

feedback,

paragraph 5.t.

87080600hf

870728

PDR

ADQCK 05000250

PDR

REPORT

DETAILS

Persons

Contacted

Licensee

Employees

  • C. M. Wethy, Vice President
  • C. J. Baker, Plant Manager - Nuclear
  • E. F. Hayes, guality Control

(OC) Supervisor

  • J. A. Labarraque,

Technical

Support Supervisor

  • W. Bladow, guality Assurance

(gA) Superintendent

  • D. D. Grandage,

Operations

Superintendent

  • J. Arias, Jr., Regulatory

and Compliance Supervisor

  • D.

W. Haase,

Chairman,

Safety Engineering

Group (SEG)-

  • G. Salamon,

Compliance

Engineer

  • D. R. Whitney, Compliance

Engineer

  • M. 0. Kulp, Project Engineer
  • J. C. Strong, Electrical

Department

Supervisor

  • R. Broadnax,

Support Supervisor - Training

Other

licensee

employees

contacted

included

engineers,

technicians,

operators,

and office personnel.

NRC Resident

Inspectors

D.

R. Brewer, Senior Resident

Inspector

K.

W. VanDyne, Resident

Inspector

  • J. B. MacDonald, Resident

Inspector

  • Attended Exit Interview

Exit Interview

The inspection

scope

and findings were summarized

on July 10,

1987, with

those

persons

indicated in paragraph I above.

The inspection

described

the

areas

inspected

and

discussed

in detail

the following inspection

findings.

No dissenting

comments

were received

from the licensee.

The

following items from previous inspection reports

were closed:

(Closed)

Escalated

Enforcement

Action (EA) 86-20

VI Failure to Promptly

Identify Conditions Adverse to guality With Respect

to Component

Cooling

Water

Flow Through Residual

Heat

Removal

Heat Exchangers,

Single Failure

Concerns

of

an

Intake

Cooling Water -Control

Valve,

and

Resolution

of

Component

Cooling

Water

Problems

for

Safety

Injection

Pumps.

(Paragraph

3.c)

(Closed)

EA 86-20-V:

Failure

to

Perform

Technical

Specification

'Surveillance

Testing

for Station

Batteries,

Failure

to

Adequately

Establish

and

Implement Procedures

With Respect

to Documentation

of Post

Maintenance

Testing

and

Root Cause of Problems

on Plant

Work Orders,

and

Failure to Take Adequate

Corrective Action With Respect

to Missing Valve

Parts

and

Safety

Related

Condensate

Storage

Tank

Level

Indication

Concerns.

(Paragraph

3.a)

(Closed)

EA 86-20-III:

Failure to Comply With Technical Specification 3.8

and 3.4 Concerning,

Respectively,

Auxiliary Feedwater

System

and Safety

Injection System Operability.

(Paragraph

3.b)

(Closed)

Unresolved

Item

(UNR)

250,251/85-40-13:

Failure

to

Meet

Coranitment to Install Adequate

DC Lighting to Support Local

AFW Operations

During Shutdown

From Outside the Control

Room.

(Paragraph

5.c)

(Closed)

UNR 250,251/85-40-25:

Inspector

Concerns

Pertaining

to Tubing

Sections

of the Nitrogen

Backup to the Auxiliary Feedwater

System

Being

Adequately Supported.

(Paragraph

5.e)

(Open)

UNR 250,251/85-40-29:

Review of Licensee's

Thermal

Overload Size

for Valve Operators

(Paragraph

5.g)

(Closed)

UNR 250,251/85-40-30:

Insufficient Test

Data

and

Review of

Manufacturer's

Calculations

to Insure the Operability of MOVs 3-1403

and

4-1403

Steam Supply to the Auxiliary Feedwater

Pump.

(Paragraph

5.h)

(Closed)

UNR 250,251/85-40-33:

Review Apparent Conflict Between Technical Specification 4.8.2.b

and Vendor Recommendations.

(Paragraph 5.i)

(Closed)

UNR 250,251/86-18-01:

Lack of Documentation to Indicate

Formal

Operability Evaluation.

(Paragraph

5.k)

(Open)

UNR 250,251/86-18-13:

Lack of Procedures

for Loss of

DC Power.

(Paragraph

S.o)

(Closed)

UNR 250,251/86-19-03:

Failure to Provide Requalification

Exams

Within Required

Time Period.

(Paragraph

5.p)

(Closed)

UNR 250,251/86-46-02:

Tracking of Corrective Actions to Findings

of Licensee

Internal Training Assessment.

(Paragraph

S.r)

(Closed)

UNR 250,251/87-07-02:

Implementation of Revised

Required

Reading

Program

and

Resolution

of

Outstanding

Required

Reading

Items.

(Paragraph 5.t)

(Closed)

UNR

250,251/87-09-01:

Excessive

Overtime

By

Operations

Personnel.

(Paragraph

5.v)

(Closed)

UNR 250,251/87-09-02:

Utilization of Non-qualified Instructors

to Teach

Systems

and Integrated

Plant Response.

(Paragraph

5.w)

.

(Cl osed)

Inspector

Fol 1 ow-up

Item (IFI)

250/84-25-01/

251/84-26-01:

Inspector

Concerns

Pertaining

to Non-shift Licensed Operators

Performing

the Functions of Licensed Operator

on

a quarterly Basis.

(Paragraph

5.a)

i

e

3.

(Closed)

IFI 250,251/85-22-10:

Completion of

Commitments

to Train

Licensed

Operators

on the

Loss of Inverters

and Associated Vital Buses.

(Paragraph

S.b)

(Closed)

IFI 250,251/85-40-16:

High Radiation

Levels in the Auxiliary

Feedwater

Pump

(AFW) Area Following a

LOCA on Unit 3.

(Paragraph

5.d)

(Closed)

IFI 250,251/85-40-28:

Review the

New Maintenance

Training and

the Qualification Tracking System.

(Paragraph 5.f)

(Open) IFI 250,251/85-40-38:

Determine

Adequacy of Fail Safe Testing for

Auxiliary Feedwater

Flow Control Valve.

(Paragraph 5.j)

(Closed)

IFI 250,251/86-18-02:

Lack of Adequate Criteria for a Safety

Evaluation Determination.

(Paragraph

5.k)

(Closed)

IFI 250,251/86-18-05:

Need to Develop

and

Implement Corrective

Action Program for Motor Operated

Valves (Paragraph 5.l)

(Cl osed)

IFI

250,251/86-18-09:

Control

Over

Plant

Scaf folding.

(Paragraph

5.m)

(Closed)

IFI 250,251/86-18-10:

Configuration Control

Concerns

Over the

Procedural

Requirement

of Valve Lineup Versus'he

Actual Field Position.

(Paragraph

5.n)

(Closed)

IFI 250,251/86-24-01:

Inspector

Concerns

Pertaining

to Post

Accident Sampling

System

(PASS) Calibrations.

(Paragraph

5.q)

(Closed)

IFI 250,251/87-07-01:

Resolution of Training Records

and Files

Involving the

Recertification

of Quality Control

(QC)

Inspectors,

(Paragraph

5.s)

(Open)

IFI 250,251/87-07-03:

Generation

of Electrical

Breaker Setpoint

Document.

