L-80-412, Forwards Steam Generator Insp Results from Current Outage. Results Show No New Phenomena & Verify General Denting Pattern within Predictable Limits Consistent W/Previous Insp.Requests Permission to Return to Full Power Operation

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Forwards Steam Generator Insp Results from Current Outage. Results Show No New Phenomena & Verify General Denting Pattern within Predictable Limits Consistent W/Previous Insp.Requests Permission to Return to Full Power Operation
ML17340A507
Person / Time
Site: Turkey Point 
Issue date: 12/18/1980
From: Robert E. Uhrig
FLORIDA POWER & LIGHT CO.
To: Eisenhut D
Office of Nuclear Reactor Regulation
Shared Package
ML17340A508 List:
References
L-80-412, NUDOCS 8012220301
Download: ML17340A507 (6)


Text

REGULATORY

'ORMATION DISTRIBUTION SY 4 (RIDS)

ACCESSION NBR:8012220301 DOC ~ DATE: 80/12/18 NOTARIZED:

NO FACIL:50-251 Turkey Point Plant~

Unit 4~ Florida Power and Light C

AUTH BYNAME AUTHOR AFFILIATION UHRIGg R,E ~

Florida Power L Light Co, RECIP ~ NAME RECIPIENT AFFILIATION EISENHUT,D.G.

Division of Licensing DOCKET 05000251

SUBJECT:

Forwards steam generator insp results from current outrage.

Results show no new phenomena 8 verify general denting pattern within predictable limits L consistent w/previous insp.Requests permission to return to full power operation, SB~

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DISTRIBUTION CODE:

A001S COPIES RECEIVED:LTR ~ ENCL SIZE ~

TITLE: General Distribution for af ter Issuance of Oper ting License NOTES:

RECIPIENT ID CODE/NAME ACTION:

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FLOAIDAPOWER 4 LIGHTCOMPANY December 18, 1980 L-80-412

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C/1 Office of Nuclear Reactor Regulation Attention:

Mr. Darrell G. Eisenhut, Director Division of Licensing U.

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Nuclear Regulatory Commission Washington, D.C.

20555 r4 ~

Dear Mr. Eisenhut:

Re:

Turkey Point Unit 4 Docket No. 50-251 Steam Generator Ins ections The results of the Turkey Point Unit 4 steam generator inspections conducted during the current outage are attached.

The inspections which were performed in accordance with Turkey Point Unit 4 operating license DPR-41 showed no new phenomena and verified that the general pattern of denting in Unit 4 is within predictable limits and consistent with previous inspections of the Turkey Point Units.

The general criteria applied for steam generator inspections and preventive plugging are the same as previously applied to Turkey Point Units 3 and 4.

This approach provides reasonable assurance of steam generator tube integrity such that safe operation of the unit during normal full power operation and during hypothetical accident conditions is assured for an operating period in excess of six equivalent full power months.

Therefore, the implementation of thi s program with the resulting preventive plugging, enables continued safe full power operation of Turkey Point Unit 4.

Total steam generator tube plugging at the conclusion of the current outage will be approximately 23.8X.

This is conservatively bounded by the 25K tube plugging ECCS analysis.

The results of this inspection and the preventive tube plugging program have been reviewed by the Turkey Point Plant Nuclear Safety Committee and the Florida Power 8 Light Company Nuclear Review Board.

They have concluded that based on the inspection results, the implemented plugging pattern, and previously submitted

analyses, that the return of Turkey Point Unit 4 to full power operation for at least six equivalent months does not involve an unreviewed safety question.

In accordance with condition D.l of operating license DPR-41, Florida Power 8

Light Company requests permission to return Unit 4 to power operation for a period of six equivalent full power months.

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Darrell G. Eisenhut Office of Nuclear Reactor Regulation Page 2

Based on our current schedule, we could be ready to resume power operation by January 11, 1981.

l<e will keep you advised of any significant changes.

Me have determined that this is a Class III request in accordance with 10 CfR 170.

Accordingly, a check for $4,000 is enclosed.

Very truly yours, o ert E. Uhrig Vice President Advanced Systems 8 Technology REU/RJA/ras Attachment cc:

J.

P. O'Reilly, Region II Harold F. Reis, Esquire

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