(Paragraph

5.u)

The licensee

did not identify as proprietary any of the materials

provided

to or reviewed

by the inspectors

during this inspection.

Licensee Action on Previous

Enforcement Matters

(92702)

On August 18,

1986,

the

NRC issued

a Confirmatory Order

and Notice of

Violation and Proposed

Imposition of Civil Penalties

related to Inspection

Reports

250,251/85-32,

250,251/85-40,

250,251/86-02,

250,251/86-11,

and

250,251/86-26.

This enforcement

action combined violations and unresolved

items

discussed

in these

inspections.

To ensure

that all of the

inspection findings presented

in these

reports

have

been

addressed,

this

section

of the

report

presents

closeout

of the violations

as

they

originally appeared

in the inspection reports.

a.

Escalated

Enforcement

Action

(EA) 86-20-V:

Failure

to

Perform

Technical

Specification Surveillance

Testing for Station Batteries,

Failure to Adequately Establish

and

Implement Procedures

With Respect

to Documentation

of Post

Maintenance

Testing

and

Root

Cause

of

Problems

on

Plant

Work Orders,

and

Failure

to

Take

Adequate

Corrective Action With Respect

to Missing Valve Parts

and Safety

Related

Condensate

Storage

Tank Level Indication

Concerns.

This

EA originated

from violation 250,251/86-26-10,

which

encompassed

previously

identified violation

250,251/86-11-03

and

unresolved

i tems

250,251/86-02-04,

250,251/85-40-01,

250,251/85-40-02,

250,251/85-40-34,

and 250,251/85-40-35.

EA 86-20, V.A.1

EA 86-20, V.A.2

EA 86-20, V.B.1

EA 86-20, V.B.2

EA 86-20, V.B.3.a

EA 86-20, V.B.3.b

closed

closed

closed

closed

closed

closed

(Closed)

EA 86-20,

V.A.l.: Licensee's

Failure to Incorporate

Vendor

Recommendations

for Compensating

Specific

Gravity

Readings, for

Temperature

and Level.

Inspection

Report

250,251/85-40

delineated

concerns

that

Plant

Operating

Procedure

(OP)

9604. 1,

D.C.

System - 'Periodic Tests

and

Maintenance,

did not provide adequate

instructions for compensating

specific gravity for temperature

and level.

Additionally, the

procedure

did not contain

acceptance

criteria for specific gravity

readings.

Procedure

OP 9604. 1 has

been cancelled

and

superseded

by

Procedure

O-SME-003.2,

approval

date

March 30,

1987,

125

VDC Station

Battery Monthly Maintenance.

O-SME-003.2 adequately

addresses

the

subject of compensating

specific gravity readings for temperature

and

level including acceptance criteria.

The

licensee

issued

On-The-Spot

Change

to procedure

4-0SP-201.3,

dated

May 28,

1987,

NPO Daily Logs to add instructional

guidance for

the

purpose

of calculating

the corrected

specific gravity values.

This calculation

provides

the

Nuclear

Plant Operator

(NPO) with

a

means

of properly verifying the specific gravity for the safety

related batteries

as required

by Technical Specification 4.8.2.b

and

interim Technical

Specification 3/4.8.2.l.a.

Additionally, the

licensee will conduct training to ensure

that the

aforementioned

calculations

are

performed correctly.

Based

on this information, the item is. closed.

This item also closes

part of violation 250,251/86-26-10.

(Closed)

EA 86-20, V.A.2.: Licensee

Failure to Adequately

Load Test

the Safety-Related

Station Batteries.

Inspection

Report

250,251/85-40

delineated

concerns

that

the

licensee's

testing of safety-related

station batteries

did not meet

the intent of specification

design

requirements

contained

in Plant

Change

Modification

83-05

(which

replaced

the

safety-related

batteries.)

Additionally, the testing

did not

meet

acceptance

criteria identified in section

8.2 of the

FSAR, which requires

the

batteries

to carry their expected

shutdown

loads, following a unit

trip and

loss of all

AC power for a period of approximately

one

hour, without battery terminal voltage falling below

105. volts D.C.

Procedure

O-SME-003.4,

dated

February 6,

1987,

125

VDC Station

Battery

Annual

Maintenance,

adequately

verifies that the safety-

related

station batteries

are

capable

of supplying

and maintaining

the actual

or simulated

emergency

loads for

a period of one hour.

The test

time criteria is in agreement

with the requirements

of the

FSAR.

A review of the

load profile specified

in .O-SME-003.4 to

simulate

emergency

loads

was not conducted

to determine

the accuracy

of the profile.

Based

on this information, the item is closed.

This item also closes

part of violation 250,251/86-26-10.

(Closed)

EA 86-20,

V.B. 1: Licensee's

Failure to Provide

Adequate

Documentation for the Justification of Continued

Operation with

a

Degraded Auxiliary Feedwater

(AFW) System.

EA 86-20,

V.B.1 documents

the licensee's

failure to provide adequate

documentation

for justification to allow operation without locating

missing

check

valve

parts

from the

degraded

AFW system.

The

licensee

has

revised Administrative Procedure

(AP) 0190.12.,

dated

February 24,

1987,

Nonconforming Materials,

Parts

or

Components

to

govern the scenario for a component of an existing operating

system

which is found to

be nonconforming.

If a nonconforming condition

exists,

a Plant Work Order

(PWO) shall

be issued,

and if an engineer-

ing specification is affected,

a Nonconformance

Report

(NCR) shall

be

issued.

Additionally, the revision requires

the guality Control

(gC)

department

to ensure

that appropriate

action is taken to resolve

the

NCR, including adding

gC hold points to the

PWO requiring

NCR

resolution prior to returning the component to operation.

Based

on this information, the item is closed.

This item also closes

part of violation 250,251/86-26-10.

(Closed)

EA 86-20,

V.B.2:

Failure to Establish

Measures

to Ensure

that Conditions

Adverse to guality and Nonconformances

are Promptly

Identified and Corrected.

Inspection

Report

250,251/85-40

delineated

concerns

pertaining

to

the licensee's

failure to adequately

control the design modification

process

for Plant Change Modification (PC/M) 80-77, Unit 3 Condensate

Storage

Tank Redundant

Level Alarms and

PC/M 80-71, Unit 4 Condensate

Storage

Level

Alarms and the various operating

procedures

resulting

from these

PCMs.

As

a result of these

concerns,

the licensee

has

revised Administrative Procedure

0190.15,

dated April 7, 1987, Plant

Changes

and Modifications, which should provide an increased

level of

control in the review, approval

and implementation of PC/Ms.

Based

on this information, the item is closed.

This item also closes

part of violation 250,251/86-26-10.

(Closed)

EA 86-20,

V.B.3.b:

Failure to Implement Procedures

which

Document Root Cause

Failures

on Safety-related

Equipment.

(Closed)

EA 86-20, V.B.3.a:

Failure to Implement Procedural

Require-

ments for Documentation of Post-maintenance

Testing.

Inspection

Report

85-40

delineated

concerns

pertaining

to

the

licensee's

failure to implement procedures

which call for documenta-

tion of root cause failures or to perform post-maintenance

testing.

In response

to these

concerns,

the licensee

has conducted

seminars

to

reiterate

to the maintenance staff the need for documenting

the root

cause

of a problem

on Plant

Work Orders

(PWOs).

The licensee

has

also

issued

Administrative Procedure

0190.28,

dated

May 29,

1987,

Post-maintenance

Testing,

which provides

guidelines for selecting

and

documenting

post-maintenance

testing

following completion of

maintenance

activities.

Review of completed

PWOs verified that the

maintenance

staff is performing post-maintenance

testing

and

docu-

menting root cause failures.

Based

on this information,

items

V.B.3.a

and

V.B.3.b are closed.

This item also closes part of violation 250,251/86-26-10.

Escalated

Enforcement

Action

(EA) 86-20, III:

Failure to Comply

With Technical Specification 3.8

and 3.4 Concerning,

Respectively,

Auxiliary Feedwater

System

and Safety Injection System Operability.

This

EA originated from violation 250,251/86-26-08,

which encompassed

previously identified violations 250,251/86-26-06

and 250,251/86-11-02

and unresolved

item 250,251/86-02-03.

EA 86-20, III.A

EA 86-20, III.B

closed

closed

(Closed)

EA 86-20, III.A:

Exceeding Limiting Condition for Operation

Due to Inadequate

Management

Controls in Properly Determining Opera-

bilityy

of the Auxiliary Feedwater

(AFW) System.

A nonconforming

condition with the auxiliary feedwater

pump steam

supply valves

was identified

on January

2,

1986

and

no action

was

taken until January 7,

1986.

Results of radiography

indicated that

the

steam

supply valves

had bent guide studs,

however,

no action

was

taken

which

led

to

an operability

concern, with the auxiliary

feedwater

system.

To resolve

these

concerns,

the licensee

implemented

Plant

Change/

Modifications

(PC/M)86-009 for Unit 4

and

86-011 for Unit 3.

The

PC/Ms replaced

a

number of valves in the system beginning with the

motor operated

steam

supply valves.

These

were changed

from solid.

wedge gate

valves

to globe valves.

Solid wedge

gate valves tend to

Q

o

leak,

are susceptible

to seat

erosion

and,

therefore,

are not the

best

choice

for steam

service.

Globe

valves

are

designed

to

throttle,

are

less

susceptible

to seat

erosion

and, therefore,

are

better suited for steam applications.

Additionally, new tilting disk

check valves

have

been installed

both upstream

and downstream of the

motor

operated

steam

supply

valves.

The existing

downstream

stopcheck

valve has

been

completely

removed while the upstream

stop

check

has

been

replaced

with

a manually operated

globe valve.

The

stop

check valves previously used in the system

are subject to disc

flutter under

low flow conditions. Tilting disc

check

valves

are

better suited for steam applications

and, therefore,

should respond

better under low flow conditions.

Based

on this information, the item is closed.

This item also closes

part of violation 250,251/86-26-11.

(Closed)

EA-86-20,

111.B:

Vio1ation of Technical

Specification

Concerning

the Operability of a Safety Injection Pump.

A violation of Technical Specification 3.4. 1.4 occurred in that Unit

3 start-up

was conducted

with only three of the required four safety

injection

pumps operable.

The fourth pump was inoperable

due to the

discharge

valves

being closed.

The discharge

valves

had

been closed

during

a

previous

maintenance

effort.

When

- maintenance

was

completed,

the

pump

was

tested

for operability

by

a flow path

established

through

a recirculation line.

After the test,

the

pump

was

declared

operable,

however,

the

discharge

valves

were

never

opened.

The operability test did not address

verification of valve

line-up.

Also the required plant equipment clearance

review prior to

start-up

was

inadequate

in that it failed to identify the safety

injection

pump discharge

valves

as being closed.

The licensee

has

included into Administrative Procedure

(AP)0103.4,

In Plant

Clearance

Orders,

a

common

equipment

clearance

log in

conjunction with separate

clearance

logs for Unit 3

and Unit 4.

Previously,

common clearances

were maintained

under

the Unit 3 log.

This

new process

should help expedite

the review process

as well as

assist

in identifying equipment

maintained

under

a clearance

order.

The licensee

also places

Technical

Specification

and safety-related

equipment

in the

Equipment

Out of Service

Log along with the

clearance

number.

This requirement

is delineated

in step 5.3.3 of

AP-0103.4,

In Plant

Clearance

Orders

as

well

as

step

8.5.3 of

AP-0103.2,

Responsibilities

of Operators

and Shift Technicians

on

Shift and Maintenance of Operating

Logs and Records.

The inspector

also

reviewed

General

Operating

Procedure

(GOP)-503,

Cold

Shutdown

to

Hot Stand-by.

Within this

procedure

there

are

requirements

that both Clearance

and Equipment Out of Service

Logs

be

reviewed.

Specifically step 4.3 under Precautions

and Limitations

requires

a review of the Clearance

Logs

be performed to insure that

safety related

components

are not on

a clearance

order. Additionally,

step

3. 1.4.8 of the

same

operating

procedure

requires

that the

Equipment Out of Service

Log also

be reviewed.

Based

on this information, the item is closed.

This item also closes

part of violation 50-250,251/86-26-08.

(Closed)

EA 86-20,

VI:

Failure to Promptly Identify Conditions

Adverse

to guality With Respect

to

Component

Cooling Water

Flow

Through

Residual

Heat

Removal

Heat

Exchangers,

Single

Failure

Concerns of an Intake Cooling Water Control Valve, and Resolution of

Component Cooling Water Problems for Safety .Injection Pumps.

This

EA

originated

from previously identified violations

250,251/86-26-01,

250,251/86-26-02,

and

250,251/86-26-03,

and

unresolved

items

250,251/86-10-03,

250,251/86-10-04,

and 86-18-03.

These

items were-

administratively closed since they were redundant

with this violation

and this violation was identified as 250,251/86-26-11.

EA 86-20, VI.A

closed

EA 86-20, VI.B

closed

EA 86-20, VI.C

closed

(Closed)

EA 86-20,-V1.A:

Failure to Promptly Identify and Correct

Conditions Adverse

To guality with Respect

to Component

Cooling Water

Flow through Residual

Heat Removal

Heat Exchangers.

Component cooling water

(CCW) flow through the residual

heat

removal

heat

exchangers

appeared

to

be below flow levels

assumed for in

the

accident analysis.

Component cooling water valves were subsequently

repositioned

from 30 to

100 percent

open.

The repositioning

was

completed with no evaluation

or testing

performed to determine

the

effects

on flow to other

components/systems

served

by component

cooling water system.

To fully address

the component cooling water system flow requirements

the

licensee

wrote

and

performed

two special

procedures.

These

special

procedures

were

used to balance

CCW flow.

Special

procedure

(SP)

86-11

was satisfactorily

completed

on Unit

4

on

May 11,

1986

as

noted

in Inspection

report 87-09,

under close

out of IFI

250,251/86-24-09.

Special

Procedure

(SP)

86-05

was also satisfac-

torily completed

on Unit

3

on March 18,

1986,

as

indicated

in

a

letter from the Office of Nuclear Reactor Regulation

(NRR), accepting

the test results

as valid.

Based

on this information, the item is closed.

This item also closes

part of violation 250,251/86-26-11.

(Closed)

EA 86-20,

Vl.B:

Single Failure

Concerns

of an Intake

Cooling Water Control Valve Failure.

Failure to take

prompt corrective action in evaluating

the safety

significance of a failure of an Intake Cooling Water

(ICW) valve to

close

on

a loss of power and/or it's control air supply resulting in

a

reduction

of

ICW flow to

the

component

cooling water

heat

exchangers.

To correctly identify and maintain adequate

ICW flow the licensee

has

made

changes

to the following procedures:

Off Normal

Operating

Procedure

(ONOP)

3408.1,

Intake Cooling

Water Malfunction

Step 5.2.1,

as listed under immediate operator actions,

requires

control valve CV-2201 to be isolated during

a design basis

event

concurrent with only one

ICW pump running.

This action assures

adequate

flow through the

component

cooling water heat exchang-

ers

by minimizing

ICW flow through

the turbine plant cooling

water heat exchangers.

3/4 EOP-E-0 Reactor Trip or Safety Injection

Step

10,

under the

response

not obtained

column with only one

ICW

pump

running,

requires

dispatching

personnel

to isolate

CV-2201 by closing the manual isolation valve.

This action will

have

the

same

end result

as listed previously under

Procedure

3408.1 Intake Cooling Water Malfunction.

3-0P-019,

Operating

Procedure

for the

Intake

Cooling Water

System

(ICW)

Attachment I,

page

6 of 10 requires

valve 3-50-406

CCW/ICW

bypass

around

Control

Valve

(CV) 2202 to be open.

CV-2202 is

then

shut

and

set

in the

automatic

mode for 110'F.

This

operational

line-up allows cooling flow to be maintained

through

the

component

cooling water

heat

exchanger

regardless

of the

posi tion of the control valve.

Based

on this information, the item is closed.

This item also closes

part of violation 250,251/86-26-11.

(Closed)

EA 86-20,

Vl.C:

Resolution of Component

Cooling Water

Safety Injection

Pump Cooling.

A piping error on Unit 4, Train A and Train

B component cooling water

(CCW) system

was identified by the licensee.

Procedural

controls in

place at the time excluded the use of Unit 4

CCW for safety injection

(SI)

pump cooling.

However, there were cases

noted while Unit 3 was

shut

down

and its component

cooling water system secured that Unit 4

CCW was

used to supply SI

pump cooling.

Because of the piping error,

this operational

line-up could have resulted

in the safety injection

pumps

being

inoperable

due to insufficient cooling to the

SI

pump

thrust bearings.

In response

to this, the licensee

completed

Plant

Change/Modification

(PC/M)83-008.

This

PC/M modified the piping

i

10

such that the flow reversal

and cross-train-connection

deficiencies

on Unit 4 have

been corrected.

Additionally, 3/4-0P-030,

Component

Cooling Mater System,

has

been

revised.

The procedure

requires

Uhit 3 to supply

CCM for SI

pump

cooling with Unit 4

shutdown.

Conversely,

with Unit 3

shutdown,

Unit 4

CCW will supply SI pumping.

Based

on this information, the item is closed.

The item also closes

part of violation 50-250,251/86-26-11.

4.

Unresolved

Items

0

No unresolved

items were identified during this inspection.

5.

Licensee Action on Previous

Inspector Identified Items

a.

(Closed)

IFI

250/84-25-01/251/84-26-01:

Inspector

Concerns

Pertaining

to Non-shift Licensed Operators

Performing the Functions

of Licensed Operator

on

a quarterly Basis.

IFI 84-25/84-26 delineated

concerns

that non-shift licensed operators

may not

be performing'he

functions of licensed

operators.

The

inspectors

reviewed

the list of non-shift licensed operators

against

shift

compliment

logs

to determine

that

the non-shift

licensed

operators

were

performing

the functions of an operator

or senior

operator

as required

by 10 CFR 55.31(e).

Based

on this information, the item is closed.

b.

(Closed)

IFI 250,251/85-22-10:

Completion of Commitments

to Train

Licensed

Operators

on the

Loss of Inverters

and Associated

Vital

Buses.

During 1985 the licensee

experienced

a series

of inverter trips and

the loss of associated

vital buses.

The corrective actions for these

trips. included operator training

on mitigating the loss of inverters

and vital buses,

training

on the

change

over to

new auto-transfer

inverters,

and replacement

of the failing inverters.

The

new,

more

reliable inverters

were installed

and the inspector verified that the

committed training was provided to licensed

operators

as follows:

On-shift training

was

provided

to shift licensed

personnel

between

June

28 and July 18,

1985.

Training was provided

as

an

interim corrective

measure

to ensure that operators

were

aware

of what

equipment

would

be lost with

each

inverter

and

associated

vital

bus

and

how to mitigate

the

resultant

transient.

The

inspector

verified that all licensed shift

personnel

completed this training.

11

The 1985-86 Licensed Operator Requalification Training, Cycle 4,

provided

a class

on the replacement

of the

120 volt AC inverters

and

the

operation

of the

new inverters.

Replacement

of the

inverters

was

completed

under Plant Change/Modification

(PC/M)83-117.

The

inspectors

reviewed

the

lesson

plans

associated

with this training

and

concluded

that the training appeared

adequate

to support the inverter change

over and operation.

The licensee

issued

several

Training Briefs associated

with both

the

loss

of

AC inverters

and

the installation of the

new

inverters in 1985.

The inspector

reviewed these training briefs

and

associated

attendance

lists," and this training

appeared

adequate

to meet the intended functions.

Based

on this information, the item is closed.

(Closed)

UNR 250,251/85-40-13:

Failure to Meet Commitment to Install

Adequate

DC Lighting to Support

Local

AFW Operations

During Shutdown

From Outside the Control

Room.

The licensee

had committed in 1981 to install adequate

DC lighting to

support

necessary

local Auxiliary Feedwater

(AFW) operations

during

periods

of control

room inaccessibility

'and

a loss of normal

AC

lighting.

During

a walkthrough of the Control

Room Inaccessibility

Procedure,

ONOP-103,

in 1985, it was determined that the installed

DC

lighting

was

inadequate

to

meet

this

previous

commitment.

In

response

to this deficiency,

the licensee installed

22 additional

DC

lights in the

AFW and nitrogen addition locations

in 1985.

These

additional

lights

were installed

under

Plant

Change/Modifications

(PCM);85-177

(Unit 3)

and 85-178 (Unit 4), Addition of Component

Lighting for

AFW System;

PCM 85-170, Install Unit 3

AFW Valve Access

Platform;

and

PCM 85-175, Nitrogen Station Additions and relocations.

A review of this additional

DC lighting by the inspector

and

a second

walkthrough

of

the

control

room inaccessibility

procedure

on

February 4,

1987,

indicated

that

the

additional

lighting

was

adequate.

Based

on this information, the item is closed.

(Closed)

IFI 250,251/85-40-16:

High

Radiation

Levels

in the

Auxiliary Feedwater

(AFW) Pump Area Following a

LOCA on Unit 3.

The licensee's

Post Accident Zone

Map indicated potential

very high

radiation levels in the

AFW area following a

LOCA on Unit 3 due to

shine

from the

personnel

hatch.

In the

event

an operator

was

required

to perform local

AFW operations

for Unit 4 during this

period,

excessive

radiation

exposure

could occur.

The licensee

has

revised

Off-Normal Operating

Procedure

7308.1,

Malfunction of the

Auxiliary Feedwater

System,

to contain

a "caution" regarding this

potential.

The

caution

statement

requires

that

Health

Physics

12

coverage

shall

be obtained prior to entering the

AFW area

during

a

LOCA on Unit 3.

Based

on this information, the item is closed.

(Closed)

UNR 250,251/85-40-25:

'Inspector

Concerns

Pertaining

to

Tubing Sections

of the Nitrogen

Backup to the Auxiliary Feedwater

(AFW) System Being Inadequately

Supported;

UNR 85-40-25 delineated

concerns that portions of the nitrogen backup

to

the

auxiliary

feedwater

supply

system

instrument air

were

inadequately

supported

as specified

by the licensees

specification

No.

5177-J711,

Rev. 2,

Design

Guide for Seismic

Class

I Instrument

Tubing Installation.

As

a result of these

concerns,

the licensee

contracted

with Bechtel

to perform

system

walkdowns

according

to

procedure

5177-499-G-001,

Rev. 2, Procedure for the Walkdown of Small

Piping

and

Instrumentation

Tubing.

This

walkdown determined

the

backup

nitrogen

system

to

be

operable.

Non-Conformance

Reports

(NCRs), including NCR-614-86

and 961-86,

were generated

to document

and

accept-as-is

or correct

the

existing field discrepancies.

Additionally, Plant

Change/Modification

(PC/M)85-175

and

85-176,

Nitrogen

Station

Additions

and

Relocations,

were initiated

to

relocate

the existing backup nitrogen bottle station for AFW control

valve instrument air and

add

new bottle stations for Units

3 and 4.

The

inspector

performed

a field survey to obtain

general

system

layout and confirm adequate

tubing support.

No discrepant

conditions

were observed.

Based

on this information, the item is closed.

(Closed)

IFI 250,251/85-40-28:

Review the

New Maintenance

Training

and the gualification Tracking System.

IFI 85-40-28 identified that the Maintenance

Department did not have

qualification cards

or on-the-job

(OJT) records

to ensure

that only

qualified personnel

were assigned

to perform tasks.

At present,

the

Maintenance

Department

is in the process

of completing task

sheets

for each

employee.

These

task sheets will be completed

(signed-off)

as

a result of either classroom training,

OJT performance

as judged

by a certified OJT observer,

or incumbent qualification based

on past

job

performance.

The

end result

is that

each

employee will be

identified as to which tasks that employee is presently qualified to

perform.

That

information will be

as

loaded

into the Training

Information Management

System

(TRIMS) computer.

All maintenance

task

sheets

are scheduled

to be completed

by July 31, 1987.

Although no time table

has

been established,

the licensee

intends to

interface

the

TRIMS computer with the Nuclear

Job Planning

System

(NJPS),

which is used

to track Plant

Work Orders

(PWO).

Such

an

interface

would permit identification on each

PWO of those

personnel

qualified to perform that particular task.

In the interim period,

a

13

manual

system will be

used

to track personnel

task qualifications.

Interviews with maintenance

supervision

indicated that plans for a

manual

system

have not been finalized, but a conscientious effort is

being made to institute

a workable system.

Concerning

maintenance

training,

the

licensee

began

a

formal

maintenance

training cycle in January,

1986.

The licensee

committed

to continuously

cycle

at least

12

percent

of 'the

mechanical,

electrical,

and

I8C personnel

through this training.

This should

result

in

a maintenance

individual receiving

40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of training

every

8 weeks or about

200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> annually.

Finally, the Training Department is scheduled

in September,

1987 to

submit

the

completed

Job

Task Analysis

Package

for Mechanical,

Electrical

and

ISC Maintenance

Departments

to

INPO for accreditation

of the Maintenance Training Program.

Based

on this information, the item is closed.

(Open)

UNR 250,251/85-40-29:

Review of Licensee's

Thermal

Overload

Size for Valve Operators

Inspection

Report

250,251/85-40

delineated

a

concern

over

the

apparent

difference

between

the manufacturer's

recommended

thermal

overload

size

and

the

size

chosen

by the

licensee

to satisfy

Regulatory

Guide 1.106.

Conversations

with licensee

personnel

indicated

that

they

are

developing

a

program

to review and, if necessary,

change

heater

sizes.

This

program

is

encompassing

a

review of applicable

Regulatory

Guides,

manufacturer's

data,

etc.,

and

is

not yet

complete.

Based

on this information, the item will remain

open until

the licensee's

review is complete.

(Closed)

UNR 250,251/85-40-30:

Insufficient Test Data

and Review of

Manufacturers

Calculations to Insure the Operability of (MOVs) 3-1403

and 4-1403

Steam Supply to the Auxiliary Feedwater

Pump.

'nspection

Report

85-40 delineated

a concern

over the'ccuracy

of

calculations

used

to derive the voltage. drop to

DC Motor Operated

Valves

(MOVs) 3-1403

and 4-1403.

The portion of the calculation in

question

was the current value.

The licensee's

calculation utilized

full load current

(8 amps),

wherein

the manufacturer

recommended

using the starting current value (53 amps).

Conversations

with licensee

personnel

indicate

new calculations

have

been

completed.

The values

used

in the calculation

were

53

amps

(starting current)

and

111 volts

DC.

This calculation

revealed

a

voltage available

to

MOVs 3-1403

and 4-1403 of greater

than

90 volts

DC which is within the manufacturer's

requirements.

14

Based

on this information, the item is closed.

(Closed)

UNR 250,251/85-40-33:

Review Apparent Conflict Between

Technical Specification 4.8.2.b

and Vendor Recommendations

UNR 85-40-33

delineated

concerns

that

the Technical Specification 4.8.2.b,

which requires

the licensee

to perform a monthly equalizing

charge

on the safety-related

batteries,

was in conflict with the

recommendations

contained within Gould-GNB maintenance

manual.

A

review of the telephone

conference

memorandum

dated January

10, 1986,

between

representatives

of Gould

and

the

licensee

indicate that

monthly equalizing

charges will only minimally shorten

the expected

battery life. It should

be noted'hat

the licensee

has

submitted

by

letter dated

November 28,

1986, to the

NRC a Technical Specification

change to provide for an as-needed

equalizing charge.

Based

on this information, the item is closed.

(Open) 250,251/85-40-38:

Determine

Adequacy of Licensee's

Fail Safe

Testing for Auxiliary Feedwater

Flow (AFW) Control Valves

Inspection

Report 250/85-40 delineated

a concern over the licensee's

present

means

of fail safe testing for the

AFW system flow control

valves.

Present

means of testing is for the valves to be driven open

and then closed,

using the control switch.

The licensee

states

that

by using the control switch, the air supply to the valve is isolated

and, thereby, satisfies

the requirements

of ASME XI-IWV-3415.

Pending further review of this item in the

NRC Region II office, this

item will remain open.

(Closed)

UNR 250,251/86-18-01:

Lack of Documentation

to Indicate

Formal Operability Evaluation

(Closed)

IFI 250,251/86-18-02:

Lack of Adequate Criteria for

a

Safety Evaluation Determination

UNR 86-18-01

delineated

concerns

that the licensee's

operability

evaluation

should

be formally documented

with the bases

for those

results.

Additionally,

a

mechanism

should

be in place to notify

plant, management

of the significance of evaluations

which may effect

plant operability.

IFI

86-18-02

delineated

concerns

that

the

licensee

had

not

established

adequate criteria to determine

a need to perform

a safety

evaluation.

Review of Open

Item Review Sheets for the Select

System

Assessment

Program

noted the addition of extensive

comments

in the Engineering

Evaluation section which elaborated

on the

need to perform

a safety

evaluation

or justification for not performing

these

evaluations.

e

15

Additionally, concerns

pertaining

to the lack of formal procedures

and

documentation

in the

Phase

1 systems

review process

led to the

developement

of the following procedures:

PTN-EP 5.2,

Rev. 0,

Comprehensive

System

Review

SEG

Phase II,

which identifies

the

actions

to

be

taken

by the

Safety

Engineering

Group

members

during their special

comprehensive

review of the Select

Systems.

PTN-EP 3.2,

Rev. 0, Control of the Integrated

Tasks

Punchlist

for Select

Systems

PTN 3

5 4., which governs

the implementation

and maintenance

of the Integrated

Tracking System,

including the

criteria

which shall

be

met for items

to

be

added

to the

.punchlist.

PTN-EP

3.1,

Rev. 0,

Preliminary

Engineering

Assessment

of

Reportability,

which establishes

the

requirements

for the

engineering

review

and

evaluation

of

items

identified

by

Requests

for Technical

Assistance.

These evaluations

shall

be

performed to determine

the potential

safety significance of all

open items, to establish

the priority for resolution of the open

items, to identify the

need for a detailed

safety assessment

by

Engineering

and to identify a plan of action for close

out of

- the items.

Additional

engineering

procedures

were

developed

to

govern

engineering

safety

assessments,

initial engineering

assessments

of

operability and the processing of requests for technical

assistance.

Based

on

the

above

information,

items

250,251/86-18-01

and

250,251/86-18-02

are closed.

1.

(Closed)

IFI 250,251/86-18-05:

Need

to

Develop

and

Implement

Corrective Action Program for Motor Operated

Valves

(MOVs)

IFI 86-18-05 delineated

concerns

pertaining to the licensee's

need

'to

complete

and

implement

a

work plan to correct

MOV problems.

Specifically, the

MOV's addressed

were MOV-3-750 and 3-751, Residual

Heat

Removal

(RHR) isolation valves.

The work plan

was required to

adjust the

open

bypass

switches

to prevent inadvertent

torque switch

trip during valve unseating.

The licensee

has

in place,

Plant

Change/Mofification

(PC/M)

Packages86-168

and

86-169.

These

packages

were developed

by the licensee's

Engineering

Department

and

Plant Nuclear Safety Cormittee

(PNSC)

approved

on February

19, 1987.

During the recent refueling outage,

PC/M 86-168

was

completed

on

Unit 3 while PC/M 86-169 is scheduled for completion

on Unit 4 during

the next refueling outage.

This item will be tracked

by the'esident

inspectors.

Based

on this information, the item is closed.

16

(Closed) IFI 250,251/86-18-09:

Control Over Plant Scaffolding.

The licensee

had not maintained

adequate

controls over erection

and

dismantling of plant scaffolding.

This lack of control resulted in

numerous

problems

including erection

over redundant

components

of

safety-related

systems,

interference with valves

and instrumentation,

attachment

to safety-related

components

and conduit,

interference

with emergency

operations

and access,

and the failure to promptly

remove the scaffolding

when related

work was completed.

In addition

the

control

of scaffolding

erected

by plant

personnel

differed

significantly from the

control

over scaffolding

erected

by the

Construction

Organization.

The

licensee

has

made

significant

improvements

in the controls over plant scaffolding.

Administrative

Procedure

O-ADM-012, Scaffold

Control,

and

Plant

Construction

Administrative Procedure

ASP-29, Control of Construction Scaffolding,

have

been

revised

and

upgraded

to provide

these

added

controls.

These

procedures

insure that plant

and construction

scaffolding are

carefully planned

and

coordinated

with the Operations/Maintenance

Coordinator or Nuclear Watch Engineer,

and that scaffolding:

- is fire retardant

- does

not block equipment or component

access

- does not hinder equipment or component operation

- is not attached

to components,

equipment,

piping, conduit, or

security barriers

- does not create conditions where personnel

working in the area

would cause

unwanted activation of valves or switches

- does not interfere with area lighting

- is removed within 14 days of work completion

All scaffolding is provided with control

number

and identification

tag

and is inspected

on

a monthly basis to ensure

compliance.

Based

on this information, the item is closed.

(Closed)

IFI 250,251/86-18-10:

Configuration Control

Concerns

Over

the Procedural

Requirement

of Valve Lineup Versus the'ctual

Field

Position.

IFI 250,251/86-18-10

delineated

concerns

pertaining to discrepancies

between

actual

valve position

and the operational

line-up required

by

3/4-0P-68,

Containment

Spray

System,

Administrative Procedure

(AP)

0103.5,

and the system

drawing for valves

942V and

942W, containment

spray

pumps

3A, 3B,

4A and

4B discharge

header drains.

The inspector

reviewed 3/4-0P-68,

Containment

Spray

System for the above mentioned

valves

and

compared

the procedurally required position against

the

system

drawing

5610-T-E-4510,

revision

71.

No discrepancies

were

noted.

Since the original inspection,

AP-0103.5

has

been cancelled

and

superseded

by O-ADM-205, Administrative Control of Valves,

Locks

and Switches.

0-ADM-205 was reviewed for the above mentioned

valves

17

and

compared

against

both

the

system

drawing

and 3/4-0P-68,

once

again

no discrepancies

were noted.

Based

on this information, the item is closed.

(Open)

UNR 250,251/86-18-13:

Lack of Procedures

for Loss of

DC

Power.

UNR 86-18-13

delineated

the licensee's

lack of procedures

for the

loss of DC power.

The licensee

is developing

an interim procedure to

be

used

in the event

a

125v vital

DC

Bus is lost

due to battery

charger failure and

a subsequent

battery failure.

For the long term,

a procedure will be developed,

following completion of a Request for

Engineering

Assistance

(REA), which will direct operators

how to

respond

to loss of indication

and control following a loss of DC.

The

REA associated

with this procedure

should

be expedited

due to

lessons

learned

from loss of

DC at other facilities.

The licensee

has

projected

a completion

date of September

15,

1987 for these

procedures.

This item will remain

open pending completion of these

procedures.

(Closed)

UNR 250,251/86-19-03:

Failure to Provide Requalification

Exams Within Required

Time Period

UNR 250,251/86-19-03

delineated

the licensee's

failure to provide

a

requalification

exam retest within 60 days of the previous

examina-

tion date

as required

by Administrative Procedure

(AP) 0301 Licensed

Operator Requalification

Program.

The Training Superintendent

issued

a policy statement

on

May 19,

1986,

regarding

the

examination

process.

That policy statement

set forth definitive retest

time

restrictions

and directed actions

to be taken if a licensed operator

failed

a requalification

examination.

AP-0301

was

subsequently

revised

and upgraded

on February

19,

1987.

Based

on this information, the'item is closed.

(Closed)

IFI 250,251/86-24-01:

Inspector

Concerns

Pertaining to Post

Accident Sampling

System

(PASS) Calibrations

IFI 86-24-01 delineated

concerns

that the licensee

had not performed

the required calibrations for the

PASS inputs for the nuclear

data

computer

channels.

The

licensee's

Preventive

Maintenance

(PM)

program established

the following PMs for the

PASS:

-PM-94005,

PASS Dissolved

Oxygen Analyzer

-PM-94006,

PASS Liquid pH Analyzer

-PM-94007,

PASS Hydrogen Analyzer

-PM-94008,

PASS Sample

Pressure

18

-PM-94009,

PASS

Gas

and Liquid Flow Monitor Calibration

-PM-94010,

PASS Inlet and Cooled

Sample Temperature

Monitor

Calibration

The aforementioned

PMs were completed to satisfy the concerns of IFI

250,251/86-24-01.

The aforementioned

PMs are currently overdue

as

a

result of the current refueling outage

instrumentation

calibration

back'log.

The hydrogen analyzer

and the gas

and liquid flow monitors

are currently the subject of Plant

Change Modification (PC/M) 84-70,

Post Accident Sampling System

Long Term Modifications.

The intent of

this

PC/M is to enhance

PASS operation

and to provide

a higher

on-line reliability factor.

Upon completion of the

PC/M,

PMs

PM-94007

and

PM-94009 will

be

revised

- to reflect

the

new

instrumentation

calibration

requirements

and all

PASS calibrations

will be performed.

Based

on this information, the item is closed.

(Closed)

UNR 250,251/86-46-02:

Tracking of Corrective Actions to

Findings of Licensee

Internal Training Assessment.

UNR 86-46-02

delineated

concerns

pertaining

to

the

licensee's

findings during

an internal training assessment.

In 1986,

a

team

consisting of representatives

from the licensees'orporate

Staff,

Training Staff,

and guality Assurance

Department,

conducted

an

assessment

of the Turkey Point Training Program.

The assessment

was

conducted

against

the requirements

of the

NRC, gA, and

INPO.

This

internal training assessment

identified

165 deficiencies

related to

the

above criteria.

Each of these

specific

deficiencies

was

identified as

an action item under

a corrective action

program.

At

the time of this closeout

inspection,

the licensee

had completed the

corrective

actions for in excess

of 140 of the

165 action items.

The

remaining

items to

be completed

were primarily enhancements

to the

training program or related to standardization

between

the licensee's

two nuclear facilities.

In addition, the inspector verified that the

48

items

identified

by the

licensee

as

being

related

to

NRC

requirements

had

been

completed.

The

adequacy

of the corrective

action

has

been

reviewed

by

the

licensee's

guality Assurance

Department.

Based

on this information, the item is closed.

(Closed)

IFI 250,251/87-07-01:

Resolution of Training Records

and

Files

Involving

the

Recertification

of guality

Control

(gC)

Inspectors.

IFI 87-07-01

delineated

concerns

pertaining

to the

licensee's

inadequate

maintenance

of records

and documentation for the periodic

recertification of gC inspectors.

The licensee's

corrective actions

involve the utilization of Enclosure

2 to Administrative Procedure

O-ADM-971, Certification of guality Control Inspectors,

to document

19

the recertification

of

gC inspectors.

Recertification will be

documented

under

the

"Basis for Certification" section

of this

enclosure,

by indicating "continued acceptable

performance

during the

reporting period".

This

method of recertification

appears

to be

adequate

providing that the period of acceptable

performance

was in

the

same inspection

area

as the recertification.

Based

on this information, the item is closed

t.

(Closed)

UNR 250,251/87-07-02:

Implementation of Revised

Required

Reading

Program

and Resolution of Outstanding

Required

Reading Items.

UNR 87-07-02 delineated

concerns

pertaining to the licensee's

revised

required

reading

program

and resolution of the backlog of required

reading

items.

NUREG 0737,

Item I.C.5, requires that operational

experience

feedback

information

be provided to operations

personnel

on

a regular basis,

and that this information be screened

to prevent

obscuring priority information.

This item was

opened

because

the

licensee

was not screening this information and the large

volume of

information being

provided

appeared

to be contributing to untimely

and

inadequate

reviews

by operations

personnel.

The licensee's

corrective actions to this item have included:

Establishment

of

a

revised

operational

experience

feedback

program

by the Training Department.

This program requires

the

Training Staff to screen this information including the numerous

procedure revisions resulting from the Procedure

Upgrade

Program

(PUP),

to. ensure

only relevant

information is forwarded to

operators.

The inspectors

reviewed this process

and noted that

the volume of material

had decreased

significantly.

Upgrading

procedural

controls

over

the

documentation

and

timeliness

of operational

experience

feedback

reviews.

The

Training

Report

Cover

Letter

included

in the

procedures

controlling licensed

operator,

non-licensed

operator

and Shift

Technical

Advisor (STA) training requires that each individual

review the material

and sign the cover letter within 13 weeks of

issuance.

In addition,

the

procedures

prohibit an individual

from assuming shift responsibilities if he or she is greater

than

13 weeks behind

on this required reading.

Removal of the backlog of required reading that had accumulated

in the control

room under

the

previous

program.

This large

volume of backlog

information is in the

process

of being

screened

by the Training Staff.

Safety-related

and relevant

information contained

in this

backlog

is

being

provided to

operators

under

the

revised

program and/or

incorporated

into

requalification training.

Based

on this information, the item is closed.

20

Although

the

licensee's

corrective

actions

to

the

programmatic

controls

over

operation

experience

feedback

training

appeared

adequate

to close

the

open

item above,

the implementation of this

training

was

determined

to be

inadequate.

The licensee

implements

the

requirements

of

NUREG 0737

Item I.C.5

through

a

revised

operational

experience

feedback

required

reading

program.

The

procedures

which

implement this

program; Administrative

Procedure

(AP) 031,

Licensed

Operator

Requalification

Program,

and

AP 0303,

Non-Licensed

Operator Initial Training

and Requalification

Program,

require that all licensed

and nonlicensed

operators

shall

review and

acknowledge

this material within 13

weeks of distribution.

These

procedures

further require that

a licensed

or nonlicensed

operator

who is greater

than the

13 weeks

delinquent shall

not

assume unit

responsibility.

Additionally, Operations

Surveillance

Procedure

200.1,

Schedule of Plant Checks

and Survei llances,

requires

the Plant

Supervisor - Nuclear

(PS-N) to ensure all shift personnel

training

reports

(operational

experience

feedback)

are

up-to-date

on

each

8-hour shift.

Contr ary to the

above,

the inspectors

determined

on June 7,

1987,

that four licensed

operators

had failed to review and

acknowledge

material

dated

March 24

and

March 27,

1987;

greater

than

a 13-week

period.

These

licensed

operators

had

been

permitted to assume unit

responsibilities,

and at the time of the inspection

two were assigned

to the

day shift and

two to the night shift.

In addition,

a large

numbei

of non-licensed

operators

were greater

than

13 weeks delin-

quent

on

one or more training reports

dating

back to January

1987.

These

non-licensed

operators,

including two who had not reviewed

any

of the material

since January,

had also

been permitted to assume unit

responsibilities.

The inspectors

notified the licensee

that they

were

in continuing

noncompliance

with their approved

procedures

covering operational

experience

feedback.

In response,

the licensee

provided training

and

ensured

that all

licensed

and

nonlicensed

operators

were within the

13-week

review period prior to assuming

unit responsibility.

Subsequently,

the inspectors

determined that the licensee's

guality

Assurance

(gA) Department

had issued

a finding in this

same area.

On

June

23,

1987,

gA issued

Corrective Action Request

(CAR)87-028,

Operator

Review of Training Reports,

Repeat

Noncompliance.

This is

listed

as

a repeat

noncompliance

because

there

were two previous

gA

findings in the

same area.

CAR 86-783,

dated

December

10, 1986, also

cited that licensed

and nonlicensed

operators

were in noncompliance

with procedures

in that

they were

assuming

unit responsibilities

while greater

than

13 weeks delinquent

on Training Reports.

Manage-

ment's

response

to the

CAR, as detailed in PEN-PMN 87-027, indicated

that the Night Order

Book would

be utilized to reemphasize

to the

PS-Ns

to

ensure

licensed

and

nonlicensed

operators

comply with

procedures

and time limits on Training Reports.

I'n addition, it was

21

indicated

that discussions

were

underway with

PUP to

reduce

the

volume of required reading.

gA determined this management

response

to

be

inadequate,

as

detailed

in

CAR 86-783,

for the following

reasons:

No scheduled

completion date

was assigned.

The

deficiencies

regarding

nonlicensed

operators

were

not

addres'sed.

Both licensed

and nonlicensed

operators

continue to assume unit

responsibility without reviewing training reports

as required

by

procedures.

Management's

response

to

CAR 86-783 indicated that all training was

completed

by January

23,

1987.

In addition,

two corrective actions

were identified including

(1)

the

streamlining

of the training

reports

by the Training Department,

and

(2) increased

awareness

as

implemented

by the Operations

Department.

During

an inspection

in February

1987,

(250,251/87-07),

inspectors

noted that the licensee

had not implemented this proposed

screening

process

for Training Reports,

and

= that

due to the large

volume,

operators

continued

to

be delinquent

in reviews.

In response

to

Unresolved

Item 87-07-02,

the

licensee

implemented

this

proposal

screening

process

which

reduced

the

volume of required

reading

considerably.

Despite

the

previous

gA and

NRC findings,

and

the

revision to the program,

CAR 87-028 noted

on June 23,

1987, that both

licensed

and non-licensed

operators

were in nonconformance

with the

procedures

in assuming

unit responsibility while greater

than

13

weeks

delinquent.

This

CAR again specifically requested

management

not to allow the

delinquent

operators

to

assume

responsibility.

Despite this request,

the inspectors

determined

on July 7, 1987, that

both licensed

and nonlicensed

operators

who were more than

13 weeks

delinquent

on Training

Reports

were

continuing

to

assume

unit

responsibility.

10 CFR 50 Appendix

B Criterion

XVI requires

that

identified deficiencies

be

promptly corrected.

This failure to

adequately

implement the requirements

of

NUREG 0737 Item I.C.5, to

implement

approved

procedures

and to take

prompt corrective action

will be

a violation (250, 251/87-32-01).

(Open)

IFI

250,251/87-07-03:

Generation

of Electrical

Breaker

Setpoint

Document.

IFI

87-07-03

delineated

concerns

pertaining

to the

licensee's

generation

of an Electrical

Breaker Setpoint

document.

The Request

for Engineering

Assessment

(REA) is

scheduled

for February

5

August 8,

1988.

Pending

completion of the

REA

and

subsequent

Setpoint

Document development,

this will remain

an open item.

22

(Closed)

UNR 250,251/87-09-01.

Excessive

Overtime

By Operations

Personnel.

UNR 87-09-01

delineated

concerns

pertaining to excessive

overtime

by operations

personnel.

This

item is administratively closed.

Corrective

action

to

be

tracked

under

Notice

of Violation,

250,251/87-24-01

dated

June 30, 1987.

(Closed)

UNR

250,251/87-09-02:

Utilization

of.

Nonqualified

Instructors to Teach

Systems

and Integrated Plant Response.

UNR 87-09-02 delineated

concerns

pertaining to the licensees

use of

nonqualified

instructors

to

teach

systems

and

integrated

plant

response.

NUREG 0737,

items I.A.I.2

and I.A.2.3, requires

that

instructors

who

teach

systems,

integrated

plant

response,

or

simulator to licensed

individuals,

demonstrate

their proficiency

through

successful

completion of

an Senior Reactor

Operator

(SRO)

level examination.

Primarily due to a high failure rate of licensed

instructors

on

NRC requalification

examinations,

the

licensee

had

experienced

a shortage

of qualified licensed

operator instructors.

As

a result,

the licensee

had,

on occasion,

utilized instructors

to

teach

the areas

referenced

above

who had failed

NRC requalification

examinations,

who were

non-licensed,

and contract instructors

who

were not certified to teach

these

areas

or who had not received

any

site specific training.

The

licensee

has

taken

the

following

corrective actions:

r

Prohibited

SRO licensed instructors

who have failed

NRC requali-

fication examinations

from teaching

licensed

operators until,

they successfully

complete

on

NRC examination.

Eliminated contract instructors

who were not commercially

SRO

licensed

from the licensed operator

and licensed requalification

training programs.

Contracted

an'dditional

15 instructors,

all of

whom

were

previously

SRO licensed

on commercial facilities.

Implemented

a five week site specific

systems

training course

for contract

instructors.

The

inspector

reviewed

a matrix

designed

to ensure that contract instructors

complete

each area-

of training,

and that they are not utilized to teach

a system or

area prior to receiving the training.

This matrix appeared

to

provide

adequate

interim controls

over contract

instructors

until procedures

can

be developed

and implemented.

Based

on this information, the item is closed.